ML18016A242

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Insp Rept 50-400/97-10 on 970914-1025.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support
ML18016A242
Person / Time
Site: Harris 
Issue date: 11/20/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18016A239 List:
References
50-400-97-10, NUDOCS 9712040078
Download: ML18016A242 (25)


See also: IR 05000400/1997010

Text

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U. S. -NUCLEAR REGULATORY COMMISSION

REGION II

Docket No:

License

No:

50-400

NPF-63

Report

No:

~ ~

50-400/97-10

Licensee: .....:

Carolina

Power

8 Light (CP8L)

t

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~

Faci 1 ity

I

I

Shearon Harris Nuclear Power Plant, Unit 1

Location:

5413 Shearon Harris Road

New Hill. NC 27562

Dates:

September

14 - October 25,

1997

Inspectors:

J.

Brady, Senior

Resident

Inspector

G. MacDonald, Project Engineer

(Sections.M8.2,

El. 1,

E8.1)

Approved by:

M. Shymlock, Chief. Projects

Branch 4

Division of Reactor

Projects

97i2040078 97ii20

PDR

ADOCK 05000400

8

PDR

EXECUTIVE SUMMARY

Shearon Harris Nuclear

Power

Plant, Unit 1

NRC Inspection

Report 50-400/97-10

This integrated

inspection included aspects

of licensee operations,

maintenance,

engineering,

and plant support.

The report covers

a 6-week

period of resident inspection; in addition, it includes the results of

announced

inspections

=by a regional projects inspector

.

~0erati ons

~

Operations

per formance during the period was acceptable.

(Section 01.1)

~

Self-assessment

activities were acceptable.

The root cause

investigation

and Plant Nuclear, Safety Committee discussion

related to

the turbine-driven auxiliary. feedwater

pump

(TDAFWP) forced outage

was

good.

(Section 07.1)

P

~

A violation was identified for Failure to Establish

and Implement

Operating

and Surveillance

Procedures.

Three examples

were identified:

1) opening the feed regulating valves prior to opening the associated

block valves,

2) not placing

a second

feedwater

pump in service at the

required point causing

a turbine runback,

and 3) failing to establish

adequate

procedures for when to place

a second

feedwater

pump in service

and when

a turbine runback occurs.

(Section 08. 1)

Maintenance

Maintenance

and surveillance activities observed

were being properly

conducted.

Maintenance

and Operations

personnel

performing the

surveillances

were appropriately sensitive to potential

problems

and

appropriately performed peer checking to identify potential

problems

before they impacted plant operations.

(Sections Hl.1 and M2.1)

~

A noncited violation was identified for failure to establish

and

implement

TDAFWP Maintenance

procedures.

Two examples

were identified:

1) failure to follow a maintenance

procedure for installation of the

TDAFWP coupling.

and 2) failure to establish

an adequate

procedure for

gasket cutting and assembly of the

TDAFWP.

(Section

H8. 1)

~

A fourth example of the Failure to Establish

and Implement Operating

and

Surveillance

Procedures

was identified for deadheading

the

TDAFWP.

(Section H8.1)

En ineerin

In general,

Engineering acti vities were being adequately

conducted in

accordance

with requi red procedures.

A noncited violation was

identified for the unapproved

extension of a temporary modification due

date.

(Section El. 1)

Communications within engineering

management

related to the

TDAFWP

needed

improvement.

(Section

E7.2)

~PI tt

The control of contamination

and dose for the site was good and was

attributable to good teamwork between the various departments.

(Section

R1. 1)

1

Emergency

Preparedness

activities, in general.

were adequately

'onducted.

(Section Pl. 1)

The performance of Security and Safeguards

activities were good.

(Section Sl.l)

I

Fire Protection activities were being adequately

conducted.

(Section'1.1)

IP

Re ort Details

Summar

of'lant Status

Unit 1 began this inspection period at 100 percent

power.

The unit remained

at essentially

100 per cent power for the rest of the period.

01

Conduct of Oper ations

01.1

Gener al

Comments

I. 0 erations

a.

Ins ection 'Sco

e

71707

The inspectors

conducted

frequent reviews of ongoing plant operations

including plant simulator training activities.

Simulator activities

were observed during the, emergency exercise

and are also addressed

in

Section Pl.l.

b. Observations

and Findin s

,. In general.

the conduct of operations

was professional

and safety-

conscious.

Routine activities were adequately

performed.

Operations

shift crews were appropriately sensitive to plant equipment conditions

and maintained

a questioning attitude in relation to unexpected

equipment

responses.

Abnormal

and emergency activities observed during

observation of plant simulator training was good.

c.

Conclusions

Operations

performance during the period was acceptable.

02

Operational

Status of Facilities and Equipment

02.1

En ineered Safet

Feature

S stem Walkdowns

71707

The inspectors

used Inspection

Procedure

71707 to walk down accessible

portions of the following ESF systems:

~

Control

Room Ventilation (FSAR Sections

9.4. 1 and 7.3. 1)

Equipment operability, material condition,

and housekeeping

were

acceptable

in all cases.

Several

minor discrepancies

in System

Description SD-173, Control

Room

HVAC System,

Revision

6 were brought to

the licensee's

attention.

The inspectors identified no substantive

concerns

as

a result of these

walkdowns.

07.1

Quality Assurance in Operations

Licensee Self-Assessment

Activities

Ins ection Sco

e

40500

During the inspection period, the inspectors

reviewed multiple licensee

self-assessment

activities, including:

I

~

Plant-Nuclear Safety Committee

(PNSC) meetings

on September. 17,-

1997; September.25,

1997October

10, 1997,

and October 22,

1997;

~

.

~

-

p

f II(

~ I

~

.

Nuclear Assessment

Section Audits on Radwaste

Shipping

(HNAS97-134), Operations

(HNAS97-109),

and Corrective Action (HNAS97-151);

Obser vations

and Findin s

~

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II

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The inspector considered

the root cause analysis for the turbine-driven

auxiliary feedwater

pump

(TDAFWP) forced outage

and the

PNSC meeting

(September

25,

1997) discussing the root cause analysis

good.

There was

considerable

discussion

at the

PNSC meeting concerning the broad

implications of the overall problems associated

with the

TDAFWP forced

outage

and recovery efforts.

The

PNSC discussed

the inspector 's

observations

documented in Inspection Report 50-400/97-09.

section 01.2

and Ml.2.

The observations

included

common ties between the operations

events

and recent training weaknesses

identified during initial licensed

operator qualification exams.

and also with recent requalification

failures.

These aspects

were included in the cor rective actions for

condition report

(CR) 97-04094

and involved development of skills

remediation plans for some of the recent initial licensed class

and

revision of the instant senior

reactor operator

(SRO) program to

incorporate

lessons

learned.

An additional observation

from the 97-09

Inspection Report, in relation to generator

synchronization

problems,

was also included in the corrective actions for

CR 97-04094.

PNSC

discussions

revealed that the plant and simulator do not perform.

similarly on synchronization.

Participation in the

PNSC by the members

was good.

In addition, the chairman did a good job of controlling the

flow of the meeting.

The specific issues

are discussed

in Sections

08. 1

and M8.1.

Conclusions

Self-assessment

activities were acceptable.

The root cause

investigation

and

PNSC discussion

related to the

TDAFWP forced outage

was good.

08

08.1

.3

Hiscellaneous

Operations

Issues

(92901)

Closed

URI 50-400/97-09-01:

TDAFWP Forced Outage

Problems

This item was left unresolved

based

on review of the root, cause

determination-for the

TDAFWP problems.

The inspector reviewed'the root

cause investigations for condition reports

(CR) 97-04094.

97-04109.

97-04112-1.

LER 50-400/97-022-00.

and attended

the

PNSC meeting that:

discussed

the root cause analysis

for these 'condition reports

on

(September

25, 1997).

Condition report 97-04109 dealt with feedwater regulating block valves

not being opened prior to opening..the

feedwater,regulating

.valves.

The

inspector

had observed .i.n Inspection Report-50-400/97-09 that the<<

opening of the regulating valves prior to opening the block valves

was

contrary to:step

102 'of General

Procedure

.(GP)

005,

Power

Oper ation "

(Hode 2 to Hode 1); Revision 18.-

The root cause,

as determined

by the

investigation,

was that,.the, pre-evolution brief did not discuss the

operation of the feed regulating valves

as

a contingency source-of

water.

Consequently,

when they were needed.

the operator

assigned to

operate

them was not fully prepared,

and did not tollow the procedure.

A contributing cause identified was that the location in the procedure

of the steps to open the valves

was incorrect.

The inspector concluded

that this was based

on the current operation of the plant.

The

PNSC

discussion

concluded that the steps

were adequately

located for how the

simulator operated.,

However,

a

PNSC action item was opened to

investigate

why the simulator and plant were different for the

synchronization evolution.

The failure to follow procedure

GP-005 in

opening the feed regulating block valves

was

a violation of'S 6.8

~ 1 and

is designated

violation 50-400/97-10-01,

example

1, Failure to Establish

and Implement Operating

and Surveillance

Procedures.

Condition Report 97-04112-1 dealt with a turbine runback that occurred

while placing

a second

main feed

pump in ser vice.

The root cause

was

identified as the senior control operator

not following the note prior

to step 131.c of GP-005 which stated that

a second

feed

pump was to be

placed in service prior to 300 psig first stage turbine pressure after

exceeding

6.0 million pounds per hour total feed flow.

The senior

control operator

had stated that he thought the turbine runback

was at

370 psig instead of the 310 psig stated in the procedure.

Procedure

APP-ALB-020, Hain Control Board,

Revision

6 had listed the setpoint at

370 psig and was the one the senior

control operator

was recently

familiar with.

The failure to follow procedure

GP-005 in placing

a

second

main feed

pump in service

was

a violation of TS 6.8. 1 and is

designated

violation 50-400/97-10-01 'xample 2, Failure to Establish

and Implement Operating

and Surveillance

Procedures.

Two previous condition reports

addressed

the setpoint issue.

CR 95-

02730 addressed

changes to procedures

after the setpoint

was changed

during the performance of EPT-093, Turbine First Stage

Pressure

Data,

after refueling outage six.

Engineering Service Request

95-00946,

Revision 1, was issued in April 1996 to implement the corrective action

08.2

4

and identified that AOP-012,

Feedwater

Malfunctions,

and APP-ALB-016,

Hain Control Board,

needed to be changed.

CR 96-01254-2 addressed

a

turbine runback that, occurred

May 4,

1996 where

a second

feed

pump was

being placed in service at

a value too -close to the runback -set point.

Both of these condition =reports

had identified that procedures

were

inconsistent

in relation to the turbine runback setpoint.

These

procedures

included GP-005,

OP-134.01,

Feedwater

System,

AOP-010.

and

APP-ALB-020.

The only procedure that was changed

was procedure

GP-005.

The personnel

error

which caused

the September

1997 runback could have

been prevented

by proper management prioritization of the identified

corrective -actions,.for, the.3995

and

1996 condition reports;

Consequently,

the inspector concluded that the operator would not have

had the incorrect value -stored in his mind had the proper prioritization

occurred.

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The inspector confirmed that the following conflicting statements

identified in the root cause investigation were in the procedures..

General

Procedure

(GP) 005,

Power Operation

(Mode 2 to Mode 1),

Revision 18, section 5.0; step

131 states that

a turbine runback will

occur at approximately

310 psig.

-.The second

main feedwater

pump should

be started prior to exceeding

300 psig turbine first stage

pressure

and

after exceeding

6.0 and before 6.7 million pounds

per

hour total feed

,flow.

Operating

Procedure

134.01,

Feedwater

System,

Revision 8,

Section 5, states that

a second

feedpump should be started

when total

flow to the steam generator s is in the range of 6.0 to 6.7 million

pounds per hour total feed flow.

AOP-010,

Feedwater Malfunctions,

Revision 12, states that above

330 psig first stage pressure

(60K),

a

turbine runback will occur.

APP-ALB-020, Main Control Board,

Revision 6, states for windows 1-1, 1-2. 1-3. 1-4,

and 2-2, that

a

turbine runback occurs at greater

than 370 psig first stage turbine

pressure.

The inspector concluded that the conflicts in where the

turbine runback occurs

and when to start

a second

feedwater

pump had

been identified by two previous

CRs and had been outstanding f'r

approximately two years.

The failure to establish

adequate

procedures

related to GP-005,

OP-134.01,

AOP-010,

and APP-ALB-020 providing

different values for the turbine runback

and inconsistent

guidance

on

when the second

main feedwater

pump should be started is considered

an

additional

example of a violation of. TS 6.8.1

and is designated

violation 50-400/97-10-01,

example 3, Failure to Establish

and Implement

Operating

and Surveillance

Procedures.

Closed

URI 50-400/97-01-01:

Tracking Operator

License Conditions in

the

MCR

This item was opened to review whether unqualified operators

were

allowed to stand watch due to a lack of an immediate license condition

verification log in the main control

room.

The inspector

discussed this

issue with numerous

licensee

personnel

and managers

including the

operations

manager, training manager,

and various shift superintendents.

The inspector

also reviewed various electronic mail messages

sent after

some recent requalification failures.

The inspector

was convinced that

the current practice of Training providing immediate notification of

08.3

failures to the Operations

manager. via electronic mail was effective.

The inspector

observed that the electronic mail was forwarded by the

.

operations

manager

to all shift superintendents

with instructions not to

allow the identified individuals to stand watch.

The inspector

also

reviewed .watch, standing lists to verify that qualified individuals stood

watch.

The combination of these

convinced the inspector that only

qualified personnelhave

stood watch.

The inspector

reviewed -a .beta test .of the Personnel

Qualification

Tracking System which'.when data

has,been

completely loaded will provide

the i'mmediate. tracking function for the. shift superintendent.

The

operations

support organization

was beginning the process of loading the

data into the program.

The inspector

was

shown

how training 'could

immediately place

a flag 'on.'the qualifi'cation of an individual that had

failed requalification.

The inspector

concluded that the program

addressed

the

NRC concern in this -area.

This item is closed.

Closed

LER 50-400/96-008-'02:.Reactor

Trip due to the failure of a

switch yard breaker

disconnect

switch.

This supplement

was issued

October

14,

1997 to update informati.on on normal service water

pump

problems.

The information was already provided in LER 96-018-01

and was

already considered

when supplement

1 was closed.

This item is closed.

II. Maintenance

Conduct of Maintenance

General

Comments

Ins ection Sco

e

62707

The inspectors

observed all or portions of the following work

activities:

~

WR/JO 97-AKRS1

Install N-42 detector current

~

WR/JO 97-AHHN1

Unload solidified waste ingot

~

WR/JO 96-ABFMl--

Install-spent fuel rack in "B" spent fuel pool

~

WR/JO 97-AJZSl

Ground Isolation on

OC bus

Observations

and Findin s

The inspectors

found the work performed under these activities to be

professional

and thorough.

All work observed

was performed with the

work package

present

and in active use.

Technicians

were experienced

and knowledgeable of their assigned

tasks.

The inspectors

frequently

observed

supervisors

and system engineers

monitoring job progress,

and

quality control personnel

were present

whenever required

by procedure.

Peer-checking

and self checking techniques

were being used.

When

applicable,

appropriate radiation control measures

were in place.

Conclusions

Maintenance activities observed

were being properly conducted.

Maintenance

and Material Condition of Facilities and Equipment

Surveillance Observation

Ins ection Sco

e

61726

The inspectors. observed all or portions of the -following surveillance

tests:

~

MST-I0275

0, Monitor OAI-21WG-1101 Calibration,

Revision

7

MST-I0045

Nuclear Instrumentation

System

Power

Range

N-42

Calibration. Revision

9

OST-1005

Control

Rod and

Rod Position Indicator Exercise

Monthly Interval, Revision

7

~

OST-1124

-6.9 kv Emergency

Bus Undervoltage Trip Accuatuation

Device Operational

Test,

Monthly Interval,

Modes 1-2-

3-4, Revision

10

Observations

and Findin s

The inspector

found that the testing

was adequately

performed.

During

the performance of HST-I0045 technicians

perf'orming the surveillance

found that the detector current values that were input were incorrect.

The error resulted

from an improper transfer of the engineering

data to

the surveillance data sheet.

The technicians

found this prior to the

completion of the test

and prior to instrumentation

channel

N-42 being

declared operable.

As

a result,

a portion of'he surveillance

had to be

reperformed.

The error occurred

due to inadequate

self-checking.

Condition Report 97-047-33

was written to address

the data transfer

error.

The inspector

found that the peer checking performed during this

surveillance

was positive and was the technique that resulted in the

problem being found.

During performance of OST-1005 the operators

found

a potential

problem

with the in-hold-out switch related to the time it took for the rods to

move from step

224 to step

225 for shutdown

bank "C".

The operators

appropriately stopped the test

and formulated

a troubleshooting

plan.

The operators

found that for the last step the switch had to be held in

the out position for

a longer period of'ime.

Condition Report 97-04483

was written to address this issue.

The operators

also found that the

same problem had been encountered

during the previous performance

but

had not been

documented.

The test

was then successfully

completed.

The

inspector

found the operators to be appropriately sensitive to problems

they encountered

during testing.

MB

H8.1

Conclusions

The surveillance

performances

were adequately

conducted.

Maintenance

and.Operations

persorinel

performing the survei llances were appropriately

sensitive to potential

problems

and appropriately performed peer

checking to identify potentia'1

problems before they impacted plant

operations..

Miscellaneous

Maintenance

Issues

(92700.

92902,

90712)

1

Clo'sed

URI 50-400/97-09-01:

TDAFWP Forced:Outage

Problems

This item.was left unresolved

based

on review of..the root cause

determination for the:turbine-driven auxiliary feedwater-

pump

(TDAFWP)

problems.-'he

inspector

reviewed the root cause investigation for

condition report 97-04094.

LER 50-400/97-022-00,

and attended the

PNSC

meeting that discussed

the root cause investigation.

The root cause

investigation

and

LER concluded that the root cause of the coupling

being installed backwards

was

a personnel

error caused

by not performing

adequate self checking.

In addition, other causes

were fatigue due to

overtime. and time pressure

due to the coupling being hot.

The overtime

had been properly authorized in accordance

with procedure

AP-012,

Control of Overtime Hours,

Revision 4.

The inspector concluded that the

root cause

was accurate

and that the failure to install the coupling

properly was

a violation of procedure

CH-H0071, Ingersoll-Rand Turbine

Driven Auxiliary Feedwater

Pump Size 4X9 NH-7 Disassembly

and

Maintenance,

Revision 6.

Corrective actions

included counseling

and

lessons

learned for maintenance

department

personnel.

This non-

repetitive. licensee-identified

and corrected violation is being treated

as

a Non-Cited Violation, consistent with Section VII.B.l of the

NRC

Enforcement Policy and is designated

NCV 50-400/97-10-02,

Inadequate

TDAFWP Maintenance Activities.

During TDAFWP reassembly

the

pump leaked

and was reassembled

several

times.

The investigation determined the problem to be

a gasket cutting

and reassembly

procedure

problem.

The procedure

reassembled

the

pump

such that the outer stuffing box was inserted prior to setting the upper

casing

on the gasket.

Thus. the stuffing box 0-ring could be affected

by the gasket being cut oversize or under size, without any method of

evaluating the 0-ring seating surface

adequacy prior to pressurizing the

pump.

The licensee

determined that the proper way,to perform this task

was to cut the gasket slightly oversize in the 0-ring area,

and then

retrim the gasket with the upper casing installed, prior to inserting

the stuffing box.

This would ensure that the 0-ring seating

area

was

smooth.

The root cause of the split casing gasket

problem was

identified as

a lack of adequate

technical

guidance in the Technical

Manual

and procedure

CH-M0071.

The technical

manual did not provide any

guidance

on gasket cutting for the split casing

pump, although the

vendor was aware that specific gasket cutting techniques

were necessary.

Consequently.

the procedure also did not have any specific guidance.

Corrective actions included review and revision of split casing

pump

maintenance

procedures

and maintenance

department training.

The

~

~

8

licensee did find. some minimal gasket cutting instructions in the motor

driven auxiliary feedwater

pump procedures.

The motor driven pumps are

also split casing

pumps but are

a different model.

The inspector

concluded that the root cause investigation

was accurate

and that the

inadequate

procedure

was

a violation of TS 6.8. 1.

This non-repetitive,

licensee-identified

and corrected violation is being treated

as "a Non'-

Cited Violation, consistent with Section VII.B.1 of the

NRC Enforcement

Policy and is considered

'a second

example of NCV 50-400/97-10-02,

Inadequate

TDAFWP Maintenance Activities.

The root -cause..of .the .TDAFWP deadheading

was attributed to a lack of

situational

awareness:regarding

equipment conditions related to flow

path and cooling status

of:,equipment being tested.

A contributing cause

included

a failure to relay 'important,information during the test to the

key decision

makers 'on shift regarding .the status of the

TDAFWP

recirculation.

A second

cause

included that the risks and consequences

associated

with securing auxiliary"feedwater flow with recirculation

isolated were not adequately

reviewed/assessed.

The inspector

considered that there

was adequate

guidance in Procedure

OST-1080,

Auxiliary Feedwater

Pump

1X-SAB Full Flow Test Quarterly Interval,.

Revision 1. concerning securing

feed flow in steps

37 and 38, which

direct reestablishing

the recirculation flow path prior to securing

feed

flow.

The purpose of'hose steps

was to ensure that the

pump was not

deadheaded.

The failure to follow procedure

OST-1080 in securing

auxiliary feedwater

flow prior to establishing

a recirculation

flow path

was

a violation of TS 6.8. 1 for failure to follow procedures

and is

designated

violation 50-400/97-10-01,

example 4, Failure to Establish

and Implement Operating

and Surveillance

Procedures.

Closed

LER 50-400/96-022-00:

Wiring Discrepancy

Found in Reactor

Auxiliary Building Ventilation System Circuitry

This

LER was originally discussed

in NRC Inspection Report 50-400/96-11

section

M8.1 and described

a self-disclosing condition in which

a wiring

lead was terminated incorrectly in the "A" train reactor auxiliary

building ventilation system.

The

LER remained

open pending the

licensee's

completion of further corrective actions to train maintenance

and quality control personnel

on this event.

The inspector's

reviewed the valida'tion package for LER 50-400/96-022-00

and verified through inspection of training records that required

training was completed.

This item is closed.

E1

Conduct of Engineer ing

III. En ineerin

El. 1

En ineerin

Service

Re uests

Ins ection -Sco

e

37551

I

The inspectors

reviewed all or portions of the following Engineering

Service Requests

to determine if procedure

EGR-NGGC-005

Engineering

Service Requests,

Revision 5, was being followed:

~ ,

'-

ESR 9500278 Installation of Additional

BWR Spent

Fuel

Racks in "B"

Spent

Fuel Pool. Revision 0:

.

~

ESR 9700747

AH-7 (1A-SA)* Operability Determination,

Revision

0

l

~

ESR 9700745

1BD-48 (PCV-8400c) Simulated

Open Signal,

Revision

0

~

ESR 9700024

Computer

Room HVAC, Revision 3

Observations

and Findin s

In general,

the

ESRs reviewed were adequate.

ESR 9700024,

Computer

Room HVAC, was prepared to resolve

an issue for

Technical Specification 4.7.6.d.3 which requires the main control

room.

to be maintained'at

a positive pressure of 1/8 inches of mercury gauge

with respect to adjacent

areas

(computer room).

The issue

was

originalty identified during surveillance testing

when pressure

differential testing of adjacent

areas to the main control

room was not

performed.

An additional

concern

was identified that if the computer

room was pressurized,

the main control

room could not meet its

surveillance

requirement.

A 10 CFR 50.59 safety evaluation

was written

to remove requirements

in the

FSAR to pressurize

the computer

and

communication

room and

FSAR Review and Approval

Form (RAF) 2082 was

prepared.

An Engineering Disposition Engineering Service Request

(ESR)

9600243

was prepared to address

which dampers to reposition to prevent

computer

room pressurization.

Clearance

tags were hung to implement

ESR

9600243.

LER 96-007-00

was prepared for this issue.

'emporary Modification 9700024 included

FSAR changes

which were

different from the

FSAR page markups

(RAF 2082) initially prepared.

Licensing rejected

RAF 2082 due to these differences.

In April, 1997,

the clearance

tags were removed

and dampers

were locked in their safety-

related position per

ESR 9700024.

On May 24,

1997,

ESR 9700024 Revision

3 was approved

by the Plant Vice President

designee to move the

expi ration date for the temporary modification to August 1,

1997, after

completion of refueling outage

RFO-7.

Temporary modification extensions

past the next refueling outage required approval, by the Plant Vice

President

or designee

per licensee

procedure

EGR-NGGC-005,

Engineering

Service Requests,

Revision 4, Attachment

3 section A3.6.3.

On July 22,

E7.1

E7.2

10

1997, engineering

personnel

processed

an extension of temporary

modification 9700024 from August 1,

1997, till May 1,

1998.

This

extension

was inot reviewed

and approved

by the Plant Vice President

or

designee

as required.

After being informed by the inspectors of the

unauthorized

extension.

licensee

management

took corrective action which

included initiation of condition report 97-0448,

review of the temporary

modification,:.and issuance of a

memo to all members of the Harris

Engineering Section regarding procedural

requi rements for temporary

modification approval

and extension. " The

FSAR change for this item was

rescheduled .to.,be included in the December,

1997,

FSAR amendment

package.

I

The extension .of temporary modification 9700024 past

May 24,

1997; was

a

violation of licensee.~procedure

EGR-NGGC-005;

Engineering Service

Requests,

Revision 4.. This failure. constitutes

a violation-of minor

significance

and is being treated .as

a Non-Cited Violation, consistent.

with Section

IV of the

NRC Enforcement Policy (NCV 50-400/97-10-03).

Conclusions

In general,

Engineering activities were being adequately

conducted in

accordance

with required procedures.

A noncited violation was

identified for the unapproved

extension of a temporary modification due

date.

Quality Assurance in Engineering Activities

S ecial

FSAR Review

37551

A recent discovery of a licensee operating their facility in a manner

contrary to the Updated Final Safety Analysis Report

(UFSAR) description

highlighted the need for a special

focused

review that compares plant

practices.

procedures

and/or parameters

to the

FSAR descriptions.

While

performing the inspections

discussed

in this report, the inspectors

reviewed the applicable portions of the

FSAR that related to the areas

inspected.

The inspector s did not find any additional discrepancies

other than those identified by the licensee.

TOAFW Pum

Problems

Ins ection Sco

e

37551

The inspector

reviewed the root cause investigation for condition report

97-04025 which described

engineering troubleshooting

problems associated

with the turbine-driven auxiliary feedwater

pump

(TDAFWP) forced outage

and attended

the associated

PNSC meeting conducted

September

25,

1997

(Section 07. 1).

Inspection

Report 50-400/97-09

(Section

E4. 1) discusses

a weakness

in troubleshooting

related to this issue:

The root cause

investigation also addressed

rebaselining

the pump at

a different flow

point.

Observations

and Findin s

.11

E8

E8.1

NRC Bulletin 88-04, Safety-related

Pump Loss,

had warned of flow

instability at low flows while on recirculation.

Flow instability

becomes

more severe

as flow is .decreased,

and can cause

pump damage

from

ump vibration. excessive

forces

on the impeller,

and cavitation.

The

ulletin recommended that the limitations associated

with these

hydraulic phenomena

be considered

when specifying minimum flow capacity.

The licensee's

response to the bulletin, dated July ll and November

1,

1988,.did'not describe

any problems with the auxiliary feedwater

system.

There was. no mention of the licensee.'s

investigation

and response to

NRC

Bulletin 88-04, in the root cause investigation,

LER.

or at the

PNSC

meeting.

Although the inspector

had informed licensee

management of the

bulletin at the time. the-maintenance

was being performed,

the inspector

found that the system engineer

who performed the root cause

assessment

had not been told about. it.

The inspector

concluded that poor

communication within engineering

management

was the cause of the

problem.

Conclusions

Communications within engineering

management

related to the

TDAFWP

needed

improvement.

Miscellaneous

Engineering Issues

(92700)

Closed

LER 50-400/96-024-00:

Common

Mode Failure in the Reactor

Auxiliary Building Electrical

Equipment Protection

Rooms Ventilation

System

This

LER was discussed

in NRC Inspection Report 50-400/96-11 section

E8.2 and described

a

common

mode failure that could prevent both Reactor

Auxiliary Building (RAB) Electrical

Equipment Protection

Rooms Supply

Fans

AH-16A and AH-16B from operating.

This failure was related to two

nonsafety-related

ionization detectors

in the AH-16 ductwork that are

wired in parallel to form a fire detection

zone permissive.

Due to the

system's

design,

a failure of either detector would preclude satisfying

the fan's start permissive

and prevent the fans from maintaining area

temperatures

to ensure the operability of safety-related

equipment,

following a safety injection signal.

This deficiency had been

identified on November 21,

1996,

and the licensee

concluded that the

condition was contrary to the design basis of the plant.

The safety significance of this deficiency was low because

the fans

would be manually started

as directed

by operating

procedures

following

a safety injection signal.

The fans were not credited in the Harris

Plant Probabilistic Safety Assessment

and would not affect core damage

frequency.

The

LER was due to inadequate

original plant design.

Review of FSAR

sections 9.4.5, 7.3.1,

3. 1,

and 8.3.1 confirmed that the plant's design

basis for the

RAB Electrical

Equipment Protection

Rooms Supply Fans

. 12

AH-16A and, AH-16B called for the fans to be designed for single failure

and that the use of fire detection

zone

151 for both fans was

an

original design basis

common

mode failure.

The inspectors

reviewed

modification

ESR 96-00573 which added

new fire detectors

in new fire

protection

zone

151A to eliminate the

common

mode failure potential.

The inspectors

reviewed the circuit modifications,

performed

a

modification walkdown,'nd reviewed the post modification testing.

\\

Based

on review of the circuit .changes

and plant walkdowns the

inspectors verified that the new detectors

and

new fire zone eliminated

the potential

common

mode failure.

The inspectors

noted that the post

modification testing verified the fan trip interlocks within each safety

train but did not positively verify that fan operation

was not affected

by fire defector, actuation in the opposite train fire zone.

Despite not

positively verifying that fire detection would not impact fan operation

in the opposite train, the inspectors

determined that the modification

was adequate

based

on the post modification testing performed

and the

circuit reviews

and plant walkdowns.

This original design basis

common

mode failure was

a violation of 10 CFR 50 Appendix A. Criterion 3 - Fire Protection.

This non-repetitive,

licensee-identified

and corrected violation is being treated

as

a Non-

Cited Violation, consistent with Section VII.B.1 of the

NRC Enforcement

Policy

(NCV 50-400/97-10-04).

This

LER is closed.

IV. Plant

Su

ort

R1

Rl.1

C.

Radiological Protection

and Chemistry

(RP8C) Controls

General

Comments

Ins ection Sco

e

71750

The inspector

observed radiological controls during the conduct of tours

and observation of maintenance activities.

Observations

and Findin s

The inspector

found radiological controls to be acceptable.

The general

approach to the control of contamination

and dose for the site was good.

Teamwork between the various departments

continued to be

a major

contributor to the good control of dose.

Conclusions

The control of contamination

and dose for the site was good and was

attributable to good teamwork between the various departments.

~

P1.1

Conduct of EP Activities

General

Comments'

.=13-

Ins ection Sco

e

71750

The inspectors'bserved

Emergency

Preparedness

activities to determine

their effectiveness.

b; *'Observations

and Findin s

I

~

S1

~

Sl.l

a.

~ The Harris Emergency Exercise

was conducted

On October

7,

1997.

The

Exercise

was conducted with full NRC participation.

The evaluation of

the exercise

was documented in Inspection

Report 50-400/97-11.

Si'mulator

Control

Room activities were observed

during

NRC participation

in the drill and found to be acceptable.

-The operations shift crew was

observed to be followi'ng Emergency

and Abnormal Operating Procedures.

'Conclusions

Emergency-Preparedness

activities, in general,

were adequately

conducted.

Conduct of Security and Safeguards Activities

General

Comments

Ins ection Sco

e

71750

The inspector

obser ved security and safeguards

activities during the

conduct of tours, observation of maintenance activities,

and the

emergency

preparedness

dri 1 1 .

Observations

and Findin s

The inspector

found the performance of these activities was good.

Compensatory

measures

were posted

when necessary

and properly conducted.

One communications

issue

was identified by the licensee during the

Emergency

Preparedness

exercise.

The inspector

found that Security

management

was appropriately investigating

and resolving this

observation.

Conclusions

The performance of Security and Safeguards activities were good.

14

F1

Control of Fire Protection Activities

Fl. 1

General

Comments

a.

Ins ection Sco

e

71750

I

The inspector

obser ved Are protection equipment

and activities during

the conduct of tours

and observation of maintenance activities.

I

1

I'

i

b.

Observations

and Findin 5 "

The inspector

found the fire protection activities to be acceptable.

c.

Conclusions

J

f'ire

Protecti'on activities were being adequately "conducted.

V. Mana ement Meetin s

Xl

Exit Meeting Summary

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on October 30.

1997.

The

licensee

acknowledged the findings presented.

The inspectors

asked the licensee whether any of the material

examined

during the inspection should be considered proprietary.

No proprietary

information was identified.

Licensee

15

PARTIAL LIST OF PERSONS

CONTACTED

D.. Batton, Superintendent,

On-Line Scheduling

D. Braund, Superintendent,

Security

B. Clark, General

Manager,

Harris Plant

A. Cockeri ll, Superintendent,

I&C Electrical

Systems

J. Collins. Manager,

Maintenance

J.

Donahue,

Director. Site Operations.

Harris Plant

J.

Eads,

Supervisor;

Licensing

and Regulatory

Programs

W. Gurganious',

Superintendent.

Environmental

and Chemistry

M. Hamby, Supervisor,

CAP/OEF

M. Ke'ef,=Manager'<i Training

B. Meyer, Manager,

Operations

K. Neuschaefer,

Superintendent;

Radiation Protection

W. Peavyhouse,

Superintendent,

Design Control

W. Robinson,

Vice. President,

Harris Plant

S. Sewell. Superintendent,

Mechanical

Systems

D. Tibbitts, Manager.

Nuclear Assessment

C.

VanDenburgh,

Manager,

Regulatory Affairs

NRC

V. Rooney.

Harris Project Manager,

NRR

M. Shymlock, Chief, Reactor Projects

Branch 4

16

INSPECTION

PROCEDURES

USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving,

and

Preventing

Problems

IP 61726:

Sur veil lance

Obser vations

IP 62707:

Maintenance

Observation

IP 71707:

Plant Operations

IP 71750:.

Plant Support Activities

IP 90712:

In-office Revi,ew of LERs

IP 92700:

Onsite.Followup-of Events

IP 92901

=

Followup - Plant Operations

IP 92902:

Followup - Maintenance

50-400/97-10-02

NCV

50-400/97-10-03

50-400/97-10-04

NCV

NCV

Closed

~Den ed

50-400/97-10-01

VIO

ITEMS OPENED,

CLOSED,

AND DISCUSSED

r'

S

"I

Failure to establish

and implement operating

and

surveillance

procedures;

4 examples

(Section 08.1:

Section M8.1).

Inadequate

TDAFWP maintenance activities;

2 examples

(Section M8.1).

Computer

Room

HVAC tempor ary modification extension

(Section E1.1).

Common

Mode Failure in the Reactor Auxiliary Building

Electrical

Equipment Protection

Rooms Ventilation

System

(Section E8.1).

50-400/96-022-00

50-400/96-024-00

50-400/97-09-01

50-400/97-10-02

50-400/97-10/03

50-400/97-10-04

50-400/97-01-01

50-400/96-008-02

LER

Wiring discrepancy

found in Reactor Auxiliary Building

~

ventilation

system circuitry (Section M8.2).

LER

Common

mode failure in the Reactor Auxiliary Building

Electrical

Equipment Protection

Rooms Ventilation

System (Section E8.1).

URI

TDAFWP forced outage

problems

(Section

MB.1).

NCY

Inadequate

TDAFWP maintenance activities;

2 examples

(Section M8.1).

NCV

Computer

Room

HVAC temporary modification extension

(Section E1.1).

NCV,

Common

Mode Failure in the Reactor Auxiliary Building

Electr ical Equipment Protection

Rooms Ventilation

System (Section

EB. 1).

URI

Tracking Operator

License Conditions in the

MCR

(Section 08.2)

LER

Reactor Trip due to the failure of a switch yard

breaker

disconnect switch.

(Section 08.3)