ML17331B089

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Forwards Insp Repts 50-315/93-12 & 50-316/93-12 on 930817-0928 & Notice of Violation.Expresses Concern About Numerous Deficiencies Identified W/Feedwater Control Sys Temporary Mod 2-93-015
ML17331B089
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 11/24/1993
From: Grant G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Fitzpatrick E
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
Shared Package
ML17331B090 List:
References
NUDOCS 9312070130
Download: ML17331B089 (6)


See also: IR 05000315/1993012

Text

FORD 1

REGULATORY INFORMATION DISTRIBUTION SYSTEM (BIDS)

I

,". ACCESSION 'BR: 9312070130

DOC. DATE: 93/1 1 /24

NOTARIZED:

NO

DOCKET

ACIL: 50..315 Donald

C.

Cook Nuclear

Power

Plant'nit ii Indiana

M

05000315

50-316 Donald

C.

Cook Nuclear

PoUJer Pianti Unit 2i Indiana

M

05000316

AUTH. NAME

AUTHOR AFFILIATION

GRANTe G. E.

Region

3 (Post

820201)

RECIP. NAME

RECIPIENT AFFILIATION

FITZPATRICK'.

Indiana Michigan Poeer

Co.

(formerly Indiana

& Michigan Ele 'R

SUB JECT:

Forwards

insp repts

50-315/93-12

& 50-316/93-12

on

930817-0928

& notice of violation. Expresses

concern

about

I

numerous

def ic ienc'ies identified m/feedeater

control sos

temporary

mod 2-93-015.

'0

DISTRIBUTION CODE:

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COPIES

RECEIVED: LTR

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SIZE:

TITLE: General

(50 Dkt)-Insp Rept/Notice of Violation Response

NOTES:

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PD3-1

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EXTERNAL: EG&G/BRYCEi J. H.

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NRC

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NOTE TO ALL RIDS" RECIPIEYTS:

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UNITEO STATES

NUCLEAR REGULATORY COMMISSION

REGION III

799 ROOSEVELT ROAD

GLEN ELLYN, ILUNOIS60137-5927

NOV 24 I993

Docket No. 50-315

Docket No. 50-316

Indiana Michigan Power

Company

ATTN:

Hr.

E.

E. Fitzpatrick

Vice President

1 Riverside

Plaza

Columbus,

OH

43216

Dear Hr. Fitzpatrick:

This refers to the system

based

instrumentation

and control inspection

(SBICI)

conducted

by Hr. Z. Falevits

and others of this office on August

17 through

September

28,

1993.

The inspection

included

a review of activities authorized

for your D.

C.

Cook Nuclear

Power Plant, Units

1 and 2.

This inspection

focused

on the design

and configuration of selected

instrumentation

and

control

systems

and components.

We discussed

our inspection findings with

Hr. Blind and others of your staff at the conclusion of the inspection

on

September

28,

1993.

Areas examined during the inspection

are identified in the report.

The team

assessed

the design,

implementation,

and engineering/technical

support

relative to s'elected

instrumentation

and control

( I&C) systems.

The

inspectors

selectively reviewed the setpoint

program,

design calculations,

relevant procedures,

representative

records,

installed equipment,

and

interviewed engineering

and technical

support staff.

The team concluded

the design

and operation of the

I&C systems

examined

were

generally acceptable.

During the, inspection strengths

were identified in the

engineering staff experience

level, the guidance

provided

by Instrument

Loop

Setpoint Hethodology Guide,

and the measuring

and test

equipment

program.

However, in addition to the issues

identified in the attached

Notice of

Violation, weaknesses

were identified in ILC training for corporate

engineers

and

I&C component training for plant engineers.

We are particularly concerned

about the numerous deficiencies

we identified

with your feedwater control

system temporary modification 2-93-015.

For

example,

the engineer

inappropriately referenced

an unrelated

system's

drawing

to identify the I/I converter terminations rather

than referring to the

specific I/I converter's

vendor manual.

In another

case,

by failing to

consult the vendor manual,

the engineer

neglected

to include

a required

resistor in the I/I circuit.

Your independent

modification review failed to

identify the errors.

This particular I/I converter failed in service

and

caused

a reactor trip.

The errors

and omissions identified with this

temporary modification are unacceptable

in

a modification program developed

to

assure

the facility's safe operation.

Because

of this issue's

significance

and generic implications,

you are requested

to address

the issue

in addition

to your response

to the attached

Notice of Violation.

9312070130

931124

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Indiana Michigan Power

Company

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During this inspection,

certain of your activities were in violation of NRC

requirements,

as specified in the enclosed

Notice.

The first violation is of

concern

because

omissions,

errors

and discrepancies

in setpoint calculations

and design

drawings could affect equipment operability or safe

shutdown.

The

concern with the second violation is the safety

impact of engineers

taking

an

overly restrictive interpretation of the Updated Final Safety Analysis Report

in determining whether

a safety evaluation is necessary.

You are required to respond to this letter and should follow the instructions

specified in the enclosed

Notice when preparing your response.

In your

response,

you should document the specific actions

taken

and

any additional

actions you plan to prevent recurrence.

After reviewing your response

to this

Notice, including .your proposed corrective actions

and the results of future

inspections,

the

NRC will determine whether further

NRC enforcement

action is

necessary

to ensure

compliance with NRC regulatory requirements.

We also

request that you respond

in writing to all open

and unresolved

items noted in

this report.

We understand

that you are evaluating your organization's ability to provide

timely information during

NRC inspections.

We are interested

in your findings

because

of the issues direct effect on inspection efficiency and

effectiveness.

We therefore request that when your evaluation is complete

that

we meet to discuss

your conclusions.

In accordance

with 10 CFR 2.790 of the Commission's

regulations,

a copy of

this letter, its enclosures,

and your response

to this letter will be placed

in the

NRC Publ'ic Document

Room.

The responses

directed

by this letter

and the accompanying

Notice are not

subject to the clearance

procedures

of the Office of Management

and Budget

as

required

by the

Paperwork Reduction Act of 1980,

PL 96-511.

We will gladly discu'ss

any questions

you have concerning this inspection.

Sincerely,

Enclosures:

1,

Notice of Violation

2.

Inspection

Reports

No. 50-315/93012(DRS);

No.

50-316/93012(DRS)

Appendix

A Personnel

Contacted

See Attached Distribution

LQM~U.

Geoffrey E.

Gr

, Director

Division of Reactor

Safety

Indiana Michigan Power

Company

Distribution

cc w/enclosures:

A. A. Blind, Plant Manager

OC/LFDCB

Resident

Inspector, RIII

James

R. Padgett,

Michigan

Public Service

Commission

'IS

Coordinator,

USEPA,

Region

V Office

Michigan Department of

Public Health

D. C.

Cook

LPM,

NRR

D. Norkin,

NRR