ML17342A361
| ML17342A361 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 01/07/1986 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17342A360 | List: |
| References | |
| 50-250-85-42, NUDOCS 8601130182 | |
| Download: ML17342A361 (4) | |
Text
ENCLOSURE 1
NOTICE OF VIOLATION Florida Power and Light Company Turkey Point Unit 3 Docket No. 50-250 License No.
DPR-31 The following violation was identified during an inspection conducted on November 12 - December 9,
1985.
The Severity Level was assigned in accordance with the NRC Enforcement Policy (10 CFR Part 2, Appendix C).
Technical Specification (TS) 6.8. 1 requires that written procedures and administrative policies be established, implemented, and maintained that meet or exceed the requirements and recommendations of sections
- 5. 1 and 5.3 of ANSI N18.7-1972 and Appendix A of USNRC Regulatory Guide 1.33.
Appendix A of USNRC Regulatory Guide 1.33 recommends that written procedures be established covering operation of the nuclear instrument system and the feedwater system.
'a ~
Off-normal operating procedure
- 12108, Source Range Nuclear Instrumenta-tion Malfunction, dated August 22, 1984, requires (section 5.2. 1) that a failed instrument be taken out of service by placing the level trip switch in the bypass position.
Contrary to the
- above, on November 30,
- 1985, a Unit 3 source range nuclear instrument (N-32) was taken out of service without placing the level trip switch in the bypass position.
Subsequently, when the instrument was re-energized, an electrical surge generated an input signal spike which was not bypassed and exceeded the instrument's trip setpoint.
The trip signal from the instrument caused an actuation of the reactor protection system.
b.
Operating procedure 3-0P-074, Steam Generator Feedwater
- Pump, dated September 11, 1985, requires (section
- 5. 1. 1) that the condensate system be aligned for normal operation in accordance with procedure 3-0P-073, Condensate
- System, as an initial condition prior to starting a steam generator feedwater pump.
Contrary to the
- above, on December 4,
- 1985, the 3B steam generator feedwater pump was started and the initial condition of section
- 5. 1.1 of 3-OP-074 was not met.
The subsequent trip of the 3B steam generator feedwater pump due to the improper condensate system alignment resulted in an initiation of the auxiliary feedwater system.
This is a Severity Level IV violation (Supplement I).
I PDR 130182 8hoi07
<<011@
ADO'5000250 PDR
'l'I~ II 'Ir<<;I II
~
'I F s, I
f f ~ Iyf 1
s IF r I<<
1 sls
<<F v
, 1'
<<1 1
sf<<
I g
I',
1 31<<'1 ~
l 1 <<, <<
~
l
~ l s<<r' I
I
, I' I
I ~
~
1 I S<<
<<1$
~ ~
f<<ls' rI F
., A I
~ I
<<1 1 ~
~ f.
~
I <>I'>>>>1 M I
l IP>>
f ~
>>I ">> ~ )>>
Pff I\\
. <<l ~ 'l P
~
>>P I
r, I
)'I f
I,
>>1>>I
'pe.
- f
(>>
$ (>>P>>
III'ft
<<p f
n Ill
~ ~
I fp I
~
I I
I
<<>>P P P <<<<
<<n
~
L I,,X pn fl f
~
~- f',
II I'I 'I p>>
f 4,
g ~
E f