05000315/LER-1980-023-03, /03L-0:on 800916,steam Generator 2 Channel 3 Level Indication Was Found to Be Indicating 6% Lower than Other Channels.Caused by Pinhole Leak in Impulse Line at Socket Weld.Repaired & Returned to Svc

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/03L-0:on 800916,steam Generator 2 Channel 3 Level Indication Was Found to Be Indicating 6% Lower than Other Channels.Caused by Pinhole Leak in Impulse Line at Socket Weld.Repaired & Returned to Svc
ML17331A473
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 10/03/1980
From: Delong S
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17331A471 List:
References
LER-80-023-03L-01, LER-80-23-3L-1, NUDOCS 8010090371
Download: ML17331A473 (2)


LER-1980-023, /03L-0:on 800916,steam Generator 2 Channel 3 Level Indication Was Found to Be Indicating 6% Lower than Other Channels.Caused by Pinhole Leak in Impulse Line at Socket Weld.Repaired & Returned to Svc
Event date:
Report date:
3151980023R03 - NRC Website

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~02 DURING NORMAL OPERATION THE STEAM GENERATOR 2 CHANNEL 3 LEVEL INDICATION WAS FOUND BE INDICATING 6 PERCENT LOWER THAN THE ASSOCIATED CHANNELS FOR THAT GENERATOR.

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