05000315/LER-1981-001-03, /03L-0:on 810112,boron Concentration in Boron Injection Tank & North Boric Acid Storage Tank Found Diluted Below Tech Spec Level.Cause Unknown.Boron Concentration Increased

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/03L-0:on 810112,boron Concentration in Boron Injection Tank & North Boric Acid Storage Tank Found Diluted Below Tech Spec Level.Cause Unknown.Boron Concentration Increased
ML17331A640
Person / Time
Site: Cook 
Issue date: 02/13/1981
From: Keith R
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17326A843 List:
References
LER-81-001-03L-01, LER-81-1-3L-1, NUDOCS 8102190585
Download: ML17331A640 (2)


LER-1981-001, /03L-0:on 810112,boron Concentration in Boron Injection Tank & North Boric Acid Storage Tank Found Diluted Below Tech Spec Level.Cause Unknown.Boron Concentration Increased
Event date:
Report date:
3151981001R03 - NRC Website

text

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