ML18010A434

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Insp Rept 50-400/91-21 on 910824-0928.Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Security,Fire Protection,Surveillance,Maint,Lers, & Main Control Board Annunciator
ML18010A434
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 10/09/1991
From: Christensen H, Shannon M, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18010A432 List:
References
50-400-91-21, NUDOCS 9111200027
Download: ML18010A434 (13)


See also: IR 05000400/1991021

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UNITEDSTATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 3M23

Report

Noe I

50-400/91-21

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

License No.:

NPF-63

Facility Name:

Harris

1

Inspection

Condu t

August 24 - September

28,

1991

Inspectors:

w,

endor Res>dent

nspector

ate

1gne

H.

Shannon.,

Resident

Inspector

Da

e

igned

Approved by:

. Chri st nsen,

Secti on Chi ef

Division of Reactor Projects

/vvI - 9-'F(

Date Signed

SUMMARY

Scope:

This routine inspection

was

conducted

by two resident

inspectors

in the areas

of plant

operations,

radiological

controls,

security,

fire protection,

surveillance

observation,

maintenance

observation,

licensee

event reports,

Plant

Nuclear

Safety

Committee activities,

main control

board

annunciator

review,

and licensee

action

on previous

inspection

items.

Numerous facility

tours were conducted

and facility operations

observed.

Some of these

tours

and,

observations

were conducted

on backshifts.

Results:

One violation was identified:

Failure to properly establish

a procedure for

properly setting the blowdown rings

on Crosby relief valves

(paragraph 9.e).

9111~000P7

911009

PDR

ADOCI( 05000400

PDFI

REPORT

DETAILS

1.

Persons

Contacted

Licensee

Employees

  • P. Beane,

Manager, guality Control

  • J. Collins, Manager,

Operations

  • C. Gibson,

Manager,

Programs

and Procedures

  • C. Hinnant,

General

Manager,

Harris Plant

D. McCarthy, Manager, Site Engineering

  • B. Meyer, Manager,

Environmental

and Radiation Monitoring

  • R. Morgan,

Manager,

Project Assessment

  • T. Morton, Manager,

Maintenance

  • J. Nevill, Manager,

Technical

Support

C. Olexi k, Manager,

Regulatory Compliance

A. Powell, Manager,

Harris Training Unit

R. Richey, Vice President,

Harris Nuclear Project

H. Smith, Manager,

Radwaste

Operation

  • F. Strehle,

Manager, guality Assurance

Engineering

  • M. Wallace,

Sr. Specialist,

Regulatory Compliance

E. Willett, Manager,

Outages

and Modifications

W. Wilson, Manager,

Spent Nuclear Fuel

Other

licensee

employees

contacted

included

office,

operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

Acronyms

and initialisms

used

throughout this report are listed in the

last paragraph.

2.

Review of Plant Operations

(71707)

The plant continued in power operation

(Mode 1) for the duration of this

inspection period.

a ~

Shift Logs

and Facility Records

The inspector

reviewed

records

and discussed

various entries

with

operations

personnel

to verify compliance,. with

the

Technical

Specifications

(TS)

and

the licensee's

administrative

procedures.

The following records

were reviewed:

Shift Supervisor's

Log; Control

Operator's

Log; Night Order Book; Equipment Inoperable

Record; Active

Clearance

Log; Jumper

and

Wire Removal

Log; Temporary Modification

Log; Chemistry Daily Reports; Shift Turnover Checklist;

and selected

Radwaste

Logs.

In addition,

the inspector

independently

verified

clearance

order tagouts.

The inspectors

found the

logs to

be readable,

well organized,

and

provided

sufficient

information

on

plant

status

and

events.

Clearance

tagouts

were

found

to

be

properly

implemented.

No

violations or deviations

were identified.

b.

Facility Tours

and Observations

Throughout

the inspection

period, facility tours

were. conducted.to

observe

operations,

surveillance,

and

maintenance

activities

in

progress.

Some

of these

observations

were

conducted

during

backshifts.

Also, during this inspection

period,

licensee

meetings

were attended

by the inspectors

to observe

planning

and

management

activities.

The facility tours

and observations

encompassed

the

following areas:

security perimeter

fence; control

room;

emergency

diesel

generator

building;

reactor

auxiliary building;

waste

processing

building;

turbine

building;

fuel

handling

building;

emergency

service

water

building;

battery

rooms;

electrical

switchgear

rooms;

and the technical

support center.

During these tours,

the following observations

were made:

(I)

Monitoring Instrumentation

- Equipment operating

status,

area

atmospheric

and liquid radiation monitors, electrical

system

. lineup,

reactor

operating

parameters,

and auxiliary equipment

, operating

parameters

were

observed

to verify that indicated

parameters

were

in accordance

with the

TS for the current

operational

mode.

(2)

Shift Staffing - The inspectors

verified that operating shift

staffing was in accordance

with TS requirements

and that control

room

operations

were

being

conducted

in

an

orderly

and

professional

manner.

In addition,

the inspector

observed shift

turnovers

on various occasions

to verify the continuity of plant

status,

operational

problems,

and

other

pertinent

plant

information during these

turnovers.

(3)

Plant

Housekeeping

Conditions

-

Storage

of material

and

components,

and

cleanliness

conditions

of various

areas

throughout

the facility were

observed

to determine

whether

safety and/or fire hazards

existed.

(4)

Radiological

Protection

Program - Radiation protection control

activities

were

observed

routinely to verify that

these

activities

were in conformance

with the facility policies

and

procedures,

and in compliance with regulatory requirements..

The

inspectors

also

reviewed

selected

radiation

work permits

to

verify that controls

were adequate.

(5)

Security Control -

The

performance

of various shifts of the

security force was

observed

in the conduct of daily activities

which included:

protected

and vital

area

access

controls;

searching

of personnel,

packages,

and vehicles;

badge

issuance

and retrieval; escorting of visitors; patrols;

and

compensatory'osts.

In addition,

the inspector

observed

the operational

status

of

Closed

Circuit Television

(CCTV) monitors,

the

Intrusion Detection

system

in the central

and

secondary

alarm

stations,

protected

area

lighting, protected

and vital area

barrier integrity,

and the security organization interface with

operations

and maintenance.

(6)

Fire Protection

- Fire protection activities, staffing

and

equipment

were observed

to verify that fire brigade staffing was

appropriate

and

that fire alarms,

extinguishing

equipment,

actuating

controls,

fire

fighting

equipment,

emergency

equipment, and.fire barriers

were operable.

The

inspectors

found

plant

housekeeping

and

component

material

condition to be quite 'good.

The licensee's

adherence

to radiological

controls,

security controls, fire protection

requirements,

and

TS

requirements

in these

areas

were satisfactory.

c.

Review of Nonconformance

Reports

Adverse

Condition

Reports

(ACRs)

were

reviewed

to verify the

following:

TS were complied with, corrective actions

as identified

in the reports

were

accomplished

or being

pursued for completion,

generic

items

were identified and reported,

and

items were reported

as required

by the TS.

No violations or deviations

were identified.

3.

Surveillance

Observation

(61726)

Surveillance

tests

were observed

to verify that approved

procedures

were

being

used;

qualified personnel

were

conducting

the tests;

tests

were

adequate

to verify equipment

operability;

calibrated

equipment

was

utilized; and

TS requirements

were followed.

The following tests

were observed

and/or data reviewed:

OST-1008

RHR Pump Operability

OST-1092

1B-SB Residual

Heat

Removal

Pump Operability

OST-1108

RHR Pump Operability

OST-1502

RHR Loop Suction

Remote Position Indicating and Timing Test

OST-1804

RHR Remote Position Indication and Timing Test

EPT-033

Emergency

Safeguards

Sequencer

System Test

EST-220

Type

C LLRT of Containment

Purge

Exhaust Penetration

(M-58)

The

performance

of these

procedures

was

found to

be satisfactory with

proper

use

of calibrated

test

equipment,

necessary

-communications

established,

notification/authorization

of control

room personnel,

and

knowledgeable

personnel

performing the tasks.

No violations or deviations

were identified.

4.

Naintenance

Observation

(62703)

The

inspector

observed/reviewed

maintenance

activities

to verify that

correct

equipment

clearances

were

in effect;

work requests

and fire

prevention

work permits,

as

required,

were

issued

and

being followed;

quality control

personnel

were available for inspection activities

as

required;

and,

TS requirements

were being followed.

Haintenance

was observed

and work packages

were reviewed for the following

maintenance

(WR/JO) activities:

Replacement

of solenoid

in trip logic for the "8" emergency

diesel.

generator.

"A" chiller trip and subsequent

troubleshooting.

"8" containment

exhaust isolation valve leak repairs.

"8"

emergency

diesel

generator

sequencer

failure

and

subsequent

troubleshooting.

The inspectors

found the performance

of the above work to be satisfactory

with proper implementation of independent

verification requirements.

The

performance

of the time-dependent

maintenance

on the sequencer

was well

organized

and well executed.

No violations or deviations

were identified.

5.

Review of Licensee

Event Reports

(92700)

The following LERs were reviewed for potential

generic

impact, to detect

trends,

and to determine

whether corrective actions

appeared

appropriate.

Events that were reported

immediately were reviewed

as

they occurred to

determine if the

TS were satisfied.

LERs were reviewed in accordance

with

the current

NRC Enforcement Policy.

a ~

(Closed)

LER 90-08:

This

LER reported

a discrepancy

in the amperage

rating for a circuit breaker

providing overcurrent protection for an

electrical

containment

penetration.

This matter

was

previously

discussed

in

NRC Inspection

Report 50-400/90-14.

The licensee

has

completed

a review of other circuits for similar discrepancies

and

,

has revised plant drawings accordingly.

b.

(Closed)

LER 90-17:

This

LER repor ted

the inoperability of an

essential

services chiller.

This event

was previously discussed

in

NRC Inspection

Report 50-400/90-14

and

was the subject of a licensee

identified violation

(NCV 400/90-14-01).

The licensee

has completed

identification tagging of the chiller valves

and installation of a

trough to help protect tubing and valves.

co

(Open)

LER 91-16:

This

LER reported

the lifting of several

component

cooling water relief valves

during

a

pump start.

This matter

was

previously discussed

in

NRC Inspection

Report

50-400/91-18

and

was

the subject of an unresolved

item (URI 400/91-18-01).

This event

was

also similar to an event which occurred in August 1990, during which

operation

of two

CCW

pumps

caused

component

cooling water

system

pressure

to increase

and

CCW system relief valves lifted and failed

to reset.

The licensee

is presently ,limiting system

pressure

to

approximately

95 psig

by initiating flow through

a residual

heat

removal

heat exchanger.

Procedural

guidance

and training have

been

provided to establish

proper relief valve settings.

The

blowdown

ring settings

of all

CCW system relief valves

were verified to be

properly set.

The

licensee

is

pursuing

plant modifications to

correct this recurrent

problem

and

is investigating

other plant

systems

with .similar relief valves.

.The

LER will remain

open pending

completion of this additional corrective action.

d.

(Open)

LER 91-17:

This

LER reported that

a composite

sample for a

secondary

waste

tank continuous

release

was not taken

as required

by

the

TS.

Since

no activity was

indicated

by in-line radiation

monitors

or isotopic analysis

of the water prior to release,

the

licensee

determined

that

no safety

consequences

resulted

from

this'vent.

The licensee's

corrective action will include counseling of

the

technician

who failed to initiate the

composite

sample

and

revising the applicable plant procedure to require

a signoff for this

action being completed.

The

LER will remain

open pending completion

of the corrective action.

No violations or deviations

were identified.

6.

Annual

Emergency Drill (71707)

On September

10,

1991,

the

annual

emergency drill was

conducted

by the

licensee

to verify the

effectiveness

of the

Radiological

Emergency

Response

Plan

and

implementing

procedures.

Details

of the drill,

including the results of critiques held,

are discussed

in

NRC Inspection

Report 50-400/91-24.

The inspectors

noticed

a slight delay

by the

licensee

when declaring

emergency classifications.

This tended to also delay the reporting of the

event to the State

and the

NRC.

In general,

however,

performance

during

the drill was considered

to

be excellent

and the scenario

was considered

to be challenging.

Review of Plant Nuclear Safety Committee Activities (40500)

The

inspectors

attended

selected'NSC

meetings

to

observe

committee

activities

and

verify

TS

requirements

with respect

to

committee

composition, duties,

and responsibilities.

Minutes from this meeting were

also

reviewed

to verify accurate

documentation.

Besides

the typical

monthly required topics, efforts to trend reactor coolant

pump oil leakage

and action to

be taken

on low oil reservoir level

were discussed.

The

trending

and action plan were created

by system engineers

but received

the

additional

review by the

PNSC for conservatism.

The inspector

considers

the

conduct of these

meetings

to

be

good

and that committee actions/

recommendations

enhance

the safe operation of the plant.

No violations or deviations

were identified.

Main Control

Board Annunciator Review (71707)

Due to recent

industry events

involving loss of power to main control

board annunciator

systems,

a review of the plant annunciator

system

was

performed in accordance

with an

NRC memorandum

dated August 19,

1991.

The

Final Safety Analysis Report,

system description, electrical, drawings,

and

plant incident

reports

associated

with the

annunciator

system

were

reviewed

during this effort.

A loss of power to the annunciator

system

was also discussed

with operating

personnel

to determine

what action they

would perform.

The annunciator

system is powered

by three internal annunciator

inverters

which, in turn, receive

power from primary and standby

power sources.

The

primary source of power's

from 120

VAC distribution panel

UPP-lA which

receives

power from an uninterruptible

power supply fed from non-safety

480

VAC motor control centers

MCC-1D21 and

MCC-1E21.

The standby

source

of power consists

of 125

VDC distribution panel

DP-1A-1 which receives

power from the station battery or associated

battery chargers.

Selection

of the primary or standby

power supply is via an automatic transfer relay

in the internal

annunciator

inverter which senses

voltage degradation

on

the primary source

and automatically switches

to the standby

source.

The licensee's

emergency

action level flowpaths require the declaration of

an

ALERT if 50 percent

or more of the annunciators

lose

power for greater

than

10 minutes.

A SITE

AREA

EMERGENCY is declared if this loss is

coincident with a plant transient.

A previous event at Harris occurred in

August

1988

where

approximately

60~ percent of the 'main control

board

annunciators

lost power.

The licensee

declared

an ALERT and power to the

annunciator

system

was quickly restored.

In conclusion,

the inspector

found that the annunciator

system

had

a

reliable source of power, action required in case of loss of power to the

system

was appropriately

specified,

and operators

were

knowledgeable

of

the required action.

No violations or deviations

were identified.

9.

Licensee

Action" on Previously Identified Inspection

Findings

(92702

5

92701)

a.

(Closed)

IFI 400/90-10-03:

Follow licensee's

activities to correct

linkage failure of emergency

service chiller return valves.

The licensee

plans to continue

using the present

"monoball" linkage

assemblies

for

these

valves.

The failure rate of this

type of

linkage

does

not appear

to

be excessive

and this action

was

deemed

appropriate.

b.

(Closed) Violation 400/90-21-04:

Failure to perform

a written safety

evaluation.

c ~

d.

e.

The

inspector

reviewed

and verified completion of the corrective

actions listed in the licensee's

response letter dated

December

28,

1990.

This matter

was previously discussed

in

NRC Inspection

Report

50-400/91-10.

The licensee

performed

a written safety evaluation of

the increase

in activity in the spent fuel pools

and determined that

although

an increase

in calculated

dose rates

would result during

a

potential

accident,

this

increase

was still well within allowed

limits.

An additional

review of the

design

basis

for the fuel

handling

building

and

supporting

systems

was

conducted

and

appropriate

procedure

revisions

were implemented.

(Closed) Violation 400/90-26-01:

Failure to maintain administrative

control of a high radiation area

key.

The

inspector

reviewed

and verified completion of the corrective

actions listed in the licensee's

response letter dated

March 1, 1991.

Appropriate plant procedures

and the corporate

Radiation Control

and

Protection

Manual

were revised to provide more prescriptive

guidance

for control of high radiation areas.

Further, the licensee

reviewed

this

event

and

the results

of an

independent

assessment

of .the

incident, with technicians

and supervisors.

(Closed)

IFI 400/91-06-01:

Review licensee's

corrective action to

close exterior doors during severe

stor'm warnings.

The

licensee

will revise

procedure

AP-301,

Adverse

Weather.

Operations,

to close

the exterior

doors

upon receipt of a severe

storm watch.

This action should

provide

enough

time to close the

doors

before actually experiencing

a severe

storm.

The licensee

is

also considering providing quick disconnects

on cables/hoses

that are

run through these

doors to facilitate rapid removal.

(Closed)

URI 400/91-18-01:

Improper

Crosby relief valve

blowdown

ring settings.

After further

review

by the

licensee, it was

determined

that

approximately

34

Crosby relief valves,'n

various

safety-related

systems

required verification of proper

blowdown ring settings.

All

of the valves that were checked

were found to be set improperly, from

a

few

notches

to

over

170

notches

from the

required

setting.

Detailed

procedures

or training

had

not

been

provided

and

the

maintenance

staff had not correctly implemented

the technical

manual

recommendations

which subsequently

resulted

in improper blowdown ring

settings.

An internal justification for continued

operation

is in effect for

three relief valves,

which if set improperly could adversely affect

system operation.

Precautions

are in place to limit system inventory

losses if these relief valves

open

and

do not reset.

The three

relief valves will be

checked for proper

blowdown ring settings

during the

next plant outage.

Fifteen additional

valves will be

checked

at

the

next available

system(s)

outage.

The licensee's

failure to provide the maintenance

staff with adequate

training and

procedures

for adjusting

the Crosby relief valve's

blowdown ring is

considered

to be

a violation.

Violation (400/91-21-01):

Failure to properly set the blowdown rings

on Crosby relief valves.

10.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

1)

at the conclusion of the inspection

on September

28,

1991.

During this

meeting,

the

inspectors

summarized

the

scope

and

findings of the

inspection

as

they are detailed

in this report, with particular emphasis

on

the

Violation

addressed

below.

The

licensee

representatives

acknowledged

the inspector's

comments

and did not identify as proprietary

any of the materials

provided to or reviewed

by the inspectors

during this

inspection.

Item Number

Descri tion and Reference

400/91-21-01

11.

Acronyms

and Initialisms

VIO:

Failure to properly set the blowdown rings

on Crosby relief valves.

(Paragraph

9.e.)

ACR

CCTV

CCW

CFR

EPT

EST

IFI

LER

NCV

NRC

OST

Adverse Condition Report

Closed Circuit Television

Component Cooling Water

Code of Federal

Regulations

Engineering

Performance

Test

Engineering Surveillance Test

Inspector

Follow-up Item

Licensee

Event Report

Non-Cited Violation

Nuclear Regulatory

Commission

Operations

Surveillance

Test

'I

PNSC

PSIG

RHR

TS

URI

VAC

VDC

VIO

WR/JO

Plant Nuclear Safety Committee

Pounds

per Square

Inch Gage

Residual

Heat Removal

Technical Specification

Unresolved

Item

Volt Alternating Current

Volts Direct Current

Violation

Work Request/Job

Order