ML18012A613

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Errata to Insp Rept 50-400/97-01 on 970105-0215.Replaces Page 14 of Subj Insp Rept & Page One of Executive Summary
ML18012A613
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 03/28/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18012A611 List:
References
50-400-97-01, 50-400-97-1, NUDOCS 9704160061
Download: ML18012A613 (7)


See also: IR 05000400/1997001

Text

14

NRC guidance to inspectors for enforcement of rated thermal

power

contained in NRC Inspection Procedure 61706.

This guidance

was not

issued for the purpose of defining rated thermal

power for licens

s.

Rated thermal

power is already defined for licensees

in their

op

ating

license

and the Technical Specification Definition section.

T

Operating License

(NPF-63)

and Technical Specifications for d

ket

50-400 state that rated thermal

power is 2775 megawatts ther al

(100

percent rated core power).

The new basis

used the enforce

nt guidance

to inspectors

for the purpose of redefining 100.0 percen

rated thermal

power

as

a number that floats based

on the amount of ti

that power

was

over rated thermal

power .

As such,

power could be as

igh as

102

ercent,

without the licensee declaring that rated t

rmal

power

had

een exceeded

and

a flux map initiated.

The inspec

or considered that

the basis statement

and the Technical Specificati

were in conflict.

The inspector

reviewed the February

21

1996

P

nt Nuclear Safety

Committee

(PNSC) meeting minutes

assoc

ed

w

h the LER.'he minutes

included

a discussion of the proble

s

t

with TS 3.2.3 due to

ammendment

50 and that the pr epar

ion

n

eview of ammendment

50 was

considered

inadequate.

The minu

als

ndicated that the words which

were included in the new TS Basi

r T

3.2.3 were discussed

and agreed

to although ther e was no ment

n th t

ey would be put in the TS Basis.

The inspector observed that t

minu

s did not mention any discussion

about processing

a TS change.

'nspector

considered that the

PNSC

missed

an opportunity to

sur t t this problem was properly

corrected.

The inspector

r evie

lic

s e calorimetric data from operator logs for

the performance of

cedur

OST-1004,

Power Range Heat Balance,

Computer Calcul

ion.

dition, the inspector discussed

the

LER and

bases

change

wi h ope

to s.

The inspector

became

aware of a

performance of

S -1004

n Har ch 20,

1996 when the calorimetric value of

power

was 100.2

er e

.

The inspector

reviewed the operator logs for

that performance

d

he OST-1004 data sheet that documented the

calorimetric, the

nterviewed the shift personnel

involved with that

performance

and t

shift supervisors for the next two shifts (24 hrs).

The inspector

co eluded from.these

reviews that the event reported in

the

LER had re

rred on Harch 20,

1996 in that power

had exceeded

100.0

percent

(100.

percent)

and

a flux map was not performed.

The

interviews

dicated that the operators

had chosen to use the new TS

Basis

as t e foundation for their decision.

The licensee's

decision

was

based

on

onsiderable

discussion

over several shifts.

The i

pector

discussed this issue with licensee

management

on

Janu

y 29,

1997.

The licensee

generated

a TS Basis

change to remove

th

conflicting verbage,

which was sent to the

NRC on February 13,

1997.

e ulator

Si nificance

10 CFR 50, Appendix B, Criterion XVI requires that measures

be

established

to assure that conditions adverse to quality such

as

deficiencies,

deviations,

and nonconformances

are promptly identified

9704i60061

970328

PDR

ADQCK 05000400

9

PDR

C

CPSL

The inspector

reviewed the February 21,

1996 Plant Nuclear Safety

Committee

(PNSC) meeting minutes associated

with the LER.

The minutes

included

a discussion of the problems created with TS 3.2.3 due to

ammendment

50 and that the preparation

and review of ammendment

50 was

considered

inadequate.

The minutes also indicated"that the words which

were included in the new TS Basis for TS 3.2.3 were discussed

and agreed

to although there was no mention that they would be put in the TS Basis.

The inspector observed that the minutes did not mention any discussion

about proces'sing

a TS change.

The inspector considered that the

PNSC

missed

an opportunity to ensure that this problem was properly corrected.

14

NRC guidance to inspectors for enfor cement of r ated thermal

power

contained in NRC Inspection

Procedure

61706.

This guidance

was not

issued for the purpose of defining rated thermal

power for licensees.

Rated thermal

power is already defined for licensees

in their operating

license

and the Technical Specification Definition section.

.The

Operating License

(NPF-63)

and Technical Specifications for docket 50-400

state that rated thermal

power is 2775 megawatts

thermal

(100 percent

rated core power).

The new basis

used the enforcement

guidance to

inspectors

for the purpose of redefining 100.0 percent rated thermal

power

as

a number that floats based

on the amount of'time that power was

over rated thermal

power.

As such,

power could be as high as

102

percent,

without the licensee declaring that rated thermal

power

had been

exceeded

and

a flux map initiated.

The inspector considered that the

basis statement

and the Technical Specification were in conflict.

The inspector

reviewed licensee calorimetric data from operator logs for

the performance of procedure

OST-1004,

Power Range Heat Balance,

Computer

Calculation.

In addition, the inspector discussed

the

LER and bases

change with operators.

The inspector

became

aware of a performance of

OST-1004 on Har ch 20,

1996 when the calorimetric value of power was 100.1

percent.

The inspector

reviewed the operator logs for that performance

and the OST-1004 data sheet that documented the calorimetric, then

interviewed the shift personnel

involved with that performance

and the

shift supervisors

for the next two shifts (24 hrs).

The inspector

concluded

from these

reviews that the event reported in the

LER had

recurred

on March 20,

1996 in that power had exceeded

100.0 percent

(100.1 percent)

and

a flux map was not performed.

The inter views

indicated that the operators

had chosen to use the new TS Basis

as the

foundation for their decision.

The licensee's

decision

was based

on

considerable

discussion

over several shifts.

The inspector

discussed this issue with licensee

management

on

January 29,

1997.

The licensee

generated

a TS Basis change to remove the

conflicting verbage,

which was sent to the

NRC on February

13,

1997.

Re ulator

Si nificance

10 CFR 50, Appendix B, Criterion XVI requires that measures

be

established

to assure that conditions adverse to quality such

as

deficiencies,

deviations,

and nonconformances

are promptly identified

ENCLOSURE 2

EXECUTIVE SUHHARY

Shearon Harris Nuclear

Power Plant, Unit 1

NRC Inspection Report 50-400/97-01

This integrated inspection included aspects of licensee operations,

engineering,

maintenance,

and plant support.

The report covers

a six- eek

period of resident inspection.

In addition, it includes the results of

announced

inspections

by regional reactor engineers

and

a regional

eactor

inspector.

~0erations

In general,

the conduct of operations

was professiona

and safety-

conscious

(Section 01.1).

Operator performance during several

abnormal

pla

challenges

was good,

including a reactor trip (Section Ol.

, subseq

nt unit restart

(Section 01.4),

and an unplanned

boro

ilutio

(Section 01.6).

The

post-trip crew debrief was excellent

e

io

01.3),

and the post-trip

review package

was thorough (Secti

n

.4).

However, there

was

a late

Notice of Unusual

Event declarat'

a

N

notification related to a

Security Alert event (Section

.

and

S ction P4).

An unresolved

item was iden

ied

er aining to the unavailability of an

immediate

means for the Ope

ns

ift Supervisor to check operator

license conditions

as

uir d

y

ant procedures

(Section 01.2).

The Licensed Operator

ifi ation program continues to meet

NRC

requirements.

I

dit

n, t

licensee

was effective in determining

the errors that

h

, or coul

have, occurred over the past year as well

Additional emp as'n

hum

per'formance error reduction techniques,

particular ly 'h

area

identifying each instance of the operators

failing to c

p y w th

nagement

standards

and expectations,

was

needed. as th

om on f

tor s that contributed to most of the personnel

errors.

Shif

ag

ent and supervisors

were proactive in taking steps

to mitigate t

num

r of operator errors

by standardizing

communications

pro ocol, ensuring operators

continuously use procedures,

and instituting

peer

check policy (Section 05.1).

A violation w

identified when inadequate

corrective actions for a

Licensee've t Report

(LER) resulted in an additional

non-compliance

with Techn

al Specification 3.2.3 Action Statement

C.1, which

r equired

core flu

apping when power exceeded

100.0 percent

power .

The cause

was the

nappropriate

use of a Technical Specifi,cation Basis

change to

accomp ish

a Technical Specification

change

(Section 08.3).

EXECUTIVE SUMMARY

Shearon Harris Nuclear Power Plant, Unit 1

NRC Inspection Report 50-400/97-01

This integrated inspection included aspects of licensee operations,

engineering,

maintenance,

and plant support.

The report covers

a six-week

period of resident inspection.

In addition, it includes the results of

announced

inspections

by regional reactor engineers

and

a regional reactor

inspector.

~0erati ons

In general,

the conduct of operations

was professional

and safety-

conscious

(Section 01.1).

Operator

performance during several

abnormal plant challenges

was good,

including a reactor tr ip (Section 01.3),

subsequent

unit restart

(Section

01.4),

and an unplanned

boron dilution (Section 01.6).

The post-trip

crew debrief was excellent (Section 01.3),

and the post-trip review

ackage

was thorough (Section 01.4).

However, there was

a late Notice of

nusual

Event declaration

and

NRC notification related to a Security

Alert event (Section 04.1 and Section P4).

o

An unresolved

item was identified pertaining to the unavailability of an

immediate

means for the Operations Shift Supervisor to check operator

license conditions

as required by pl'ant procedures

(Section 01.2).

The Licensed Operator

Requalification program continues to meet

NRC

requirements.

The training staff was effective at finding weaknesses

in

the

operator

's technical skills; however, additional

emphasis

on human

performance error reduction techniques,

particularly in the area of

identifying each instance of the operators failing to comply with

management

standards

and expectations,

was needed.

In addition, the

licensee

was effective in determining the errors that had,

or could have,

occurred

over the past year as well as the

common factors that

contributed to most of the personnel

errors.

Shift management

and

supervisors

were proactive in taking steps to mitigate the number of

operator errors by standardizing

communications protocol, ensuring

operators. continuously use procedures,

and instituting a peer check

policy (Section 05.1).

A violation was identified when inadequate

corrective actions for a

Licensee

Event Report

(LER) resulted in an additional

non-compliance with

Technical Specification 3.2.3 Action Statement

C.1, which required

core

flux mapping when power

exceeded

100.0 percent

power .

The cause

was the

inappropriate

use of a Technical Specification Basis change to accomplish

a Technical Specification change

(Section 08.3).