ML18005A786

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Insp Rept 50-400/89-01 on 890109-13.No Violations or Deviations Noted.Major Areas Inspected:Liquid & Gaseous Radioactive Effluents & Plant Chemistry
ML18005A786
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 02/09/1989
From: Hughey C, Kahle J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18005A785 List:
References
50-400-89-01, 50-400-89-1, NUDOCS 8902270114
Download: ML18005A786 (11)


See also: IR 05000400/1989001

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MAAIETTAST., N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/89-01

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Ral ei gh,

NC

27602

Docket No.:

50-400

License No.:

NPF-63

Facility Name:

Shearon Harris Nuclear

Power Plant

Inspection

Conducted:

January

9-13,

1989

Inspector:

c~

C.

.

ug ey

.

Approved by:

<~"vJ-

J;

B.

Ka

e, Chief

Ra

ological Effluents and Chemistry Section

Emergency

Preparedness

and Radiological

Protection

Branch

Division of Radiation Safety

and Safeguards

D

e Si

ne

Da

e Signed

SUNMARY

Scope:

This routine,

unannounced

inspection

was

conducted

in the

areas

of

liquid and gaseous

radioactive effluents

and plant chemistry.

Results:

Although inoperability

of

several

liquid radioactive

effluent

monitors

and stack

gaseous

effluent flow measurement

devices

had continued to

keep the licensee

in ACTION statements

of the Technical

Specifications,

there

had

been considerable

progress

toward permanent

resolutions

and fixes of these

complicated

problems.

These

issues

had

been identified during

a previous

inspection

as

Inspector

Followup Items

88-24-01

and 88-24-02

and will remain

open.

No violations or deviations

were identified.

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S

REPORT

DETAILS

1.

Persons

Contacted

Licensee

Employees

S.

Buch, Technician,

Environmental

and Chemistry

(E&C)

  • C. Hinnant, Plant General

Manager

S. Johnson,

Foreman,

E&C

J.

Leonard, Project Specialist,

Radwaste

  • H. Lipa, Supervisor,

E&C

  • A. Poland,

Project Specialist,

Radiation Control

B. Sears,

Foreman,

E&C

  • J. Sipp, Manager,

Environmental

and Radiation Control

E. Steudel,

Principal Engineer,

Special

Projects

  • D. Tibbits, Director, Regulatory Compliance

M. Wallace, Senior Specialist,

Regulatory Compliance

E. Wills, Project Specialist

Other

licensee

employees

contacted

included

construction

craftsmen,

engineers,

and technicians.

Nuclear Regulatory

Commission

  • W. Bradford,

SRI

  • Attended exit interview

2.

Licensee Action on Previously Identified Inspector

Followup Items

(92701)

a ~

(Open)

Inspector

Followup

Item (IFI) 50-400/88-24-01:

Review

licensee

resolution of contamination of liquid radwaste monitors.

As discussed

in Inspection

Report

No. 88-24,

contamination

buildup

within the

sample

chambers

of the liquid radwaste

monitors during

discharges

caused

monitor setpoints

to

be

exceeded

during releases

thereby

prematurely

terminating discharges.

The monitors affected

are listed as follows:

1) REM-01WL-3540, Treated

Laundry and Hot Shower Tank Discharge

2) REM-21WL-3541, Waste Monitor Tank Discharge

3) REM-21WS-3542,

Secondary

Waste

Sample

Tank Discharge

(continuous

release

path)

Although contamination buildup in the stainless

steel

sample

chambers

of

the

liquid

radwaste

monitors

was

indeed

occuring

during

discharges,

the

licensee

considered

extremely

low setpoints

calculated

prior to

each

release

to

be

the root

cause

of their

problem.

Some buildup of contamination in the stainless

steel

sample

'

chambers

cannot

be avoided.

The licensee

indicated that forthcoming

changes

to the Offsite Dose Calculation

Manual

(ODCM) involving the

addition of background

counts

into the

setpoint

calculation

and

increasing dilution flow to the cooling tower blow down line would

permit

an

increase

in

the

monitor setpoint

during

discharges

sufficient to eliminate spurious

discharge

terminations.

During the inspection,

all three of these

Technical

Specification

required

monitors

were out of service for various

reasons,

placing

the

licensee

in continuous

ACTION statements

of the

Technical

Specifications.

The licensee

indicated that these monitors would be

back in service within several

days after the inspection.

This item

remains

open.

b.

(Open)

IFI 50-400/88-24-02:

Review licensee

resolution

of flow

measurement

device operability in plant stacks.

As discussed

in Inspection

Report

No. 88-25, turbulent flow problems

in three

out of four plant gaseous

effluent stacks

(Nos.

1,5 and 5a)

caused

by the relatively short

and wide design of these

stacks

had

prevented

the licensee

from accurately

measuring

the flow ~ates

out

of these

stacks.

This had placed

the licensee

in continuous

ACTION

statements

of the Technical

Specifications

requiring periodic flow

rate estimations.

Previous flow modifications

had been unsuccessful

in restoring uniform flows to the plant stacks.

The

licensee

stated

that,

to resolve

the

issue,

the total

flow

through

a

stack

would

be quantified

by the

summation

of all

individual influents into each

stack.

This would be applicable for

stacks

1,

5 and

5a.

To accomplish this,

a microprocessor unit would

summarize

the influents for each

stack

by sensing

the operation of

the fan motors under various fan configurations.

Microprocessor flow

values will be

determined

from in situ flow measurements

under

various

fan configurations.

Plans

are for the

system

to

be

installed,

tested

and

operational

by

September

1989.

This

item

remains

open.

3.

Temporary

Radwaste

Demineralizer

(84750)

Plans

were

discussed

to

temporarily

install

a

vendor

supplied

(Chem-Nuclear)

liquid radwaste

demineralization

system

as

a

one year

demonstration

project.

This

system

was

to

be

used

instead

of the

permanently installed radwaste

system to decontaminate

liquid wastes prior

to discharge

and

was very similar to a system installed at Carolina

Power

and Light's Robinson

Nuclear

Power Plant.

The licensee

anticipated

the

system to be operational

by the end of January

1989.

Approximately six months

into the

demonstration

period,

the licensee

planned to evaluate

the system's

performance

and decide whether or not to

continue using this system

beyond the one year demonstration

period.

During this period,

the

permanently

installed

radwaste

system will be

shutdown

and

placed

into wet lay-up.

During wet lay-up, calibrations

would be maintained

on essential

in-line instrumentation

and pumps/motors

'ould

be stroked

and rotated periodically to maintain system operability.

The

membranes

from the

reverse

osmosis

units

were to

be

removed

and

stored.

No violations or deviations

were identified.

Steam Cycle Chemistry

(79701)

The inspector

reviewed chemistry data plots for October

and

November

1988.

Steam Generator

Owner's

Group's

Secondary

Water Chemistry Guidelines

were

exceeded

on

several

occasions

for

steam

generator

blowdown cation

conductivity,

sodium

and sulfates.

The major

source of these

impurities

was most likely condensate

polisher effluents.

Host of these

excursions

occured

during plant startup after

the -outage

and

subsequent

to

two

reactor trips/restarts.

These all occurred

during October

1988.

This

highlighted

the

need for higher

steam

generator

blowdown rates

during

plant startups.

To reduce

cation conductivity

and

sodium levels in the

blowdown during

power operations,

rinse

times

were

increased

after each

regeneration

of

anion

resins

from the

condensate

polishers

reducing

the

effluent

conductivity from 300

uS/cm to less, than

100 uS/cm.

After depletion,

mixed

bed resins

are transferred

from each in-service condensate

polisher

vessel.

The cation and anion resins

are separated

and regenerated.

After

regeneration

and rinsing,

the

anion

and cation

resins

are

mixed

back

together

and transferred

to an empty condensate

polisher vessel.

Prior to

placing

back in service,

the vessel

is recirculated

in

a closed

loop to

less

than

0.1

uS/cm to

reduce

contaminants

thrown from the polishers.

Preliminary testing indicated these

techniques

to be effective.

Contaminant

concentration

had

also

been

occurring

when

steam

generator

blowdown lines

were isolated

daily for about

one

hour

during plant

calorimetric testing.

To

reduce

this

buildup,

blowdown

was

being

temporarily increased prior to blowdown isolation.

For the

period

reviewed

in this inspection,

steam

generator

blowdown

cation conductivities

ranged

between

0.2

and

0.3

uS/cm, with chloride

levels averaging just under

2 parts

per billion (ppb).

Feedwater

cation

conductivity

averaged

less

than

0.07

uS/cm, with dissolved

oxygen

less

than 0.5 ppb and sodium less

than 0.1 ppb.

No violations or deviations

were identified.

Staffing (84750)

Since

the last

inspection

in this

area,

Foreman

positions

in the

Environmental

and Chemistry

(E&C) group had increased

from two to three.

There

had been

no major changes

in the technician staff of 11 licensee

and

11 contract

employees.

No turnover problems

were noted.

No violations or deviations

were identified.

6.

Followup of Unusual

Event (93702)

On

December

16,

1988,

during

a treated

laundry

and

hot

shower

tank

release,

a valid high radiation level trip occurred

on the

RBl-01WL-3540

monitor.

The high alarm setpoint

was

exceeded,

automatically terminating

the release.

The licensee identified this incident

as

an Unusual

Event

and

made the proper notifications to NRC.

The licensee

stated that the cause of the alarm appeared

to be settling in

the

tank during the discharge.

Pre-release

grab

sample activity in the

tank after pre-sampling

recirculation

was about

1.7 E-06 microcuries

per

milliliter (uCi/ml).

The monitor high alarm setpoint

was calculated

and

set

at

1.55 E-05 uCi/ml with monitor background

at the time normal at

about

1.21 E-05 uCi/ml.

The alarm

and

subsequent

discharge

isolation

occurred at about

5X tank level.

A post-release

grab

sample indicated the

tank activity to

be

about

2.5 E-05 uCi/ml, verifying

an

increase

in

activity during the discharge.

The tank

had

been properly recirculated

prior to taking the pre-release

grab sample.

To prevent

reoccurrences,

discharges

from the treated

laundary

and hot

shower

tank were

to

be terminated

at about

15'A tank level

and the tank

periodically cleaned.

Changes

in monitor setpoint calculation methodology

(see

Paragraph

2.a) would also prevent unplanned

discharge

terminations.

No violations or deviations

were identified.

7.

Records

Review (84750)

The inspector

reviewed the following laboratory records:

a.

Gross

alpha composite

sample

analyses

results for December

1988,

from

the plant vent stacks

(1, 3a, 5, and 5a).

All were found to be less

than the lower limit of detection.

b.

Intensity,

gain, resolution,

and

background quality control charts

for the

gamma

spectroscopy

system for November

and

December

1988.

System operability appeared

stable for the period.

C.

guality control charts for the following laboratory

instruments

and

analyses:

1.

Perkin

-

Elmer

3030B

Atomic Absorption

Spectrophotometer:

Copper, Iron, Sodium, Lithium

2.

Perkin - Elmer

Lambda

3B

UV/VIS Spectrophotometer:

Silica,

Hydrazine

3.

DIONEX 2020I Ion Chromatograph:

Chlorides, Fluorides,

Sul fates

The control charts

were well organized

and complete.

Selected

laboratory

personnel

appeared

knowledgeable

in their use

and importance.

No violations or deviations

were identified.

Semiannual

Effluent Release

Reports

(84750)

The inspector

reviewed the semiannual

radioactive effluent release

report

for the period January

1 through

June

30,

1988.

This review included

an

examination

of the liquid and

gaseous

effluent release

data for this

period

as

compared

to 1987 data

and to other Region II facilities.

This

data is summarized

in the attachment

to this report.

No abnormal

gaseous

or liquid releases

were reported during the first half

of 1988.

No significant trends

were noted in either liquid or gaseous

effluents during the first half of 1988 as

compared to 1987.

Data values

compared favorably to other Region II PWR plants.

No violations or deviations

were identified.

Additional Dilution Water Flow (84750)

During the last inspection in this area

(Inspection

Report

No. 88-24), the

inspector

and the licensee

discussed

the addition of piping that would

supply

increased

dilution water flow to the circulating water

blowdown

line from the cooling tower make-up line, bypassing

the cooling water

basin

and circulating water

system.

This additional

flow was to enable

the

licensee

to increase

the setpoint

points of the liquid radwaste

monitors during discharges

reducing the chances for inadvertent discharge

terminations

and to help conserve

water treatment

chemicals

used in the

circulating water

system.

During that

inspection,

construction

and

installation of this bypass line had not been completed.

During this inspection,

the

licensee

indicated

that

the

bypass

line

installation

and initial testing

had been completed.

This additional line

would enable

the licensee

to increase

flow in the cooling tower blowdown

line from 900 gallons

per minute to almost

18,000 gallons

per minute, at

the

maximum flow rate.

Flow rates

through

the line had

been verified

during testing

using

a combination

of make-up

pump curves

and various

pressure/flow indicators in the system.

In order to claim this additional

flow for the purpose of increasing

the

liquid radwaste

effluent monitors

setpoints

and to verify system flow

after it was placed into service,

double flow verification was required.

Two flow elements

had been installed in an above-ground,

u-bend section of

the bypass line piping adjacent

to the isolation valve for that purpose.

During testing,

however,

the indicated flow rates of the two elements

did

not agree.

The licensee

determined that inconsistent water levels in the

u-bend

area

caused

the disagreement.

Piping configuration

changes

would

be required to alleviate

the problem.

At the time of the inspection,

these

changes

were in the design/approval

process.

No violations or deviations

were identified.

Radiation Monitoring System

(84750).

The

Radiation

Monitoring

System

(RMS)

was

the

plant-wide

radiation

information

gathering

and

control

system

designed

to provide plant

personnel

with current

and

historical

measurements

of radiological

conditions

in

the

plant

during

normal

and

design

basis

accident

conditions.

The

system

included

the

process

and effluent radiation

monitors

and the airborne

and area radiation monitors.

An excessive

number of inputs to the

system

(160 total) resulted

as the

Harris project

was

reduced

from a four unit to

a single unit site, since

the

RMS was originally designed for a four unit plant.

This also resulted

in

unnecessary

personnel

and

resource

requirements

(calibrations,

maintenance,

spare parts, etc.)

as the plant

became operational,

Previous

to this

inspection,

the

licensee

had

formed

a

task

force

consisting of personnel

from various plant. disciplines to evaluate

the

RMS

and

recommend

a

plan

to plant

management

to streamline

the

RMS

by

selecting certain unnecessary

or redundant

monitors for deletion from the

system,

redesignation,

or other

appropriate

methods.

This

plan

was

formulated with various priorities taken into account

such

as Regulatory

Guide 1.97 requirements,

Techncial

Specification/ODCM requirements,

safety

needs,

and

needs

contributing to more efficient and safe plant operation

but not necessarily

required

by regulations.

Some examples of unnecessary

monitors

to

be deleted

were

area

radiation monitors in various

locker

rooms

and

a particulate

and

iodine monitor in the

Health

Physics

instrument calibration

room.

Previous to this inspection,

the task force had formalized and

recommended

a plan of action to the Plant Nuclear Safety

Committee

and

was in the

initial steps

of submitting

change

requests.

Progress

in this area will

be followed closely during upcoming inspections.

No violations or deviations

were identified.

Whole-body Counting

During

a

phone

conversation

subsequent

to this inspection

(January

30,

1989), the inspector

discussed

with the Manager of the Environmental

and

Radiation

Control

Group the benefits of informing visitors

who require

whole-body

monitoring

that

whole-body

counters

calibrated

for the

detection of fission products will not necessarily

provide accurate

data

for naturally occurring potassium-40.

11.

Ex it Intervi ew

The inspection

scope

and findings were

summarized

on January

13,

1989,

with those

persons

indicated in Paragraph

1.

The inspector

described

the

areas

inspected

and

discussed

in detail

the

inspection

findings.

No

dissenting

comments

were received

from the licensee.

The licensee

did not

identify as proprietary any of the material

provided to or reviewed

by the

inspector during this inspection.

ATTACHMENT

SHEARON HARRIS

RADIOACTIVE EFFLUENT SUMMARY

No. of Abnormal Releases

a.

Liquid

b.

Gaseous

a.

Liquid

1.

Fission

and Activation

Products

2.

Tritium

3.

Gross

Alpha

b.

Gaseous

1.

Fission

and Activation

Gases

Iodines

Tritium

Gross

Alpha

Particulate

(gross

beta/gamma)

2.

3.

4,

5.

Liquid Waste

Released

(gallons)

Activity Released

(Curies)

1987

1.83

E+07

9.08 E-1

2.48

E+2

2.73 E-4

1.71

E+3

0.00

E+0

0.00

E+0

3.15 E-6

4.43 E-6

First half of 1988

1.11

E+7

1.86 E-2

2.40

E+2

2.55 E-6

1.44

E+3

0.00

E+0

0.00

E+0

6.55 E-8

0.00

E+0