ML17332A615
| ML17332A615 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 02/28/1995 |
| From: | Blind A, Janisse J, Russo M INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9503140243 | |
| Download: ML17332A615 (6) | |
Text
PR.j!:C)RI EY' (ACCELERATED RIDS PROCESSING REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9503140243 DOC.DATE: 95/02/28 NOTARIZED-NO DOCKET N
FACIL:50-316 Donald C.
Cook Nuclear Power Plant, Unit 2, Indiana M
05000316 AUTH.NAME AUTHOR AFFILIATION JANISSE,J.D.
(formerly Indiana
& Michigan Ele RUSSO,M.E.
(formerly Indiana
& Michigan Ele BLIND,A.A.
(formerly Indiana
& Michigan Ele RECIP.NAME RECIPIENT AFFILIATION R
SUBJECT:
Monthly operating rept for Feb 1995 for DC Cook Nuclear Plant Unit 2.W/950302 ltr.
DISTRIBUTION CODE:
IE24D COPIES RECEIVED:LTR L ENCL J SIZE: 5 TITLE: Monthly Operating Report (per Tech Specs)
NOTES:
0 RECIPIENT ID CODE/NAME PD3-1 PD INTERNAL: AEOD/SPD/RRAB NRR/DISP/PIPB RGN3 EXTERNAL LITCO BRYCE 1 J H
NRC PDR COPIES LTTR ENCL 1
1 1
1 1
1 1
1 1
1 1
1 RECIPIENT ID CODE/NAME HICKMAN,J NRR/DOPS/OECB NOAC COPIES LTTR ENCL 1
1 1
1 1
1 1
1 D
C U
E NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE iVASTE!CONTACTTHE DOCUMENTCONTROL DESK, ROOM PI-37 (EXT. 504-2083 ) TO ELliiIINATEYOUR NAME FROlil DISTRIBUTIONLISTS I'OR DOCUMENTS YOU DON"I'LED!
TOTAL NUMBER OF COPIES REQUIRED:
LTTR 10 ENCL 10
indiana h1ichigan Power Company Cook Nuclear Plant One Cook Place Bridgman, Ml 49106 61 6'465 5901 March 2, 1995 U.S. Nuclear Regulatory Commission ATTN:
Document Control Desk Washington, D.C.
20555 Gentlemen:
Pursuant to the requirements of Donald C.
Cook Nuclear Plant Unit, 2 Technical Specification 6.9.1.10, the attached Monthly Operating Report for the month of February 1995 is submitted.
Respectfully, A.Q
,A.A. Blind Plant Manager Attachment c'RC Region III D.R.
Hahn R.C. Callen S.
Hamming J.G. Keppler INPO Records Center ANI Nuclear Engineering Department E.E. Fitzpatrick W.G. Smith, Jr.
S.J.
Brewer D.W. Paul S.H. Steinhart J.L. Leichner J.A.
Isom D.G. Turner E.A. Smarrella J.C. Krieger M.E. Russo 9503140243 950228 PDR ADOCK, 05000316 R
N.R.C.
OPERATING DATA REPORT DOCKET NO.
50-316 DATE 01/Mar/95 COMPLETED BY JD JANISSE TELEPHONE 616-465-5901 OPERATING STATUS
- 1. Unit Name D.
C.
Cook Unit 2
- 2. Reporting Period FEB 1995 notes 3. Licensed Thermal Power (MWt) 3411 4.
Name Plate Rating (Gross MWe) 1133
- 5. Design Electrical Rating (Net MWe) '090 6.
Maximum Dependable Capacity (GROSS MWe) 1100 7.
Maximum Deaendable Ca acit Net MWe 10 py()60
- 8. If Changes Occur in Capacity Ratings (Items no.
3 through
- 7) Since Last Report Give Reasons, 9.
Power Level To Which Restricted. If Any (Net MWe) 10.
Reasons For Restrictions. If Any:
11.
12.
13.
14.
15.
16.
17.
18.
'9.
20.
21.
22
'3.
24.
Hours in Reporting Period No. of Hrs. Reactor Was Critical Reactor Reserve Shutdown Hours Hours Generator on Line Unit Reserve Shutdown Hours Gross Therm. Energy Gen.
(MWH)
Gross Elect.
Energy Gen.
(MWH)
Net Elect. Energy Gen.
(MWH)
Unit Service Factor
'nit Availability Factor Unit Capacity Factor (MDC Net)
Unit Capacity Factor (DER Net)
Unit Forced Outage Rate Shutdowns Scheduled over Next Six None This Mo.
Yr. to Date 672.0 1416.0 544.8 1288.8 0.0 0.0 544.8 1288.8 0.0 0.0 1849586 4382999 610430 1443940 590722 1397855 81.1 91.0 81.1 91.0 82.9 93.1 80.6 90.6 18.9 9.0 Months (Type, Date,and Cumm.
150432.0 101305.3 0.0
=97823.9 0.0 298481180 96750930 93155290 66.1 66.1 59.2 57.7 15.7 Duration):
25.'f Shut Down At End of Report Period, Estimated Date of Startup:
March 1
1995
- 26. Unitsin Test Status (Prior to Commercial Operation):
Forecast Achieved INITIALCRITICALITY INITIALELECTRICITY COMMERCIAL OPERATION
AVERAGE DAILY POWER LEVEL (MWe-Net)
MONTH DOCKET NO.
50-316 UNIT TWO DATE Ol/Mar/95 COMPLETED BY JD JANISSE TELEPHONE 616-465-5901 FEB 1995 DAY 95/02/01 95/02/02 95/02/03 95/02/04 95/02/05 95/02/06 95/02/07 95/02/08 95/02/09 95/02/10 95/02/11 95/02/12 95/02/13 95/02/14 95/02/15 95/02/16 AVERAGE DAILY POWER LEVEL 1082 1085 1077 1083 1087 1088 1087 1088 1085 1079 1090 1082 1088 1087 1084 1083 DAY 95/02/17 95/02/18 95/02/19 95/02/20 95/02/21 95/02/22 95/02/23 95/02/24 95/02/25 95/02/26 95/02/27 95/02/28 AVERAGE DAILY POWER LEVEL 1085 1084 1085 1075 1086 1088 756 0
0 0
0 0
UNIT SHUTDOWNS AND POWER REDUCTIONS REPORT MONTH:
FEBRUARY 1995 UNIT NAME:
DATE:
COMPLETED BY:
TELEPHONE:
PAGE D.C.
COOK UNIT 2.
March 2, 1995 M.E. Russo 616-465-5901 Page 1 OF. 1 DURATION NO.
DATE TYPE HOURS METHOD OF SHUTTING LICENSEE DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION REASON REACTOR REPORT NO.
CODE CODE TO PREVENT RECURRENCE 241 950223 F
127.2 95-002 FC At 1645 hours0.019 days <br />0.457 hours <br />0.00272 weeks <br />6.259225e-4 months <br /> EST Unit 2 receive a reactor protection actuation from a steam flow/feed flow
- mismatch, coincident with low steam generator level in the ¹4 Steam 'Generator.
A controller failure caused the feedwater regulating valve to the ¹4 Steam Generator to close resulting in the trip.
1 F:
Forced S:
Scheduled 2
Reason:
A:
Equipment Failure (Explain)
B:
Maintenance or Test C:
Refueling D:
Regulatory Restriction E:
Operator Training and License Examination F:
Administrative G:
Operational Error (Explain)
H:
Other (Explain) 3 Method:
1:
Manual 2:
Manual Sczam 3:
Other (Explain) 4Exhibit G Instructions for preparation of data entry sheets for Licensee Event Report (LER) File (NUREG 0161) 5Exhibit I:
Same Source
DOCKET 0'NIT NAME:
COMPLETED BY:
TELEPHONE'ATE:
PAGE:
50-316 D.C.
Cook Unit 2 M.E. Russo 616-465-5901 March 2, 1995 Page 1 of 1
MONTHLY OPERATING ACTIVITIES FEBRUARY 1995 HIGHLIGHTS The unit entered the reporting period in Mode 1 at 100%
RTP.
An automatic Reactor trip occurred on February 23, 1995 at 1645 due to a faile'd closed main feedwater regulating valve.
The unit was maintained in Mode 3 for minor repairs.
The unit exited this reporting period in Mode 3.
There were no challenges to the pressurizer safety valves or power operated relief valves.
Gross electrical generation for the month of February was 610430 MWH.
DETAILS 02-23-95 1645 Reactor trip.
A failed closed main feedwater regulating valve resulted in an automatic reactor trip.
RCS in Mode 3.