ML17352A938
| ML17352A938 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 12/01/1994 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17352A937 | List: |
| References | |
| 50-250-94-23, 50-251-94-23, NUDOCS 9412130032 | |
| Download: ML17352A938 (2) | |
Text
NOTICE OF VIOLATION Florida Power and Light Company Turkey Point, Units 3 and 4
Docket Nos.
50-250, 50-251 License Nos.
DPR-31, DPR-41 During an NRC inspection conducted on October 30 through November 26,
- 1994, a
violation of NRC requirements was identified.
In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions,"
10 CFR Part 2, Appendix C, the violation is listed below:
Units 3 and 4 Technical Specification 6.8. 1 requires that written procedures be established, implemented, and maintained covering the activities referenced in Appendix A of Regulatory Guide 1.33, Revision 2, February
- 1978, which include surveillance test procedures.
Step 7.4.26 of Unit 4 surveillance test procedure 4-OSP-203. 1, Train A Engineered Safeguards Integrated Test, requires operators to place the control switches for the 3A and 3B high head safety injection pumps in STOP (spring return to AUTO).
Contrary to the above, at about 9:06 a.m.
on November 3, 1994, with Unit 3 in Mode 1 and Unit 4 in Mode 5, Unit 4 operators placed the 3A and 3B high head safety injection pump control switches in PULL-TO-STOP rather than STOP (spring return to AUTO).
This action caused the pumps to be unavailable for automatic starting on a Unit 3 safety injection signal for about 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 39 minutes.
During this time, automatic safety injection for Unit 3 was available from the 4A and 4B high head safety injection pumps.
This is a Severity Level IV violation (Supplement I).
Dated at Atlanta, Georgia thislst day of Dec.1gg4 Enclosure 9412130032 941201 PDR ADOCK 05000250 Q