ML17334A661

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Insp Repts 50-315/97-25 & 50-316/97-25 on 971228-980131. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML17334A661
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 02/20/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17334A659 List:
References
50-315-97-25, 50-316-97-25, NUDOCS 9802260166
Download: ML17334A661 (32)


See also: IR 05000315/1997025

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No:

License No:

50-315, 50-316

DPR-58, DPR-74

Report No:

50-315/97025(DRP); 50-316/97025(DRP)

Licensee:

Indiana and Michigan Power

500 Circle Drive

Buchanan, Ml 49107-1395

Facility:

Donald C. Cook Nuclear Generating Plant

Location:

'1 Cook Place

Bridgman, Ml 49106

Dates:

December 28, 1997 through January 31, 1998

Inspectors:

B. L. Bartlett, Senior Resident Inspector

B. J. Fuller, Resident Inspector

E. R. Schweibinz, Project Engineer

Approved by:

Bruce L. Burgess, Chief

Reactor Projects Branch 6

9802260ihb

980220

PDR

ADOCK 050003i5

6

PDR

EXECUTIVE SUMMARY

D. C. Cook Units 1 and 2

NRC Inspection Report No. 50-315/97025(DRP); 50-316/97025(DRP)

This inspection included aspects of licensee operations, maintenance,

engineering, and plant

support.

The report covers a five-week period of resident inspection and includes the followup to

issues identified during previous inspection reports.

~Oerations

~

The inspectors concluded that cold weather preparations had been properly implemented.

The inspectors also concluded that it was prudent to procure a stand-by boiler in order to

ensure that safety-related equipment and other plant spaces were not adversely affected

by cold weather in the event the plant heating boiler was unable to operate

(Section 01.2).

Maintenance

The inspectors concluded that the work activities observed were performed in a quality

manner with procedures present and in use.

The high quality of the Instrumentation and

Control (l&C)technician work on the Solid State Protection System (SSPS) relay repairs

was especially noteworthy. An exception to this good performance was a personnel error

by an l&Ctechnician on another activity which resulted in an invalid reactor trip signal.

In

addition, the inspectors determined that the required report regarding the inadvertent trip

signal was not going to be made to the NRC until after the inspectors questioned the lack

of a report (Section M1.1).

o

The questionable material condition of the SSPS master relay dust covers resulted in

both trains of SSPS being declared inoperable for operability under seismic conditions.

A

violation was identified when the licensee failed to make a timely report to the NRC

concerning

an unanalyzed condition that significantly compromised plant safety.

An

Unresolved Item was opened to track the review of additional data to determine when

licensee personnel were aware of the degraded condition of the SSPS relays

(Section M2.1).

Encnineering

o

Performance testing of the containment hydrogen skimming system continued during this

inspection report period. Computer modeling and engineering assessments

were being

performed in an effort to determine the as-found operability and to ensure the system

would be returned to an operable condition. An unresolved item on the as-found

condition of the hydrogen skimming system remained open.

The inspectors concluded

that the Licensee Event Report (LER) issued contained inappropriate statements

(Section E1.1).

During a review of selected LERs, the inspectors identified one event that was improperly

retracted and another event that was not reported in a timely manner.

A third LER had an

insufficient basis for retraction until the licensee performed additional calculations in

response to inspector questions.

One violation for failure to submit a timely LER was

issued (Section E8.1).

Plant Su

ort

~

No discrepancies

were noted.

Re ort Details

Summa

of Plant Status

Unit 1 remained in Mode 5, Cold Shutdown, during this inspection period. The unplanned outage

was in response

to NRC and licensee concerns with the operability of the containment

recirculation sump and other engineering issues.

Unit 2 remained in Mode 5, Cold Shutdown, during this inspection period. The unplanned outage

was in response

to NRC and licensee concerns with the operability of the containment

recirculation sump and other engineering issues.

I. 0 erations

01

Conduct of Operations

01.1

General Comments

71707

Using the referenced inspection procedure, the inspectors conducted frequent reviews of

ongoing plant operations.

The inspectors observed licensed operators closely monitoring

the panels and maintaining appropriate awareness

of plant conditions, although both

units were in Mode 5 for an extended period. Specific events and noteworthy

observations are detailed in the sections below.

01.2

Cold Weather Pre

aration

Both Units

a.

Ins ection Sco

e 71714

The inspectors verified that the licensee had implemented the procedures necessary to

prepare the plant for cold weather.

The inspectors reviewed logs and Work

Procedure R0014700, "Plant Winterization," and conducted plant walkdowns.

b.

Observations and Findin s

With both units shutdown, the licensee had to rely on the single non-safety-related

plant

heating boiler (PHB) for facility heating.

Licensee personnel obtained a commercial oil-

fired steam boiler (referred to as the alternate heating boiler) as a backup source of heat

to ensure availability of steam for plant heating requirements.

The'alternate heating

boiler was maintained in hot standby, but isolated from the plant heating system, as a

ready source of heating steam for the facility.

. The alternate heating boiler was placed into service on January 15, 1998, and again on

January 30, 1998, when the PHB was removed from service to repair system leaks.

The

alternate heating boiler maintained the facility at an acceptable temperature.

The

inspectors performed walk downs of the turbine and auxiliary buildings during the period

when the alternate heating boiler was in service to verify the absence of cold weather

problems.

0

)I

During a walkdown of the auxiliary building, the inspectors identified an opening to the

refueling water storage tank yard in the Unit 2 exterior pipeway near the Nos.

1 and 4

feed regulating valves.

The opening appeared

to be for outage related services and

allowed a significant inflowof cold air, but it did not pose an immediate threat of cold

weather damage to any equipment.

The inspectors informed the operations shift

manager, and the opening was sealed.

c.

Conclusions

The inspectors concluded that cold weather preparations had been properly implemented.

The inspectors also concluded that it was prudent to procure a stand-by boiler to ensure

that safety-related equipment and other plant spaces were not adversely affected by cold

weather in the event the plant heating boiler was unable to operate.

02

Operational Status of Facilities and Equipment

02.1

En ineered Safet

Feature S stem Walkdowns

Both Units

In addition to routine plant inspections, the inspectors used Inspection Procedure 71707

to walkdown selected portions of the essential service water system.

No operability

concerns were identified.

II. Maintenance

M1

Conduct of Maintenance

M1.1

General Comments

Ins ection Sco

e 62707 and 61726

Portions of the following maintenance job orders, action requests,

and surveillance

activities were observed or reviewed by the inspectors:

I

~

C043418, Perform airflow tests on containment hydrogen skimmer system

2-HV-CEQ-1

C043419, Perform airflow tests on containment hydrogen skimmer system

2-HV-CEQ-2

C043563, Test and repair relays on Unit 1 Train A and 8 Solid State Protection

System (SSPS)

C043565, Test and repair relays on Unit 2 Train A and 8 SSPS

C043697, Inspect diverter valves in the Unit 1 West Essential Service Water

pump strainer

J,

    • 1 I&C Head Procedure (IHP).4030.Surveillance Test Procedure (STP).410,

Revision 5, Train "A" Reactor Protection System (RPS) and Engineered Safety

Features (ESF) Reactor Trip Breaker and SSPS Automatic Trip/Actuation Logic

Functional Test

Observations and Findin s

Overall, the inspectors noted that work was performed in a quality manner with the work

packages present and in active use.

The high quality of the l&C technician work on the

SSPS relay repairs was especially noteworthy. The technicians were noted to carefully

review the procedure steps and equipment before performing each step and to closely

observe each other to avoid errors.

Additional detail concerning this job evolution is

contained in Section M2.1.

During the performance of 4030.STP.410,

an l&C technician inadvertently missed a step

which resulted in a reactor trip signal.

Licensee personnel performed a followup

investigation and took appropriate corrective action.

The failure to follow a **procedure

step-by-step,

as required by plant procedures, was a violation of 10 CFR Part 50,

Appendix B, Criterion 5, "Instructions, Procedures,

and Drawings." This non-repetitive,

licensee-identified and corrected violation is being treated as a Non-Cited Violation

consistent with Section VII.B.1 of the NRC Enforcement Policy (50-316/97025-04).

On January 8, 1998, licensee personnel called the NRC operations center to report the

inadvertent reactor protection system trip signal (reference NRC Event 33505).

On

January 21, 1998, licensee personnel called the operations center to retract Event

No. 33505 based upon additional review of the event.

On February 2, 1998, the

inspectors informed the licensee that after an NRC review of the circumstances

surrounding the event that the event was required to be reported to the NRC. Licensee

personnel stated that an LER would be issued within the 30-day requirement of

10 CFR 50.73.

Conclusions

The inspectors concluded that the work activities observed were performed in a quality

manner with procedures present and in use.

The high quality of the l&C technician work

on the SSPS relay repairs was especially noteworthy.

An exception to this good

performance was a personnel error by an l&C technician on another activity which

resulted in an invalid reactor trip signal.

In addition, the inspectors determined that the

.required report regarding the inadvertent trip signal was not going to be made to the NRC

until after the inspectors questioned the lack of a report.

Maintenance and Material Condition of Facilities and Equipment

De raded Covers on Solid State Protection S stem Master Rela s

Both Units

Ins ection Sco

e 62707

On January 8, 1998, the licensee identified degraded covers on some master relays in

the SSPS.

The inspectors observed the licensee's investigation and short-term

corrective actions.

Licensee documents reviewed included:

~

    • 1 IHP.Special Procedure (SP).SSPSA,

Revision 0, "Unit 1 Train "A", SSPS

Master Relay Replacement"

o

Revision 0, "Unit 1 Train "B", SSPS Master Relay

Replacement"

~

Revision 0, "Unit 2 Train "A", SSPS Master Relay

Replacement"

~

CR 98-0069, Covers for SSPS master relays are damaged

~

Engineering Technical Direction Memo (ENTDM)98-011, "Wiring Direction for The

Replacement of SSPS Master Relays"

~

Letter from Westinghouse

to American Electric Power (AEP-88-248), dated

May 10, 1988, Evaluation of master relay cover removal

Observations and Findin s

The SSPS master relays were installed with dust covers to keep dirt and dust from

accumulating inside the relay.

During a routine surveillance of the SSPS on January 8,

1998, an l8C technician noted that some SSPS master relay dust cover ears were

damaged or broken off. Past practice during surveillance testing of this portion of the

SSPS involved removal of the relay dust covers to allow manual actuation of the relay

contacts.

Removal of the cover required that retaining ears on the base of the relay be

pried open to release the cover.

Repeated

prying of the ears resulted in some ears being

damaged or tom off.

Condition Report (CR) 98-0069 was written to document the degraded covers.

The

prompt operability determination in the CR stated that normal operation of the relays was

not affected.

The operability determination also stated that a seismic event would likely

dislodge the covers from the relay assembly.

The operability determination concluded

that due to the light weight of the covers, it was unlikely for a dislodged cover to

spuriously actuate relays in the vicinityor to prevent relays from actuating.

Based on the

prompt operability determination, the SSPS was initiallydeclared operable with the

damaged relay covers.

The licensee's

CR preliminary reportability review also

determined that the degradation of the covers was not reportable under 10 CFR 50.72.

On January 11, 1998, the licensee performed a pull test to determine the seismic

acceptability of the covers.

A total of 38 covers (15 of 48 in Unit 1, and 23 of 48 in Unit 2)

failed the pull test.

The inspectors questioned the operability status of the SSPS.

Management and l8C personnel had determined that the relays were inoperable;

however, the relays were not logged as inoperable in the operations department

equipment out-of-service logs.

After pull testing was completed, operations department personnel declared the SSPS

operable pending engineering review of the test data.

The inspectors determined that the

job order used to test the relay covers included appropriate acceptance

criteria and that

the operations department should have declared the relays which did not meet the

acceptance

criteria inoperable.

After the inspectors questioned operations management

about the pull test results, the licensee concluded that the prompt operability

determination of the original condition report was inadequate.

Both trains of SSPS in

each unit were subsequently declared inoperable.

Based on the results of the pull testing, on January 15, 1998, the licensee determined

that the degraded SSPS relay covers were an unanalyzed condition that significantly

compromised plant safety, and a four-hour non-emergency report was made to the NRC.

10 CFR 50.72(b)(2)(i) required, in part, that the licensee report within four hours any

event found while shutdown, that, had it been found while the reactor was in operation,

would have resulted in the nuclear power plant being in an unanalyzed condition that

significantly compromised plant safety.'ecause

the pull test job order contained

appropriate. acceptance

criteria, the inspectors determined that the delay from discovering

the condition, on January 11, 1998, to reporting the condition, on January 15, 1998,

constituted a violation of 10 CFR 50.72.

(50-315/97025-01(DRP);

50-316/97025-01(DR

P)).

Replacement of the unacceptable

covers began on January 19, 1998.

Extensive

planning and coordination between the engineering, maintenance

and operations

departments were evident.

The inspectors observed portions of the planning process

and replacement of selected relays.

The I&Ctechnicians were observed to be careful,

methodical, and thorough in the performance of the relay replacement and subsequent

testing.

Preliminary data identified by the licensee showed that the SSPS relays were known to be

degraded since at least May 10, 1988, and adequate corrective actions were not taken in

a timely manner.

In May 1988, the SSPS vendor recommended

that the dust covers be

replaced or epoxied in place to prevent plastic fragments from the cover from falling into

the relay or another relay below it. The recommendation also stated that ifthe cover

began backing offthe relay during a seismic event, chattering of the normally closed

contacts could be induced.

The licensee did not followthe recommendations

of the

vendor to replace or epoxy the covers although the seismic operability of the relays was

in doubt.

Licensee and NRC persohnel are continuing to identify and review

documentation related to this issue.

Pending the results of the additional review this will

remain an Unresolved Item (50-315/97025-03(DRP); 50-316/97025-03(DRP)).

c.

Conclusions

The questionable material condition of the SSPS master relay dust covers resulted in

both trains of SSPS being declared inoperable for operability under seismic conditions.

A

violation was identified when the licensee failed to make a timely report to the NRC

concerning an unanalyzed condition that significantly compromised plant safety.

An

Unresolved Item was opened to track the review of additional data to determine when

licensee personnel were aware of the degraded condition of the SSPS relays.

0

III. En ineerin

E1

Conduct of Engineering

E1.1

0 en

Unresolved Item 50-316/97024-03

DRP

Inadvertentl

Plu

ed H dro en

Skimmer Suction Line Unit 2

a.

Ins ection Sco

e 62707

On November 26, 1997, licensee maintenance personnel identified a blockage of the

Steam Generator (S/G) No. 3 enclosure Train B hydrogen skimmer suction piping.

Subsequently,

engineering personnel initiated an assessment

of the as-found operability

and began efforts to restore the system to an operable status.

Licensee procedures and

documentation reviewed included:

~

Job Order C0043514, Investigate and repair motor operated damper 1-VMO-101

cycling at 45 degrees

~

LER 50-316/97-009-00, Blockage of containment air recirculation inlet line

~

CR 98-0033, During containment hydrogen skimmer tests on Unit 1, flow rates

were found below the acceptance

criteria.

b.

Observations and Findin s

As part of the corrective action for a blocked hydrogen skimmer line (referred to as the

CEQ system) the licensee committed to perform flow testing of both trains in both Unit 1

and Unit 2. On January 4, 1998, the licensee tested the Unit 1 CEQ fans and identified

that flows from various compartments

in both trains were lower than required by the

Updated Final Safety Analysis Report (UFSAR). Subsequently,

licensee personnel

determined that the low flow on the No.

1 CEQ system was due to a mis-positioned

shutoff damper, 1-VMO-101.

Damper 1-VMO-101 was improperly re-installed during maintenance

such that instead of

going from full closed to full open on an actuation signal it was partially open at all times.

In addition to reducing flow through the skimmer line, the mis-positioned damper also

created an ice condenser bypass flow path.

Unresolved Item (50-316/97024-03(DRP)) was initiallyopened pending the results of'a

proposed surveillance test.

During this inspection period, the licensee determined that

flows through the safety system were less than stated in the UFSAR. However, the CEQ

flows were discussed twice in the UFSAR.

In Chapter 5, "Containment," higher, normal

values were listed and in Chapter 14, "Accident Analysis," lower values were listed. The

lower values reflected more realistic assumptions.

The values identified during the

surveillance test were between the two values listed in the UFSAR.

The licensee determined that while the flowwas degraded, constituting a potentially non-

conforming condition, a specific operability decision could yet be made without further

analysis.

The initial flow tests performed during pre-operational testing were performed

with the ice condenser empty of ice. This test condition eliminated any concerns with ice

melt during testing.

Additional flow tests and computer modeling were required because

with the ice condenser filled with ice, test conditions identical to the preoperational tests

could not be established.

c.

Conclusions

Performance testing of the containment hydrogen skimming system continued during this

inspection report period. Computer modeling and engineering assessments

were being

performed to determine the as-found operability and to ensure the system would be

returned to an operable condition. An unresolved item on the as-found condition of the

hydrogen skimming system remained open.

EB

Miscellaneous Engineering Issues

E8.1

Review of Selected LERs

Both Units

a.

Ins ection Sco

e 92700

The inspectors reviewed selected LERs to verify that the reports were timely, complete,

and appropriate.

The LERs reviewed were:

LER 50-316/97003, Revision 0, Revision 1, and Revision 2

LER 50-316/97004, Revision 0, and Revision

1

LER 50-315/97024, Revision 0

b.

Observations and Findin s

b.1.

0 en

LER 50-315/97024:

Material Discovered in Containment Degrades Containment

Recirculation Sump and Results in Condition Outside Design Basis

On September

11, 1997, with the unit shutdown, an NRC inspector identified a fibrous

material, known as Fiberfrax, in the Unit 2 lower containment, a condition that was

outside the design basis of the plant. Subsequent

inspections by the licensee confirmed

this finding and resulted in the identification of additional fibrous material.

On September

17, 1997, the licensee reported this finding to the NRC in accordance with 10 CFR 50.72(b)(2)(i).

However, the licensee did not send in the LER until October 17, 1997.

Licensee personnel submitted the LER 30 days after the date this issue was determined

to be reportable instead of within 30 days of the date of discovery.

10 CFR 50.73 (a)(1)

requires, in part, that the licensee shall submit a LER for any event of the type

described in this paragraph within 30 days after the discovery of the event.

10 CFR 50.73(a)(2)(ii)(B) describes,

in part, any event or condition that resulted in the

nuclear power plant being in a condition that was outside the design basis of the plant.

The failure to submit an LER to the NRC within 30 days of the date of discovery was a

violation of 10 CFR 50.73.

(50-315/97025-02(DRP); 50-316/97025-02(DRP)).

10

I

,]I

/I

l

0 en

LER 50-316/97003-03:

Performance of Dual Train Component Cooling Water

(CCW) Outage During Unit 2 1996 Refueling Outage Resulted in Condition Outside The

Plant's Design Basis

The licensee reported in Revisions 0, and

1 of the LER that during the Unit 2, 1996

refueling outage a dual train CCW train outage was planned and performed.

However,

certain sections of the UFSAR had not been properly considered and thus the plant had

possibly operated outside the design basis.

The licensee's failure to comply with the

UFSAR had been identified by NRC inspectors and documented in Inspection Report

No. 50-315/97201.

Subsequently

in Revision 2, the licensee retracted the LER based upon the

conclusion'hat

sufficient controls were in place to ensure the plant remained within the design basis.

The inspectors reviewed the licensee's basis for retracting the LER'and concluded that

the. basis was insufficient. The licensee had taken credit for the ability of maintenance

and operations department personnel to restore the CCW components within the spent

fuel pool (SFP) calculated time to boil upon a postulated loss of cooling.

The inspectors determined that taking credit for manual action lacked a sufficient

analyzed basis to support the conclusion that the CCW system could be restored in time

for the SFP to remain below the bulk temperature limit. The inspectors informed licensee

personnel of their conclusions and the licensee subsequently resubmitted

LER 50-316/97003, as Revision 3.

10 CFR 50.73(a)(2)(ii), required that the licensee report to the NRC conditions outside the

design basis.

The inspectors concluded that the licensee's withdrawal of the LER in

Revision 2 was not appropriate.

b.3.'losed

LER 50-316/97004-01:

Change to CCW Temperature Without Revision to

UFSAR

On August 26, 1997, with Unit 2 at 100 percent rated thermal power, the licensee

determined that the unit had operated outside its design basis during the Unit 2 1996

refueling outage.

It was determined that this event was reportable under

10 CFR 50.73(a)(2)(ii) as a condition outside the design basis.

During the refueling

outage the licensee had administratively lowered the maximum allowable CCW

temperature to 90'F. This had been done to support the thermal analysis of the SFP

during the Unit 2, 1996 refueling outage.

The UFSAR stated that the CCW system was

capable of safely handling the required safety loads at temperatures

up to 95'F.

Subsequently

in Revision 1, the licensee withdrew the LER based upon a determination

that the 90'F limit and associated

administrative controls had been reviewed as required

by 10 CFR 50.59, prior to the Unit 2 refueling outage, and that this condition did not

represent an Unreviewed Safety Question.

The inspectors reviewed the LER and determined that the design basis of the CCW

system included the capability of the CCW system to safely shutdown/maintain shutdown

the unit at a maximum initial temperature of 95'F. The licensee's analysis for the Unit 2

11

,'l

f(l

Ij

refueling outage showed that the CCW temperature was required to be maintained lower

than the UFSAR upper temperature limit in order for the SFP to be maintained within the

design basis.

This issue was reported in Inspection Report No. 50-315/97021; 50-316/97201 as

Unresolved Item 50-315/97201-23; 50-316/97201-23.

The NRC Architect Engineering

inspection team was concerned that the licensee's

10 CFR 50.59 evaluation failed to

properly recognize the safety consequence

that the CCW system could not perform its

design function to remove the required SFP heat load at its maximum operating system

temperature of 95'F, as stated in the UFSAR. Thus, the licensee was operating

outside the design basis of the CCW system and the issue was reportable under

10 CFR 50.73(a)(2)(ii) as a condition outside the design basis.

Following discussions with NRC inspectors on the 90'F limit versus the 95"F design

basis, the licensee reanalyzed the Unit 2 with more realistic assumptions.

The new

analysis demonstrated

that the SFP would be maintained within the design basis at a

CCW temperature of 95'F.

The inspectors concluded that the licensee's retraction of LER 50-316/97004 was

appropriate; however, the supporting evidence was insufficient until NRC inspectors

questioned the basis for the retraction.

The issues identified during the review of the LER

regarding the licensee's

10 CFR 50.59 evaluation of the CCW system will be tracked

under Unresolved Item 50-315/97201-23; 50-316/97201-23; therefore, this LER is closed.

c.

Conclusions

During a review of selected LERs the inspectors identified one event that was improperly

retracted and another event that was not reported in a timely manner.

A third LER had an

insufficient basis for retraction until the licensee performed additional calculations in

response

to inspector questions.

One violation for an untimely report was issued.

E8.2

Closed

LER 50-316/97009:

Blockage of containment air recirculation inlet line results in

a condition outside the design bases.

This issue is discussed

in Inspection Report

No. 50-315/97024; 50-316/97024 and above in Section E1.1 as Unresolved

Item 50-316/97024-03(DRP).

The LER did not present any new information, nor did it

include any additional licensee commitments; therefore, this LER is closed.

However, the

inspectors identified several portions of the LER which were not fullyjustified and

appeared

to be contrary to the design bases.

~

As part of the assessment

of the safety significance, the LER stated, "An

evaluation of the impact of the blockage has concluded that there would have

been adequate flow through the steam generator (S/G) enclosure to preclude

excessive accumulation of hydrogen." To support this assessment

of the safety

significance, the LER included a statement thai hydrogen would not be generated

inside the S/G compartments

and that the hydrogen generated

in the lower

compartment would be well mixed, thus having little potential for significant

amounts of hydrogen to accumulate

in the S/G compartment.

The LER also

stated that the opposite train of the hydrogen skimmer system was available

except for short periods of maintenance

and would have been capable of

providing the required flow.

12

t 'I

0

The design basis of the hydrogen skimming system as stated in the UFSAR assumed

that hydrogen would be generated

inside the S/G compartments.

Licensee personnel

informed the inspectors that the assumptions contained in the UFSAR were overly

conservative.

By using more realistic assumptions

and engineering judgement, the

licensee's engineering staff determined that lower flows through the skimmer system

would be adequate.

The inspectors considered that using different assumptions than those contained within

the UFSAR was inappropriate for evaluating the safety significance of the lower hydrogen

skimmer flow. The LER did not clearly identify that this evaluation was based on

engineering judgement and the use of assumptions different from those contained in the

design basis.

Also, the planned flow testing of the two hydrogen skimmer trains had not

been completed when the LER was issued.

Thus, the capability of either train to meet

the required flow had not been verified. These comments were provided to the

appropriate licensee staff for consideration and corrective actions, as necessary.

IV. Plant Su

ort

R1

Radiological Protection and Chemistry Controls (71750)

During the resident inspection activities, routine observations were conducted in the

areas of radiological protection and chemistry controls using Inspection Procedure 71750.

No discrepancies were noted.

S1

Conduct of Security and Safeguards Activities (71750)

During normal resident inspection activities, routine observations were conducted in the

areas of security and safeguards

activities using Inspection Procedure 71750.

No

discrepancies

were noted.

F1

Control of Fire Protection Activities (71750)

During normal resident inspection activities, routine observations were conducted in the

area of fire protection activities using Inspection Procedure 71750.

No discrepancies

were noted.

X1

Exit Meeting

The inspectors presented the inspection results to members of the licensee management

at the conclusion of the inspection on February 2, 1998.

The licensee had additional

comments on some of the findings presented.

No proprietary information was identified

by the licensee.

13

0

lI

PARTIALLIST OF PERSONS CONTACTED

Licensee

¹K. Baker, Manager, Production Engineering

¹T. Beilman, Scheduling Superintendent

¹A. Blind, Vice-President Engineering

¹J. Boesch, Maintenance Superintendent

¹D. Cooper, Plant Manager

¹S. Delong, Management Information

¹MB. Depuydt, Nuclear Licensing

¹S. Farlow, Supervisor l8C Engineering

¹M. Finissi, Supervisor, Electrical Systems

¹R. Gillespie, Operations Superintendent

¹D. Hafer, Manager, Plant Engineering

¹D. Landot, Plant Performance

¹D. Morey, Chemistry Superintendent

¹D. Noble, Radiation Protection Superintendent

¹R. Ptacek, Nuclear Licensing

¹F. Pisarsky, Supervisor, Mechanical Component Engineering

¹T. Postlewait, Manager, Design Engineering

¹P. Russell, Supervisor, Plant Protection

¹J. Sampson,

Site Vice-President

¹P. Schoepf, Supervisor, Safety-related Mechanical Systems

¹R. Stevens, Nuclear Licensing

¹J. Tyler, Manager, Plant Protection and Emergency Preparedness

¹L. VanGinhoven, Materials Management

¹A. Verteramo, Supervisor Reactor Engineering

¹S. Wolf, Performance Assurance

USNRC

¹B. Burgess, Branch Chief, Region lil

¹Denotes those present at the February 2, 1998, exit meeting.

14

IP 37551

IP 61726

IP 62707

IP 71707

IP 71750

IP 92700

INSPECTION PROCEDURES USED

On-site Engineering

Surveillance Observations

Maintenance Observation

Plant Operations

Plant Support Activities

Onsite Review of LERs

ITEMS OPENED

50-315/97025-01

50-316/97025-01

50-315/97025-02

50-316/97025-02

50-315/97025-03

50-316/97025-03

50-316/97025-04

ITEMS OPENED, CLOSED, AND DISCUSSED

VIO

Failure to report an event outside the design basis in a

timely manner in accordance with 10 CFR 50.72

VIO

Failure to report an event outside the design basis in a

timely manner in accordance with 10 CFR 50.73

URI

SSPS Relay Operability History

NCV

Failure to follow procedures

ITEMS CLOSED

50-316/97004-01

50-316/97009-00

50-315/97025-03

LER

Change to CCW temperature without revision to UFSAR

LER

Blockage of containment air recirculation inlet line results in

a condition outside the design bases

NCV

Failure to follow procedures

ITEMS UPDATED

50-316/97024-03

URI

Inadvertently Plugged Hydrogen Skimmer Suction Line

15

,I

l

l

('i

LIST OF ACRONYMS

AEP

bcc

CC

CCW

CFR

CR

DCC

DRP

DPR)

EDT

ENTDM

ESF

ESW

IS,C

IHP

IR

JO

LER

LOCA

Ml

NCV

NOV

NRC

NRR

PHB

PDR

RPS

SCFM

SE

SFP

SM

SP

SRO

SSPS

STP

S/G

UFSAR

URI

American Electric Power

blind carbon copy

carbon copy

Component Cooling Water

Code of Federal Regulations

Condition Report

Donald C. Cook

Division of Reactor Projects

Demonstration Power Reactor

Eastern Daylight Time

Engineering Technical Direction

Engineered Safety Feature

Essential Service Water

Instrumentation and Control

l8C Head Procedure

Inspection Report

Job Order

Licensee Event Report

Loss of Coolant Accident

Michigan

Non-Cited Violation

Notice of Violation

Nuclear Regulatory Commission

Nuclear Reactor Regulator

Plant Heating Boiler

Public Document Room

Reactor Protection System

Standard Cubic Feet per Minute

Safety Evaluation

Spent Fuel Pool

Shift Manager

Special Procedure

Senior Reactor Operator

Solid State Protection System

~

Surveillance Test Procedure

Steam Generator

Updated Final Safety Analysis R

Unresolved Item

Memo

eport

16

I>,

W