ML18004B895
| ML18004B895 | |
| Person / Time | |
|---|---|
| Site: | Harris |
| Issue date: | 07/17/1987 |
| From: | Belisle A, Mellen L, Moore R, Michael Scott NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18004B892 | List: |
| References | |
| 50-400-87-20, NUDOCS 8707300481 | |
| Download: ML18004B895 (18) | |
See also: IR 05000400/1987020
Text
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
ATLANTA,GEORGIA 30323
Report No.:
50-400/87-20
Licensee:
Carolina
Power
a'nd Light Company
P. 0.
Box 1551
Raleigh,
NC
27602
Docket No.:
50-400
Facility Name:
Shearon
Harris
1
inspection
Conducted:
Jun
1-5,
1987
License No.:
Inspectors:
Yi. Scott
/
I"
L. Yiellen
I
A'~w
R.
Moore
Approved by:
A.
el i sl e,
f
guality Assurance
Programs
Section
Div i s i on
of Reactor
Sa fety
Date
igned
77
Da
e S'igned
Da
e Signed
Da
e
igned
SUYiMARY
Scope:
This routine,
unannounced
inspection
was
conducted
in the
areas
of
design control
and licensee
action
on previously identified inspection findings.
Results:
Gne violation was identified.
87p7g
<81 87p7p2
8
DCICg, psppp4pp
REPORT
DETAILS
Persons
Contacted
Licensee
Employees
R. Biggerstaff, Principal Engineer,
Onsite Nuclear Safety
(ONS)
G. Blinde, Senior Specialist,
Training
G. Cambell,
Manager,
Maintenance
R. Garner, Shift Foreman,
Operations
P. Gordy, Harris Plant Construction
Section
(HPCS) Engineer
T. Gilbert, Quality Assurance
(QA) Specialist
"J. Harness,
Assistant
Plant General
Manager
W. Harris, Senior Engineer,
Technical
Support
(TS)
C. Jeffries,
Regulatory
Compliance Specialist
"R.
Lamb, Senior Engineer,
Harris Plant Engineering
Section
(HPES)
~T. Lentz, Engineering
Supervisor,
TS
"L. Loflin, Manager,
HPES
- E. Martin, Senior
QA Specialist
"C. McKenzie, Principal
QA Engineer
L. Olsen,
Engineer,
TS
W. Ponder,
Senior Engineer,
TS
"S.
Rea,
Senior Engineer,
TS
L. Rowell, Senior Engineer,
HPES
D. Shockley,
QA Auditor
'B. Slover, Project Engineer,
TS
L. Sullivan, Regulatory Compliance Specialist
W. Szuba,
Engineering Supervisor,
"D. Tibbitts, Supervisor,
Regulatory
Compliance
B. Tomlin, Senior Engineer,
TS
~M. Wallace, Specialist,
Regulatory
Compliance
~E.
Willet, Manager, Modifications (HPCS)
Other
licensee
employees
contacted
included
construction
craftsmen,
engineers,
technicians,
operators,
mechanics,
and office personnel.
NRC Resident
Inspectors
"George Maxwell, Senior Resident
Inspector
~Attended exit interview
Exit Interview
The inspection
scope
and findings were
summarized
on June
5,
1987, with
those
persons
indicated in paragraph
1 above.
The inspector
described
the
areas
inspected
and
discussed
in detail
the
inspection
findings.
No
dissenting
comments
were received
from the licensee.
Violation,
Failure
to
perform
adequate
safety
evaluations,
para-
graph 8.
The licensee
did not identify as proprietary
any of the materials
provided
to or reviewed
by the inspector during this inspection.
3.
Licensee
Action on Previous
Enforcement Matters
This subject
was not addressed
in the inspection.
4.
Unresolved
Items
Unresolved
items were not identified during this inspection.
5.
Licensee Action on Previously Identified Inspection
Findings (92701)
,a.
(Closed)
Inspector
Follow-up Item 400/86-53-08:
Surveillance
Program
Procedures
This
item identified
an
incomplete
surveillance
program
in that
not
all
procedures
required
to
perform
Technical
Specification
surveillance
requirements
had
completed
the
review
and
approval
process.
The
inspector
verified
those
specific
procedure
types
identified
in
the
initiating
report
were
presently
completed.
Additionally the
inspector
performed
a
sample
check
to verify
technical
specification
surveillances
were
scheduled
on
the
master
schedule
and that procedures
were approved to perform the tasks.
b.
(Closed)
Inspector
Follow-up Item 400/86-53-12:
Identification
and
Control of Commitment Related
Process
Instrumentation
This
item identified
an
incomplete
program for installed
process
instrumentation
used
for safety-related
or technical
specification
functions in that not all applicable
instrumentation
was identified
or entered
into
a calibration program.
The licensee
has developed
a
Required
Instrumentation
List (RIL) to identify instrumentation
required
to
meet
Final
Safety Analysis
Report
(FSAR) or technical
specification
requirements.
The list used
in conjunction with the
technical
specificati.on
Cross
Reference
List
(PGO-031)
provides
traceabi lity from technical
specification
survei llances
to specific
instruments
and the calibration procedures
for the instruments.
The
licensee
stated that the out - of - tolerance
instruments of the RIL
would be evaluated for previous
useage
per the individual instrument
cal,ibration procedures.
The inspector
reviewed the completed instrument
list and performed
random checks to verify process
instruments
were
included
as required.
Discrepancies
were not identified in this sample.
(Closed)
Inspector
Follow-up Item 400/86-33-06:
Onsite
Packaging of
Equipment
and Materials
This item identified the
need for the licensee
to direct attention to
packaging of spare parts
and material to prevent
damage
during trans-
ient from receipt
inspection
and
warehouse
storage.
The inspector
reviewed
the following procedures
to verify the programmatic guide-
lines for onsite packaging:
HNP-9.3.1,
Responsibilities
for
Packaging
Shipping
Receiving
Handling,
Storage
and
Maintenance
of Spare
Parts,
Material
and
Components
Mhile
Under
the
Control
of
Marehouse
Personnel,
Revision 0.
TMM-110, 'Receiving,
Packaging,
Storage
and Maintenance
Require-
ments for Spare
Parts Material
and Components,
Revision 0.
These
procedures
appeared
to supply adequate
guidance for protection
of
spare
parts
and material
onsite.
In addition,
the
inspector
'discussed
the potential
for damage
of parts
and
materials
with
warehouse
personnel.
Problems
were
not identified in this
area
and
i
appeared
that the guidelines
of the
above
procedures
were
adequately
implemented.
6.
Field Change
Requests
As
a result of the (}uality Assurance
preoperational
review of the licensee
Design Control
Program,
areas
were identified which required
a review to
a greater
depth,
especially with respect
to implementation.
These
areas
included Field
Change
Requests
(FCR)
and
Plant
Change
Requests
(PCR).
Field
Change
Requests
were
changes
to plant design
processed
during the
const, uction
phase utilizing guidelines
of the construction
gA program.
Following the establishment
of
a
system
as
"operable"
any
changes
were
required to
be
made via the
PCR process.
This process
required
addi-
tional
reviews
of the
specific
change
for maintenance,
operations
and
training impact.
During inspection
50-400/87-09
the inspector identified
a number of modifications being processed
via the
FCR process
although the
associated
systems
had been declared
and released
to operations.
This inspection,
in part,
reviewed this
aspect
of the
design
control
program with regards
to volume of FCRs
open
or processed
following issuance
of the
low power operating
license
and
the actions
of the licensee
to
evaluate
and closeout
remaining
FCRs.
The
FCR procedure
was cancelled
on
April 21,
1987,
which ended
the mechanism for initiating future
FCRs.
The
licensee
identified 829
FCRs which were
open or resolved following issuance
of the
low power operating
license
on October 24,
1986.
Of these,
606
were resolved prior to the specific system's
operational
date
and included
in the system
release
to operations.
These
FCRs appeared
to be appropri-
ately
processed.
Systems
under
construction,
i.e.,
waste
treatment
systems,
accounted for 25
FCRs which were properly addressed
as
FCRs.
The
remaining
196
FCRs received
a multi-discipline review by Technical
Support,
associated
discipline,
and
Environmental
and Radiological
Control
(E&RC)
to determine
impact
on plant systems,
procedures,
operations,
and training.
The result of this review was the identification of ten
FCRs with potential
impact
on
system
operations,
tests,
or training.
Of this ten
FCRs,
two
were identified
as safety-related.
The safety-related
FCRs
and
impact
were
as follows:
1)
FCR-I-1735
impacted
on training notes
and was
a document
change
only.
2)
FCR-I-3952
impacted operations
procedures
with respect to
a set
poin
change.
The following is
a list of the eight non-safety
related
FCRs
and their
impact:
FCR-I-3248,
Revision 2,
impacted
a
system description
which is due
for issuance
in August 1987.
FCR-SI-847,
Revision 2,
required
adding
computer points to scaling
documents
SCN 034 and
SCN 036.
FCR-HV-1728 and
FCR HV-1730 involved minor installation details which
impacted information in training notes.
FCR-I-3962
and FCR-I-400 impacted setpoints
and
a procedure revision.
FCR-I-3995
involved
an annunciator
window modification which changed
a procedure
reference.
FCR-l~i-2032
affected
the
chemical
feed
system
and
impacted
class
training notes.
Additionally, 101 of the
196
FCRs
open after
system turnover remain open;
36 of these
were partially implemented.
Those
FCRs not under
implementa-
tion will be deleted,
converted
to PCRs,
or receive
an equivalent review
and evaluation
process
similar to the
PCRs.
The remaining
FCRs will be
incorporated
into
an
implementation
schedule
by July 15,
1987.
The
following activities
by
the
licensee
demonstrate
positive
aggressive
action to resolve
the
FCR issue:
1)
Cancellation
of the
FCR procedure
to prevent further initiation
of FCRs.
-2)
Identification of the
scope of this issue
through review of FCRs
and associated
system
impact.
3)
Organization
and completion of multi-discipline reviews of each
open
FCR.
For the
sample
reviewed,
the licensee
appeared
to have achieved
adequate
control of the
FCR process
to provide
a timely and sufficient resolution
of potential
problems
and closeout of the
FCR program.
Per
CP8L (Harris
Nuclear .Project) letter
NRC-555 dated
May 1,
1987, (File
Number SHF/10-
10000),
the licensee
had committed to review the entire
FCR process.
7.
Plant
Change
Requests
(PCRs)
-- Implementation
The
inspector
reviewed
selected
to determine if adequate
design
controls
were
utilized to
ensure
appropriate
reviews
were
performed,
drawings
were
accurately
revised,
safety
evaluations
were
correct
and
thorough,
required
training
was
complete
and timely,
and modifications
were accurately installed.
The following PCRs were reviewed:
PCR 0
REVIEWED
TITLE
81
103
187
234
253
259
292
301
353
423
466
467
489
667
668
785
824
825
842
854
932
1026
1119
1145
1157
1190
1191
1286
1388
1515
1571
7.5
KVA Instrument
Power Supply Inverter
Demineralizer
Bypass
Around
CST and
R'MST
I/P Transducers
Indicator Scale
Changes
Appendix
R Power
Panel
Protection
(AFM) Venting Provisions
Design
Change - Turbine Driven AFM Pump Oil
7.5
KVA Inverter Ferro-Resonant
Transformer
Valves Not on Plant Drawings
RHR/SI System
Vent Valves
AFM Pump
Low-Low Suction Pressure
Switch
AFM Pump Suction
from CST
NRC Concern
ESM/AF
Containment
Spray Niniflow Orifice Replace-
ment with Throttle Valves
AFW Pump Vents
Service Air Leakage
Outside Diesel
Generator
Building
AFM Pump
Th. ust Bearing Coil Spring
Evaluation of
PCR 824
AFW Pump Bearing Walkdown
RMST Transmitter
Replacement
Essential
Chiller Recirculation
Seal
Piping
Thermolag Interference
Condensate
Storage
Tank
AFW Pump
Low Flow Trip Delay
Instrument
Loop F-113 Controller Card Update
AFW Check Valve Backleakage
Problem
AFW Check Valve Backleakage
Steam
Hammer Line number
Blowdown Valve-Temporary
Repair
The inspectors
found no evidence that
PCRs were not receiving appropriate
reviews or that single line electrical
and flow diagrams did not accurately
depict the as-built configuration of the plant. It was noted that drawing
details
are not always revised in a timely manner which could lead to work
being performed without updated
drawings;
however,
the inspectors
did not
identify any evidence
of this.
The
safety
evaluations
and
evaluations
included
in the
selected
PCR packages
were reviewed
by the inspectors.
It appeared
that
the justification for the conclusions
reached
in the evaluations
were not
always well documented.
This is addressed
in more detail
in paragraph
8
of this report.
The inspectors
reviewed the training provided for modifications installed
under
the
and
FCR programs.
The training of the onshift operators
appeared
to
be
adequate;
however,
there
appeared
to
be
an
excessive
amoun
of
time
required
to
include
modifications
.in
the
operator,
qualification
and requalification training.
Specifically, the inspectors
reviewed
the training
guide
and
system
description
for
the auxiliary
system;
neither
of
which
completely
addressed
the
recent
modifications to the system.
The inspectors
field verified
system modifications
and drawing accuracy
by extensive
walkdowns of selected
PCRs.
The following PCRs
were field
verified.
FIELD VERIFIED PCRs
153
Demineralizer
Bypass
Around
CST and
259
Venting Provisions
292
Design
Change
Turbine Driven AFW Pump Oil
423
RHR/SI System
Vent Valves
466
AFW Pump
Low-Low Suction Pressure
Switch
467
AFW Suction
From
489
tiRC Conce. n
ESW/AF
667
Containment
Spray MiniflowOrifice Replacement
668
AFW Pump Vents
785
Service Air Leakage Outside Diesel Generator Building
932
Essential
Chiller Recirculation
Seal
Piping
1145
AFW Check Valve Accessibility
1190
Pump
Low Flow Trip Delay
1286
AFW Check Valve Backleakage
Problem
1388
AFW Check Valve Backleakage
1571
Blowdown Valve Temporary Repair
There
was,
no evidence
of any discrepancies
between
the as-built config-
uration'nd
the modification.
PCR Package
Contents
The inspector
examined
the methodology,
interfaces,
and output associated
with work package
development for mechanical
PCRs.
After a design
package
has
been
developed
by
engineering
and
administratively
processed
by
Technical
Support, Harris -Plant Construction
Section
(HPCS) developed
work
packages
for implementation
of the modification.
The
packages
include
work instructions,
additional
drawings, guality Control
hold points,
and
material for the job.
The inspector
examined
the following new procedures
that had
been written
for package
development:
0'
PROCEDURE
MAP-1
TITLE
Harri s Pl ant
Modificati on
Unit of Conduct of Operations
REVISION
MAP-2
MAP-3
MAP-4
Preparation,
Approval,
and
Control of Modification Unit
Procedures
Training of Harris Modification
Unit Personnel
Process
Control
0
These
procedures
were issued
in May 1987
and were in the process of being
implemented.
Site
personnel
stated that these
documents
varied minimally
from previous construction
procedures.
These
procedures
reference
some
existing
pre-operational
procedures.
was
phasing
out
the older
referenced
procedures
and appeared
to have firm control of that evolution
appeared
to
interface
well with the
other
plant
groups.
personnel directly interfaced with trades
personnel
in work accomplishment
and,
thus,
were
spokesmen
to the other plant groups
on job status.
When
required,
routed
changes
to modifications
and to
HPES.
was
developing
a working relationship with the Technical
Support group.
The
inspector
reviewed
several
modification
work
packages
with
personnel.
With the
personnel
involved,
the
process
appeared
to
be
thorough.
With so few PCRs in process
and with the
new procedures,
was
taking their
time with the first few packages
in order
that the
mechanics
of the package
creation could be understood.
The
inspectors
examined
the
following
packages
for content
and
completeness:
NO.
TITLE
1134
1145
Flow Element
Flowing from
Duct Work Lining
AFW Check Valve Accessibility
310
Vendor Mobile Solidification
System
Hookup
These yet-to-be
closed
packages
appeared
to
be
complete
to the point of
the exceptions
noted in the packages.
Some of the Field Revisions in
1145 were difficult to follow, but all packages
had the essential
elements
required
by site
and regulatory documents.
The inspectors
extensively
reviewed
1286, Auxiliary Feedwater
(AFW)
system
modi> ication to prevent back-fill in auxiliary feed lines,
and
842,
pump thrust
bearing
coil
springs.
The.
remaining
paragraphs
discuss
these
PCRs.
1286 installed
three additional
check valves in the
AFW system motor
driven
pump train
(one
per line to each of the
steam
generators).
The
were to prevent
back
leakage
from the
steam
generators
and
main
feed lines..
The
two previously existing
in each line
(six total) did not prevent
the
back
leakage.
The primary check valves
(Pacific, Inc.) in each line which were adjacent
to the
steam
generators
that
were
to prevent
leakage
had
been
previously unsuccessfully
worked
(PCR
1145)'.
Each of three
new valves
(Anchor-Darling,
Co.)
were welded
into the
system
between
the two existing check valves in each line.
In
discussions
with site
personnel,
. the
following options
for
new
Anchor-Darling valves
had
been
considered:
replacement
of the Pacific
valves
nearest
the generator
with the new-valves,
using 'flanged
valves
instead
of welding
the
valves,
using
hangers
on
the
proposed
flanged
valves,
using
another
valve type,
using soft seated
valves,
leaving the
existing Pacific valves in place in case
soft seats
were eventually
used
(to prevent
thermal
deterioration
of the soft seat),
and installing
a
motor operated
valve in lieu of
a check valve.
Due to operational
time
limits, the welded. valve configuration
was chosen.
None of the above
two
paragraphs
of background
information was present
in the
PCR package.
The licensee
had contingency
plans
should
the
new Anchor-Darling valves
fail to prevent
back leakage.
As indicated
above, soft seats
for the
new
Anchor-Darling valves
and motor operated
valves were considered.
The site
had ordered
soft seat kits (a
new
PCR would
be required)
for the
newly
installed valves
but,
per the licensee,
they
had not ordered
hard disks
for the existing valves.
The
new valves
appeared
to
be preventing
back
leakage.
Aside from the
operability/functional tests for the system,
the
new valves
had
not,
been
challenged
with
system
Per
the
licensee,
operational
procedures
had
been
changed
to prevent the
usage of the
AFW system during
startup
which
would limit the
cycling
of
the
system
check
valves.
Further,
system
testing
(surveillance)
and
usage. will determine
whether or not the modification will be viable.
Due to the
awareness
of historical
operation
problems with check'valves
'nd
the likelihood that
the
new
Anchor-Darling
valves will probably
require cyclical
preventative
maintenance
(PM), the inspector
discussed
valve
PM with the licensee.
NRC Information Notices
such
as
86-01
and
86-09
had
addressed
problems
with check
valves
in feedwater
and
systems.
It has
been historically recognized
that
check
valves
leak,
internal
parts
separate
from the valve body,
and the valves
have active
fai lures (fail to open).
Per discussion with the Technical
Support
Group
AFW system engineer,
he was
unaware of any
PMs on the valves,
but directed
0
the inspector
to the Maintenance
Group.
The Maintenance
Manager
was aware
of
an
Ins itute
of
Nuclear
Power
Operations
Significant
Operating
Experience
Report
which Harris
Plant
Engineering
Section
(HPES)
was
reported
to
be addressing.
The maintenance
manager
said that
no
were
currently
being
performed
on
check
valves.
Per
HPES
personnel,
they were in the preliminary stages
of developing
background
information towards implementation of PMs.
and Section 6.5. 1.4. 1 of the Plant's Technical Specification
(TS) require
that
a
safety
evaluation
be written
should
a
change
or
modification to
a
safety
system
occur.
Both
documents
require
that
certain
questions
be
addressed
in preparing
the evaluation.
One of the
questions
is whether the change
or modification represents
an increase
in
probability
of
occurrence
or
the
consequences
of
an
accident
or
malfunction.
and
the
TS state
that
the
evaluation
shall
include
a written determination,
with bases.
Procedure" AP-011,
Safety
Reviews,
Revision
1,
implements
the
TS
and
requirements.
Paragraph
5.2.c,
of the
procedure
addresses
what
the
evaluator
shall
analyze
addressing
the
above
question.
The
paragraph
states
that
an
action which makes
even
a single failure to safety related
equipment
more
probable
must
be considered.
1286,
(AR( check
valves)
did contain
a safety evaluation
(Form 2,
pages
15 to 17).
Part 2, paragraph
7.3, of the evaluation
which restates
the probability increase
question
of AP-011
was
answered
"no"
and
the
bases
for this
answer
was
stated
to
be that
the modification to the
auxiliary feed
system will not affect the design
conditions of safety-
related
equipment.
Answers
to
other
questions
in evaluation
were
similarly terse.
310 and
489 had extensive
safety evaluations
which
more formally addressed
the design
envelope of the modification that they
performed.
Neither the
1286 evaluation
nor the
package itself
contained
any information or analysis
that di scussed
this extra internal
check valve parts (disk, disks pin,
and fasteners)
and/or
valve failure
potential
caused
by the valves'ddition to the
AFM system.
Aside from the
one line answer to paragraph
7.3, Part 2, of the safety evaluation,
there
was
no information from which to draw the conclusion that the three check
valves installation did not increase
the probability of system failure or
malfunction.
The above identified inadequate
safety evaluation is but one example.
825 contains
another
example of an
inadequate
evaluation,
the specifics
of which
are
detailed
below.
Both
examples
represent
a violation,
400/87-20-01,
Inadequacy
of Safety Evaluations.
There
were three
similar
generated
by the site
on the
AFM pumps.
They are
as follows:
0
10
ISSUED
DATE
NUMBER
FORM
1
INITIATION
SAFETY
EVALUATION DATE
PUMP AFFECTED/
COMMENTS
824
1-17-87
1-17-87
and
4-27-87
1A - SA/
Temporary
Modification
825
1-17-87
1-17-87
1B-SB and
Evaluation
842
1-20-87
2-3-87
All Three
Two modifications
(PCR
824
and
842)
were to
remove three thrust springs
from
each
of the three
AFN pumps
and
one modification
(PCR825)
was to
evaluate
not performing the spring removal unti 1
a later date.
The
pumps
were modified on dates
as follows; lA-SA on 1-17-87,
1Ã-SAB on 2-5-87,
and
on 3-15-87.
Per the licensee,
842
was to provide closure
of
work on all the
pumps
but maintenance
had yet to forward the
completed
work packages
to Technical
Support
Group (not in the
PCR package).
824
was
to
perform
a
temporary
modification
on
the
pump;
a
Nonconformance
Report
(87-012)
which was still open at the
time of the
inspection
indicated that the work had been
performed prior to issuance
of
the
PCR and work ticket.
The initiating impetus
to all
pump work was the fact that the
1A-SA pump
did
not
meet its
pump
curve
during operability testing.
There
were
several
contacts
made with the
pump vendor
( Ingersoll-Rand),
some of which
were not documented
in the
PCR packages.
PCR 825 references
a
memo from
the vendor
and
telephone
conversation
with. the
vendor
and documentation
for these
were not in the
PCR packages.
PCR 842 contained instructions to
remove 'the thrust springs
from the
pumps
and replace
them with a spacer.
825
which is
an
engineering
evaluation
with
a
safety
evaluation
included
provided justification for continued
operation
of
the
two
unmodified
pumps.
The engineering
evaluation
states
that the insufficient
head
problem (lA-SA pump)
was
analyzed
to
be attributable
primarily to
improper assembly
and/or
missing parts
and secondarily to abnormal
wear of
the balancing
drum.
The analysis
was not
a par t of the
PCR package
unless
it
was
the
referenced
vendor
memos
The
discovery
findings
at
the
disassembly
of the
1A-SA was not .available
in the three
PCR packages.
The safety
evaluation
( Form 2,
pages
15 to
17)
found in
PCR 825 did not
adequately
support continued
operation
of the
two unmodified
pumps.
The
Part 2, paragraph
7.3 question of the safety evaluation
as4ed
the question
as follows; Mill the probability of occurrence
of malfunction of equipment
important to safety
be increased?
0'
11
The utility answered
the question
as
no
and
the
bases
was that
AF'M pump
and
system reliability is not affected.
Although the two unmodified
pumps
were
not exhibiting
low head output
as the
pump
no explanation
as
to the potential
missing
or rubbing parts
in the
unmodified
pumps
was
given.
The removal
and replacement
of the
1A-SA springs
was thought to be
a reduction
in probabi li y of
a malfunction
(and
a repair
method).
As
with
1286, this aspect
of an inadequate
safety evaluation
represents
another
example of a violation of 10 CFR 50.59,
400/87-20-01.