ML17348B430

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Responds to Violations Noted in Insp Repts 50-250/91-52 & 50-251/91-52.Corrective Actions:Porv PCV-3-455C Closed & RCS Pressure Recovered & Night Order Issued Instructing Personnel to Conduct Preevolution Briefings
ML17348B430
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 03/19/1992
From: Goldberg J
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-92-67, NUDOCS 9203230238
Download: ML17348B430 (7)


Text

ACCELERATED DISTRIBUTION DEMONST$&TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM.(RIDS)

ACCESSION +BR:9203230238 DOC.DATE: 92/03/19 NOTARIZED: NO DOCKET FACII:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 50-251 Turkey Point Plant, Unit 4, Florida Power and Light C 05000251 UTH.NAME AUTHOR AFFILIATION LDBERG,J.H.

Florida Power

& Light Co.

RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Responds to violations noted in Insp Repts 50-250/91-52 50-251/91-52.Corrective actions:PORV PCV-3-455C closed RCS pressure recovered

& night order issued instructing personnel to conduct preevolution briefings.

DISTRIBUTION CODE: IE01D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: General (50 Dkt)-Insp Rept/Notice of Vio ation esponse NOTES:NRR RAGHAVAN,L NRR RAGHAVAN,L

/

05000250 05000251 A

RECIPIENT ID CODE/NAME PD2-2 PD INTERNAL: AEOD AEOD/DSP/TPAB NRR HARBUCK,C.

NRR/DLPQ/LHFBPT NRR/DOEA/OEAB NRR/DST/DIR SE2 NUDOCS-ABSTRACT OGC/HDS3 RGN2 FILE 01 EXTERNAL: EG&G/BRYCEiJ.H.

NSIC NOTES:

COPIES LTTR ENCL 1

1 1

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1 RECIPIENT ID CODE/NAME AULUCK,R AEOD/DEIIB DEDRO NRR MORISSEAU i D NRR/DLPQ/LPEB10 NRR/DREP/PEPB9H NRR/PMAS/ILRB12 OE DIR NRC PDR COPIES LTTR ENCL 1

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D NOTE TO ALL"RIDS" RECIPIENTS PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

A D

D TOTAL NUMBER OF COPIES REQUIRED:

LTTR 23 ENCL 23

P.O. 8 ox 14000, Juno Beach, FL 33408.0420 MAR 19 1992 L-92-67 10 'CFR2.201 U. S. Nuclear Regulatory Commission Attn:

Document Control Desk Washington, D. C.

20555 Re:

- Turkey Point Units 3 and 4

Docket Nos.

50-250 and 50-251 Reply to Notice of Violation NRC Ins ection Re ort 91-52 Florida Power and 'Light Company has reviewed the subject inspection report and pursuant to 10 CFR 2.201, the required response is attached.

If there are any questions please contact us.

Very truly yours, J.

H. Goldberg President Nuclear Division JHG/OIH/oh Attachment CC'tewart D. Ebneter, Regional Administrator, Region II, USNRC R.

C. Butcher, Senior Resident Inspector, USNRC, Turkey Point Nuclear Plant 9203230238

'F20319 PDR ADOCK 05000250 8

PDR

<go]

I )

Attachment to L-92-67 Page 1

ATTACHMENT REPLY TO A NOTICE OP VIOLATION RE:

Turkey Point Units 3 and 4

Docket Nos.

50-250 and 50-251 NRC Inspection Report 91-52

" FINDING:

"Technical Specification 6.8.1 requires that written procedures and administrative policies be established, implemented, and maintained in accordance with the

.requirements and recommendations of Appendix A of Regulatory Guide 1.33, Revision 2, dated February 1978.

Appendix A of Regulatory Guide 1.33, Revision 2, dated February

1978, recommends that written procedures be established for typical safety-related activities carried out during the operation of nuclear power plants.

Section 1.b of this Appendix recommends administrative procedures which include authorities and responsibilities for safe operation and shutdown.

Paragraph 5.6.16.1 of procedure O-ADM-200, Conduct of Operations, requires that evolution briefings be conducted=

for individuals involved in an evolution that is to be performed and that the detail of the briefing is dependent on the degree and complexity of the evolution and the number of individuals involved.

Contrary to the above, on January 14,

1992, an adequate evolution briefing was not conducted prior to the investigation of a possible malfunction of the pressurizer control group heaters with Unit 3 at 1004 power.

As a

result, power operated relief valve PCV-3-455C was, inadvertently cycled due to excessive demand on controller PC-3-444J.

This is a Severity Level IV violation (Supplement 1)."

Attachment to L-92-67 Page 2

RESPONSE

TO FINDING 1 ~

2 ~

FPL concurs with the finding.

Cause of the violation:

3 ~

The root cause was that a pre-evolution briefing was not conducted to ensure that personnel understood the.

control functions of PC-444J and precaution to be taken during manual pressure control.

The second contributor was. the lack of procedural guidance cautioning operators that increasing PC-444J demand signal will open PCV-3-455C.

Corrective actions which have been taken and the results achieved:

a 0 b.

PCV-3-455C was closed and Reactor Coolant System (RCS) pressure was recovered.

A night order was issued instructing personnel to conduct pre-evolution briefings.

~

c.

Disciplinary action was administered to the personnel involved.

Corrective actions which have been taken to avoid further violations include:

Procedures associated with pressurizer pressure control'ere reviewed.

This review identified required procedure changes to 3/4-OSP-041.23, cautioning personnel that PC-444J can open PORVs.

5..

Full compliance and completion of all corrective actions was achieved on January 17, 1992.

~,