ML18010A787

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Insp Rept 50-400/92-15 on 920718-0821.Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Security,Fire Protection,Surveillance Observation, Maint Observation & Safety Sys Walkdown
ML18010A787
Person / Time
Site: Harris 
Issue date: 09/17/1992
From: Christensen H, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18010A781 List:
References
50-400-92-15, NUDOCS 9209250012
Download: ML18010A787 (19)


See also: IR 05000400/1992015

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.IN.

ATLANTA,GEORGIA 30323

Report No.:

50-400/92-15

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

July 18 - August 21,

1992

Inspectors:

J.

edrow,

Senior

Resi

t

spec or

Licensee

No.:

NPF-63

7 /7Ip'z

Date Signed

M. Sha

non,~ esident

In

e

or

byy

b by:~. Chr'stensen,

Section Chief

Division of Reactor Projects

Date Signed

g

$ z

Da

e

igned

SUMMARY

Scope:

This routine inspection

was conducted

by two resident

inspectors

in the areas

of plant operations,

radiological controls, security, fire protection,

surveillance observation,

maintenance

observation,

safety

system

wa'lkdown,

evaluation of licensee

self-assessment,

preparations

for refueling, licensee

event reports

and licensee

action

on previous inspection

items.

Numerous

facility tours were conducted

and facility operations

observed.

Some of these

tours

and observations

were conducted

on backshifts.

Results:

One violation was identified:

Failure to properly implement plant procedures,

paragraphs

2,c

and 7.

Efforts to reduce

personnel

exposure

during radwaste

tank cleaning were

effective,

paragraph

2.b.(4).

The operational

support center

has

been relocated to the waste processing

building, paragraph

2.b.(7).

Appropriate aetio'n

was being taken to reduce

the maintenance

backlog,

paragraph

4.a.

09

S001

9~0917

9

OS000400

PDR

The continuing training program

and hands-on training facilities contributed

to increasing the. knowledge

and expertise of maintenance

personnel,

paragraph

4.b.

Appropriate management

involvement

was noted for the preventive

maintenance

deferral

process,

paragraph

4.c.

Improvement

was noted in reducing the backlog of required reviews

by the

nuclear safety review unit, paragraph

6.a.

Plant line organization self assessment

activities were considered

to be good

which reinforced quality work and the safe operation of the plant,

paragraph

6.b.

The nuclear plant support section

no longer performs

comparisons

of the

nuclear units,

paragraph

6.c.

Fuel handling procedures for new fuel receipt were considered

to be

cumbersome,

paragraph

7.

Operator action to manually control

steam pressure

following a reactor trip

was considered

to be inadequate,

paragraph 8.f.

0

REPORT DETAILS

Persons

Contacted

Licensee

Employees

J. Collins, Manager,

Operations

  • J. Cribb,

Manager, guality Control

  • C. Gibson,

Manager,

Programs

and Procedures

  • C. Hinnant,

General

Manager,

Harris Plant

  • D. Knepper,

Project Engineer,

Nuclear Engineering

Dept.

B. Heyer,

Manager,

Environmental

and Radiation Monitoring

  • T. Morton, Manager,

Maintenance

  • J. Hoyer,

Manager,

Project Assessment

  • J. Nevill, Manager,

Technical

Support

C. Olexi k, Manager,

Regulatory

Compliance

A. Powell,

Manager,

Harris Training Unit

  • C. Sawyer,

Project Engineer,

Nuclear Assessment

Dept.

  • H. Smith,

Manager,

Radwaste

Operation

G. Vaughn,

Vice President,

Harris Nuclear Project

ED Willett, Manager,

Outages

and Modifications

  • W. Wilson, Manager,

Spent Nuclear

Fuel

  • LE Woods,

Manager,

System Engineering

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Review of Plant Operations

(71707)

The plant began this inspection

period in hot standby

(Mode 3).

To

facilitate repair work, the plant was placed in hot shutdown

(Mode 4)

on

July 18 and the

"A" RHR system

was placed in service.

Following

replacement of the low pressure

turbine boot seals,

a plant heatup

was

commenced

and the hot standby condition was reached

at 3: 17 a.m.,

on

July 22.

A reactor startup

was performed

and the reactor

was taken

critical at 2:33 p.m.

Power operation

was

commenced

at 8:45 p.m.,

on

July 22.

The plant continued in power operation for the remainder of

this inspection period.

During the outage

the licensee

performed

several

repairs to secondary

plant equipment,

as well

as inspections/minor

work inside of the

containment building.

Several

main control

board deficiencies

were also

worked.

a.

Shift Logs

and Facility Records

The inspector

reviewed records

and discussed

various entries with

operations

personnel

to verify compliance with the Technical

Specifications

(TS)

and the licensee's

administrative

procedures.

The following records

were reviewed:

Shift Supervisor's

Log;

Control Operator's

Log; Night Order Book;,Equipment

Inoperable

Record; Active Clearance

Log; Grounding Device Log; Temporary

Modification Log; Chemistry Daily Reports; Shift Turnover

Checklist;

and selected

Radwaste

Logs.

In addition,

the inspector

independently verified clearance

order tagouts.

The inspectors

found the logs to be readable,

well organized,

and

provided sufficient information on plant status

and events.

Clearance

tagouts

were found to be properly implemented.

No

violations or deviations

were identified.

b.

Facility Tours

and Observations

Throughout the inspection period, facility tours were conducted

to

observe

operations,

surveillance,

and maintenance activities in

progress.

Some of these

observations

were conducted

during

backshifts.

Also, during"this inspection period, licensee

meetings

were attended

by the inspectors

to observe

planning

and

management activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter fence;

control

room; emergency

diesel

generator building; reactor

auxiliary building; waste processing

building; turbine building;

fuel handling building; emergency

service water building; battery

rooms; electrical

switchgear

rooms;

and the technical

support

center.

During these tours,

the following observations

were made:

(I)

Monitoring Instrumentation

- Equipment operating status,

area

atmospheric

and liquid radiation monitors, electrical

system lineup, reactor operating

parameters,

and auxiliary

equipment operating

parameters

were observed

to verify that

indicated parameters

were in accordance

with the

TS for the

current operational

mode.

(2)

Shift Staffing - The inspectors verified that operating

shift staffing was in accordance

with TS requirements

and

that control

room operations

were being conducted

in an

orderly and professional

manner.

In addition,

the inspector

observed shift turnovers

on various occasions

to verify- the

continuity of plant status,

operational, problems,

and other

pertinent plant information during these turnovers.

(3)

Plant Housekeeping

Conditions

- Storage of material

and

components,

and cleanliness

conditions of various

areas

throughout the Facility were observed to determine

whether

safety and/or fire hazards

existed.

(6)

Radiological

Protection

Program

- Radiation protection

control activities were observed routinely to verify that

these activities were in conformance with the facility

policies

and procedures,

and in compliance with regulatory

requirements. 'he inspectors

also reviewed selected

radiation work permits to verify that controls were

adequate.

The licensee's

activities to clean the Floor Drain Tanks

and

Waste Holdup Tank were followed.

Cleaning the sludge

from

these

tanks

was required

because filters in waste processing

systems

were frequently becoming clogged

when the tanks were

processed

to low levels.

A significant reduction in general

area

dose rates

was also achieved

which should help reduce

personnel

exposure.

The pre-evolution planning

and

briefings for this work were detailed.

Cameras

and dose

rate monitoring devices

were utilized to,remotely monitor

this work which contributed to the low personnel

exposure

received during job performance.

Security Control

- The performance of various shifts of the

security force was observed

in the conduct of daily

activities which included:

protected

and vital area

access

controls;

searching of personnel,

packages,

and vehicles;

badge

issuance

and retrieval; escorting of visitors;

patrols;

and compensatory

posts.

In addition,

the inspector

observed

the operational

status of closed circuit television

monitors, the intrusion detection

system in the central

and

secondary

alarm stations,

protected

area lighting, protected

and vital area barrier integrity,

and the security

organization interface with operations

and maintenance.

Fire Protection

- Fire protection activities, staffing and

equipment

were observed to verify that fire brigade staffing

was appropriate

and that fire alarms,

extinguishing

equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

Emergency

Response

Facility Relocation

- The licensee

has

recently completed modifications to relocate

the Operational

Support Center

(OSC) from the service building cafeteria to

the ground floor of the waste processing

building.

This

move was

made to avoid

OSC relocation during potential

emergency situations

where the area radiation levels might

increase

and necessitate

facility relocation.

During

a

licensee drill on August 5,

1992, operation of the

new

facility was observed.

The facility was considered

to be

fully functional

and equipped.

The inspectors

found plant housekeeping

and the material condition

of safety-related

components

to be good.

The licensee's

adherence

C.

to radiological controls, security controls, fire protection

requirements,

and

TS requirements

in these

areas

was satisfactory.

Review of Nonconformance

Reports

Adverse Condition Reports,(ACRs)

were reviewed to verify the

following:

TS were complied with, corrective actions

and generic

items were identified and*items were reported

as required

by

10 CFR 50.73.

ACR 92-320 reported that during

an attempt to backflush the seal

water return filter the system

was aligned improperly.

On

August 7,

1992,

radwaste

operations notified the main control

room

that the reactor coolant

pump seal

return filter required

backflushing.

Routinely these

types of evolutions require only

radwaste

personnel

action,

However,

a few filters require the

main control

room personnel

to open

bypass

valves

when the filter

is isolated.

Operating

procedure

OP-107,

Chemical

and Volume

Control

System,

Section 8.8, specifies

action to be taken to

backflush the seal

water return filter and requires that the

bypass

valve '(1CS-302)

be opened.

Contrary to this, the bypass

valve was not opened.

As

a result,

when radwaste

personnel

isolated the filter, system flow was isolated

and pressure

increased,

which challenged

the seal

return relief valve.

The.

licensee

was

asked to review all these

types of procedures

to

verify that appropriate

administrative controls were in place.

Failure to properly implement procedure

OP-107 is contrary to TS, 6.8. 1

and is considered

to be

a violation.

Violation (400/92-15-01):

Failure to properly implement plant

procedures.

Surveillance

Observation

(61726)

Surveillance tests

were observed

to verify that approved

procedures

were

being used; qualified personnel

were conducting the tests;

tests

were

adequate

to verify equipment operability; calibrated

equipment

was

utilized;

and

TS requirements

were followed.

The following tests

were observed

and/or data reviewed:

~ OST-1004

Power

Range

Heat Balance Daily Interval

Node

1 (above

15

percent

power)

~ OST-1026

.Reactor

Coolant System

Leakage

Evaluation

~ OST-1036

Shutdown Margin Calculation

~ OST-1039

Calculation of quadrant

Power Tilt Ratio,

Weekly Interval

(with alarm operable)

~ OST-1124

6.9

KV Emergency

Bus Undervoltage Trip Actuating Device

Operational

Test

~ EST-813T

Temporary Procedure for 6.9

KV Emergency

Bus Undervoltage

Trip Special

Test

'

EST-221

Type

C LLRT of Containment

Purge

Hake-up Penetration

(M-57)

~ EPT-183

1CS-744

SI Alternate Miniflow Relief Valve Relief Pressure

Test

~ EPT-184

1CS-755

SI Alternate Hiniflow Relief Valve Relief Pressure

,Test

The performance of these

procedures

was found to be satisfactory with

proper

use of calibrated test equipment,

necessary

communications

established,

notification/authorization of control

room personnel,

and

knowledgeable

personnel

having performed the tasks.

Procedure

EST-813T

was performed to verify appropriate

response

of the undervoltage

circuitry which was not previously tested

as described

in paragraph

8.g

of this report..

No violations or deviations

were observed.

Maintenance

Observation

(62703)

The inspector

observed/reviewed

maintenance activities to veri.fy that

correct equipment

clearances

were in effect; work requests

and fire

prevention work permits,

as require'd,

were issued

and being followed;

quality control personnel

were avai.lable for inspection activities

as

required;

and

TS requirements

were being followed.

Maintenance

was observed

and work packages

were reviewed for the

following maintenance activities:

Replacement

of undervoltage

relay 27A-1/1712

and associated

testing in accordance

with procedures

MST-E0045,

6.9KV Emergency

Bus

1B-SB Undervoltage

(Degraded

Voltage)

Relay

(ITE 27N) Channel

Calibration,

and OST-1124,

6.9KV Emergency

Bus Undervoltage Trip

Actuating Device Operational

Test.

Replacement

of S-2 invertor transformer in accordance

with

procedure

CH-E0020,

Replace Oil Filled and Electrical

YTIC

Capacitors

and/or Ferro-Resonant

Transformer Assembly in

Westinghouse

7.5

KVA Static Inverters.

Repair oil leak/rebuild hydraulic operator for main steam

PORV

1HS-62 in accordance

with procedures

CM-H0188, Hain Steam

Power

Operated Relief Valve

(PORV) Operator Disassembly,

Maintenance

and

Reassembly;

and

CM-H0186,

Paul

Honroe,

Hain Steam

Power Operated

Relief Valve

(PORV) Operator Fill and Bleed Procedure

and retest

in accordance

with procedure

OST-1079,

Containment Isolation

Valves Inservice Inspection

Test quarterly Interval.

Remove flow obstruction in piping for containment

cooling unit AH-

2 service water return flow transmitter

(FT-9275B).

The performance of work was satisfactory with proper documentation

of

removed

components

and independent verification of the reinstallation.

a 4

b.

The inspectors

reviewed the backlog of uncompleted

maintenance

work tickets.

The backlog presently consisted of approximately

2,000 non-outage

open work tickets which equated to approximately

10 -

12 crew weeks of work to accomplish.

This amount

was

considered

to be relatively high and was found to be fairly

constant

over the operating cycle.

Sixty percent of the tickets

were classified

as over 90 days old and most of the tickets

involved the I&C/electrical areas.

Approximately 35 percent

(700)

of the non-outage tickets were classified

as safety-related,

To

reduce

the backlog, plant management

obtained

an additional

I&C

crew during the middle of 1992 which has concentrated

on

completing the old work tickets.

The inspectors

found that this

additional

help has started to reduce the backlog.

Although the

total

amount of maintenance

backlog

was considered

to be high by

the inspectors,

the number- of safety related

work tickets

was

considered

to be manageable

and appropriate

action

was being taken

to reduce

the backlog.

The inspectors

also reviewed the maintenance

continuing training

program.

This training is conducted quarterly

and includes topics

such

as procedure

changes,

plant modifications, operating

experience,

system reviews, retraining

on complex tasks,

and

training for newly identified job skills.

This program

was

described

in training instruction TI-113; Related Technical

Training and On-The-Job Training for Selected

Maintenance

Classifications.

The inspectors

toured the licensee's

hands-on-training facilities

at the Energy

and Environmental

Center.

Areas were available for

electrical,

mechanical

and instrumentation/control

components,

as

well as

a mobile lab which contained

motor operated

valves

and

associated

diagnostic

equipment.

These facilities were utilized

- for troubleshooting

problems,

rehearsing

procedure

usage,

and

reviewing industry events.

Specific equipment

included the

following:

~ 6.9

KV electrical

bus

and breakers

~

Pumps

and motors for alignment training

~ Relief valves for disassembly/reassembly

and testing

~ Kerotest valves

~ Air operated

valves

~ Transmitters

~ Splicing electrical wires

This equipment

was also utilized during associated

continuing

training topics.

These facilities contributed to increasing

the

knowledge

and expertise of maintenance

personnel.

c.

Due to concerns

at another

CPKL plant that various

PHs were being

deferred,

the Harris

PH program was reviewed.

Requirements

regarding

PH deferral

were contained

in procedure

HHH-003,

Preventive

Maintenance

Program.

Procedurally,

before

any

PH can

be deferred,

the maintenance

supervisor

and the maintenance

manager

both sign to authorize

non-performance.

It was noted that

deferred safety-related

PHs were rescheduled

to the next available

window of opportunity depending

on plant conditions.

The

maintenance staff stated that it would be highly unlikely that

a

safety-related

PH would be voided

and not be rescheduled,

The

maintenance staff also stated that nonsafety-related

PHs were

voided,

but only after

a history search

to verify the last time

the

PM was performed.

A review of voided

PMs over the last month

found

no apparent

problems with the

PH process.

No violations or deviations

were identified.

.Safety

Systems

Walkdown (71710)

The inspector

conducted

a walkdown of the high pressure

safety injection

system to verify that the lineup was in accordance

with license

requirements

for system operability and that the system drawing

and

procedure correctly reflected "as-built" plant conditions.

The

-inspector

noted little evidence of boric acid leakage.

The licensee's

control of, boric acid leakage

was

commendable.

The licensee

had

repaired

many of the oil leaks

on the charging/safety

injection pumps

but continued attention to these

types of leaks is warranted.

Oil

leakage

was noted,

however,

on the operators for valves

1CS-218

and

1CS-

291.

An outer rubber sleeve

on

a flexible conduit for the valve

operator

on

1CS-752

was found to be tom. Also, paint was noted to be

flaking off of many valve operators

in this system.

These

minor

discrepancies

were referred to licensee

personnel

for corrective action.

E

It was also noted that sections of the system piping were warmer than

expected.

Since the alternate miniflow system

has closed isolation

valves,

there

should

be

no flow and the system should

be at ambient

temperature

which is approximately

80 degrees

F.

Temperatures

were

found

as high as

106 degrees

F with the normal charging

system

temperature

at

112 degrees

F, which indicated

leakage

between the A, B,

and

C charging

pump miniflow isolation valves.

Operations

retightened

the manual

isolation Kerotest valves

and subsequently

system

temperatures

returned to normal.

No violations or deviations

were identified.

Evaluation of Licensee Self Assessment

(40500)

a ~

The inspectors

vi.sited the licensee's

corporate office to review

the

NAD Nuclear Safety

Review

(NSR) unit activities. Specifically,

the inspectors

checked

the qualifications/experience

of NSR unit

reviewers,

the backlog status of items still pending review,

and

verified that reviews required

by TS 6.5.3 were performed.

The

NSR unit reviewers

were found to be qualified with a

substantial

number of years of nuclear experience.

The

NSR unit

has corrected

a weakness

discussed

in

NRC Inspection

Report 50-

400/90-08 regarding

a backlog of required reviews.

This backlog

has

been substantially

reduced to approximately twenty items per

site

and most of these

were

1'ess

than

one month old.

The

inspectors

checked

the quality of three

NSR modification package

reviews, five PNSC meeting minute reviews,

14

LER reviews,

and

five replies to notices of violation.

The inspectors

also

reviewed the

NSR unit's quarterly trend reports for

1992.'he

trending reports

were utilized by the licensee

to identify

appropriate

areas for further scrutiny.

Approximately three

such

mini-investigations

have

been

performed

by NSR personnel.

One

mini-investigation was conducted

which involved

a review of the

generation of a maintenance

agreement

between

the transmission

department

and individual plant generating

stations

and

was

applicable to the Harris site.

The inspector

found the

recommendations

from this review to be appropriate.

One minor problem was identified during these

reviews.

The

licensee

had not yet received

the reply to

a notice of violation

for violations 500/92-04-01

and 400/92-04-02

issued

in April 1992.

This reply had

been

issued

by the plant in May 1992 yet the

NSR

unit had not yet received the reply as of July 20.

The inspectors

discussed

this matter with licensee

personnel

who stated that the

NSR unit manager

had

been inadvertently omitted from the

distribution list for these letters.

Appropriate action

was taken

to correct the distribution list.

b.

In summary,

the inspectors

found that improvement

had

been

made

by

this organization

and that

TS requirements

regarding the

independent

reviews of plant changes,

tests,

and procedures

were

being

implemented satisfactorily,

Licensee

management

recently issued

information to plant personnel

describing

the self-assessment

process

and expectations

from

employees.

Line organization responsibilities

included individual

self-checking of work, independent verification by another

individual, supervisory observation of activity, post maintenance

testing,

management

tours,

and corrective action program

trending/reviews.

The

PNSC also contributed to line organization

self-assessment

activities.

The inspectors

attended

selected

PNSC meetings to observe

committee activities

and verify TS requirements

with respect

to

committee composition, duties,

and responsibilities.

Hinutes from

these

meetings

were also reviewed to verify accurate

documentation.

The inspector considered

the conduct

and

documentation of these

meetings to be satisfactory with good

discussion of the items presented.

During the July

21

PNSC

meeting,

the inadequate

testing of the emergency

bus undervoltage

logic circuitry was discussed.

Appropriate corrective actions

were assigned.

The regular monthly

PNSC meeting

was held

on

July 29, during which the reviews required

by TS 6.5.2.6 were

performed.

The plant general

manager

has set

an example for plant tour

expectations

by performing daily tours.

Area managers

tour plant

areas

weekly.

The operations

manager

was observed

in the control

room daily.

Plant management

continued to perform weekly

inspections of various plant areas.

The goal for these

inspections

was to include all areas within the powerblock

and the

emergency

service water,

emergency

diesel

generators,

and fuel

oi'1

storage

outside

areas

such that all areas

were toured

periodically.

The inspection

team consisted of the plant general

manager

and unit managers.

The results of several

of these

inspections

were reviewed.

Host of the findings were related to,

the general

cleanliness

and material condition of equipment.

This

type of managemen't

involvement

had

a positive effect on plant

housekeeping.

Supervisory

involvement

was evident during critical activities

involving TS equipment inoperability.

The infrequent activity

pre-evolution briefings require

management

involvement also. 'on-

critical supervisory

coaching of personnel

performance

was also

conducted.

Requirements

for the coaching

program were contained

in

a supervisory's

guide dated

February

26,

1991.

The inspector

reviewed the latest

annual

reports of coaching results

and several

of the individual observation

forms used to document

these

activities.

Observations

were conducted

at least yearly.

Comments

from these

observations

included round performance,

test/procedure

performance,

enforcement of procedural

compliance,

job skill enhancement,

deficiency identification, fire/safety

hazards,

self verification,

and communication.

The

ACR system

has

been, fully implemented.

Due to the lower

threshold for reporting problems

than the previous

system,

the

data

base has'rown

considerably,

which has

allowed more

meaningful

problem trending.

Self-identification of problems

was

considered

to be

a strength.

Adverse trends

were identified

involving valve mispositioning,

inappropriate parts/materials

issuance,

personnel

overtime,

work practices, fire barrier

inadequacy,

and tagging or labeling deficiencies.

10

c

~

Plant line orgapization

self-assessment

activities were considered

to be good which reinforced quality work and,the

safe operation of

the plant.

The

NSD Nuclear Plant Support Section

(NPSS)

no longer performs

the assessment

of the plants to the critical success

factors/performance'ndicators.

Instead,

plant personnel

assess

performance

compared to unit goals

and this information is

submitted to applicable corporate

organizations for review.

This

change discontinued

a comparison of the performance of the three

licensee

nuclear sites.

To compensate

for this; the licensee

is

developing corporate

standards

which will serve

as the unit goals

for all the licensee's

nuclear plants.

However,

NPSS personnel

provide corporate

support for generic plant programs

and perform

periodic observations

and reviews of plant activities.

The

assessments

performed

on plant activities was informal without

documentation

of review scope

or findings.

The inspectors

considered

that this assessment

process

could be strengthened

with

formal written expectations

of reviewers

and documentation

of

assessment

findings and the implementation of corporate

standards

for all sites.

~

~

~

7.

Preparations

for Refueling

(60705)

During this ins'pection period,

the licensee's

receipt

and inspection of

a new fuel shipment

was observed

on July 30,

1992.

Implementation of

applicable sections of the following procedures

was observed:

~ FHP-003

Unpacking

and Handling of New Fuel Assemblies,

Fuel Inserts

and

New Fuel Shipping Containers

~ FHP-004

New Fuel Handling Tool Operation

~ FHP-014

Fuel

and Insert Shuffle Sequence

~ FHP-020

Fuel Handling Operations

~ MMM-020

Operation,

Testing,

Maintenance

and Inspection of Cranes

and

Special Lifting Equipment

~ HPP-150

Receipt

and Surveillance of New Fuel

and Other Special

Nuclear Material

~ FMP-106

New Fuel Receipt

Inspection

The licensee

has received sixty fuel assemblies

for the next operating

cycle.

The inspector

observed

licensee

personnel

performing

a

reinspection of a fuel assembly'hich

was found to be slightly

scratched.

This damage

had

been

observed

during the inspection of a

previous fuel shipment.

This damage

was considered

to be negligible

and

use of the fuel assembly

was authorized.

The

new fuel inspectors

were

verified to be certified in accordance

with procedure

TI-109,

11

Refueling/Inspection

Team Training Program.

Receipt inspection

records

for the

new assemblies

were reviewed.

Licensee

personnel

identified

a

total of three fuel assemblies

with flaws that needed

to be evaluated.

The inspector

found that appropriate

devi ation reports

had

been

generated

to resolve these

issues.

It was determined that one assembly

had to be returned to the manufacturer for replacement.

The inspector

noted that attachments

from four different procedures

had

to be completed

by the operators

before fuel movement

was

commenced.

The senior reactor operator in charge of fuel movement

was very

knowledgeable

on the procedure

requirements

and performed the applicable

sections of the various procedures.

Although procedure utilization in

this case

was satisfactory,

the inspector felt that the procedures

could

be consolidated.

On the following day, the inspector discussed

the fuel movement

and

inspection with the senior reactor operator

who was in charge of the

fuel movement.

During this conversation

the inspector

was informed that

a fuel insert inspection

was also performed,

The operators

who

positioned

the

WABA for inspection, initially utilized a flexible strap

placed

around the"assembly

handling tool T-bar.

Operators later found

that it was quicker and easier to manually grasp

the insert

and withdraw

it the required

two feet for inspection.

The inspector questioned

whether this practice of insert withdrawal

was permissible

by plant

procedures.

Although operating

procedures

did not address

insert

movement,

procedure

FMP-106 was examined

and found to provide specific

guidance.

Section 6.3 of this procedure

specifies that the

WABAs be

handled

using the flexible strap

method.

Although little damage

could

incur from the operator's

hands-on

method of insert withdrawal, this

action

was not in accordance

with the licensee's

procedures

and is

considered

to be another

example of violation 400/92-15-01

discussed

in

paragraph

2.c of this report.

Review of Licensee

Event Reports

(92700)

The following LERs were reviewed for potential

generic

impact, to detect

trends,

and to determine

whether corrective actions

appeared

appropriate.

Events that were reported

immediately were reviewed

as

they occurred to determine if the

TS were satisfied.

LERs were reviewed

in accordance

with the current

NRC Enforcement Policy.

a

0

(Closed)

LER 91-08:

This

LER reported that the high head safety

injection system

was inoperable

due to

a failure of the system's

alternate miniflow lines.

The

LER was previously closed

in

NRC

Inspection

Report 50-400/91-23.

During the current inspection

period additional followup action

was performed related to this

event.

The inspector

reviewed

emergency

operating

procedures

and

operator training concerning

the potential diversion of flow from

the safety injection system through the alternate miniflow lines.

The inspector

found that the licensee

had

made

a change to the

EOP

User's

Guide to alert the operators

to the potentiality for this

event

and appropriate corrective action to take if necessary

to

12

isolate the diverted flow.

The licensee

had conducted training on

this event in the licensed

operator requal training during

August

12 - September

9,

1991.

Real

time training on the

procedure

changes

was provided,

and the changes

were included in

the required reading

notebook for operators

in January

1992.

Several

operating shifts were interviewed to determine

how they

would respond to this event.

The inspectors

found that the

training and procedure

changes

should

be effective in identifying

the diverted flow.

(Open)

LER 92-06:

This

LER reported that excess

flow check valves

associated

with the

RAB hydrogen supply line and auxiliary steam

line were mispositioned.

This resulted

in the failure of the

systems

to meet design requirements

and capability of the systems

to fulfilltheir safety functions.

The licensee

has completed

procedure

changes

to properly check the position for these

valves

and issued night orders describing the event

and prohibiting

hydrogen

supply system operation

unless

under direct operator

.

control.

Additional action will include real-time training,

inclusion of this event in the operator training program,

and

an

evaluation of using

an excess

flow check valve for the

RCDT as

well

as other waste

gas lines which contain hydrogen.

The

LER

will remain

open pending the completion of the above, activities.

(Closed)

LER 92-07:

This

LER reported

a reactor trip which

occurred

due to the failure of a main condenser

boot seal.

This

event

was previously discussed

in

NRC Inspection

Report 50-400/

92-13.

The licensee

completed

temporary repairs to the boot seal

which subsequently

failed again

on July 17,

1992.

The boot seals

were then replaced.

(Closed)

LER 92-08:

This

LER reported

a reactor trip which

occurred while the plant was in the hot standby condition with a

shutdown

bank of control rods withdrawn.

This event

was

previously discussed

in NRC Inspection

Report 50-400/92-13.

The

trip was caused

by

a low steam generator

level signal

due to

inadequate

control of feedwater,

The licensee

has

completed

a

debrief of the involved operations

personnel

and re-emphasized

attention to detail.

In addition the licensee

plans to perform

real-time training on this event.

(Open)

LER 92-09:

This

LER reported

a manual reactor trip which

was initiated following the loss of the running main feedwater

pump.

This event

was previously discussed

in

NRC Inspection

Report 50-400/92-13.

The licensee

has

completed repairs to the

fan supply breaker

and revised appropriate

maintenance

procedures

to detect this type of breaker failure.

The

LER will remain

open

pending the completion of operator training on this event.

(Open)

LER 92-10:

This

LER reported

another reactor trip which

occurred

due to the failure of the main condenser

boot seal.

This

event

was previously discussed

in

NRC Inspection

Report 50-400/

13

92-13.

The licensee

has replaced

both boot seals

and tested

the

main steam safety relief valve satisfactory.

The inspectors

observed this testing which showed that the safety valve was set

properly within setpoint tolerance.

Further review of post trip

data related to steam generator

pressures

revealed that manual

control of the steam generator

PORVs allowed steam pressure

to

increase

higher than normal

near the setpoint.

The inspectors

concluded that operator action to manually control

steam pressure

was inadequate

to prevent challenging the

steam generator

safety

valve.

Considering the observations

made in NRC Inspection

Report

50-400/92-13

regarding

inadequate

operator control of steam

generator levels,

licensee

management

was encouraged

to provide

additional training/guidance

regarding plant operator

response

to

reactor trips.

The

LER will remain

open pending the licensee's

investigation into other possible

boot seal failures.

g.

(Open)

LER 92-11:

This

LER reported that the emergency

bus

undervoltage logic circuitry was inadequately

tested.

Upon

reviewing

NRC Information Notice 92-40,

Inadequate

testing of

Emergency

Bus Undervoltage

Logic Circuitry, licensee

personnel

determined that the plant's

method for testing the undervoltage

circuitry was likewise deficient.

The test

method manually opened

the emergency

bus feed breakers

to simulate the low voltage

condition on the bus.

This method did not adequately verify that

the undervoltage circuitry would open the feed breakers

as

required.

When this situation

was identified, licensee

personnel

decided

that the surveillance

requirements

of TS 4.8. l. 1.2.f.4.(a)

were

not properly satisfied

and both emergency diesels

were declared

inoperable

at 1:35 p.m.,

on July 21.

A test procedure

was created

to check the omitted logic circuitry.

This procedure

was

performed satisfactory

on both emergency

bus feed breakers

and the

diesels

were declared

operable

by 2: 10 a.m.,

on July 22.

The

licensee

plans to revise the permanent test procedures

to correct

this deficiency.

The

LER will remain

open pending completion of

this additional action.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

1) at the conclusion of the inspection

on August 21,

1992.

During this

meeting,

the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed

in this report, with particular emphasis

on the Violation addressed

below.

The licensee

representatives

acknowledged

the inspector's

comments

and did not identify as

proprietary

any of the materials

provided to or reviewed

by the

inspectors

during this inspection.

No dissenting

comments

from the

licensee

were received.

Item Number

400/92-15-01

10.

Acronyms

and Initialisms

Descri tion and Reference

VIO:

Failure to properly implement plant

procedures,

paragraphs

2.c.

and 7.

ACR

-

Adverse Condition Report

EOP

-

Emergency Oprating Procedure

KV

-

Kilovolt

IEC

-

Instrumentation

and Control

LER

-

Licensee

Event Report

LLRT

-

Local

Leak Rate Test

NAD

-

Nuclear Assessment

Department

NCV

-

Non-Cited Violation

NPSS

-

Nuclear Plant Support Section

NRC

-

Nuclear Regulatory

Commission

NSD

-

Nuclear Services

Department

OSC

-

Operational

Support Center

PH

-

Preventive

Haintenance

PNSC

-

.

Plant Nuclear Safety Committee

PORV

-

Power Operated Relief Valve

RAB

-

Reactor Auxiliary Building

RCDT

-

Reactor Coolant Drain Tank

RHR

-

Residual

Heat

Removal

TS

-

Technical Specification

VIO

-

Violation

WABA

-

Wet Annular Burnable Absorber

Cl: