ML17328A914
| ML17328A914 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 02/28/1991 |
| From: | Blind A, Janisse J INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9103180245 | |
| Download: ML17328A914 (9) | |
Text
ACCELERATED DI, TRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9103180245 DOC.DATE: 91/02/28 NOTARIZED:
NO DOCKET' FACIL:50-316 Donald C.
Cook Nuclear Power Plant, Unit 2, Indiana 05000316 AUTH.NAME AUTHOR AFFXLXATION JANISSE,J.D.
Xndiana Michigan Power Co.
(formerly Xndiana
& Michigan Ele BLIND,A.A.
(formerly Xndiana
& Michigan Ele RECIP.NAME RECIPIENT AFFILIATION R
SUBJECT:
Monthly operating rept for Feb 1991 for DC Cook Unit 2.N/
910305 ltr.
DISTRIBUTION CODE:
IE24D COPXES RECEIVED:LTR ENCL SIZE:
TITLE: Monthly 'Operating Report (per Tech Specs NOTES:
D RECIPXENT ID CODE/NAME PD3-1 LA COLBURN,T.
INTERNAL: AEOD/DOA P
PEB10 REG "FI~L 0 1 EXTERNAL EG&G BRYCE iJ
~ H NSIC COPIES LTTR ENCL 3
3 1
1 1
1 1
1 1
1 1
1 1
1 RECIPIENT ID CODE/NAME PD3-1 PD AEOD/DSP/TPAB NRR/DOEA/OEAB RGN3 NRC PDR COPIES LTTR ENCL 1
1 1
1 1
1 1
1 D
S I
Q NOTE TO ALL"RIDS" RECIPIENTS:
D PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 2%79) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
TOTAL NUMBER OF COPIES REQUIRED:
LTTR 14 ENCL 14
~i'
Power Company Cook Nuclear Plant One Cook Place Bridgman, Ml 49106 616 465 5901 March 5, 1991 IHENAlUA NlCHEGQM PQWM U.S. Nuclear Regulatory Commission ATTN:
Document Control Desk Washington, D.C.
20555 Gentlemen:
Pursuant to the requirements of Donald C.
Cook Nuclear Plant Unit 2 Technical Specification 6.9.1.10, the attached Monthly Operating Report for the month of February 1991 is submitted.
Respectfully, A.A. Blind Plant Manager Attachment C
NRC R D. R.
EPRI R.C.
S.L.
J.G.
W M.P.
A J.F.
K J.J.
M D.A. T D.W.
T.O.
A S.H.
J.L.
L J.A.
W.T.
G E.A.
J.C.
K B.A.
D.F.
K E.C.
egion III Hahn Nuclear Safety Analysis Center Callen Hall eppler ecords Center uclear Engineering Department illiams, Jr.
lexich urgan arkowsky imber lake Paul rgenta Steinhart eichner Isom illett Smarrella rieger Svensson rause Schimmel 9i03i30245 9i0223 PDR ADOCK 05000316 R
N.R.C OPERATING DATA REPORT DOCKET NO.
50-316 DATE 01-Mar-91 COMPLETED BY JD JANISSE TELEPHONE 616-465-5901 OPERATING STATUS
- 1. Unit Name D.
C.
Cook Unit 2
- 2. Reporting Period FEB.91
- 3. Licensed Thermal Power (MWt) 3411 4.
Name Plate Rating (Gross MWe) 1133
- 5. Design Electrical Rating (Net MWe) 1100 6.
Maximum Dependable Capacity (GROSS MWe) 1100 7.
Maximum Dependable Capacity (Net MWe) 1060 notes
- 8. If Changes Occur in Capacity Ratings (Items no.
3 through
- 7) Since Last Report Give Reasons 9.
Power Level To Which Restricted. If Any (Net MWe) 10.
Reasons For Restrictions. If Any:
- 11. Hours in Reporting, Period 12.
No. of Has. Reactor Was Critical
- 13. Reactor Reserve Shutdown Hours
- 14. Hours Generator on Line
- 15. Unit Reserve Shutdown Hours
- 16. Gross Therm.
Energy Gen.
(MWH) 17.
Gross Elect.
Energy Gen.
(MWH)
- 18. Net Elect. Energy Gen.
(MWH)
- 19. Unit Service Factor
- 20. Unit Availability Factor
- 21. Unit Capacity Factor (MDC Net)
- 22. Unit Capacity Factor (DER Net)
- 23. Unit Forced Outage Rate 24.
Shutdowns Scheduled over Next Six This Mo.
Yr. to Date Cumm.
672 '
1416.0 115368 '
672.0 1416.0 76550.9 0.0 0 '
0.0 672.0 1416.0 75001.9 0.0 0.0 0.0 2110364
'643404 230810457 693600 1533620 75320460 668517 1481084 82540051 100.0 100.0 66.4 100.0 100.0 66.4 93.9 98.7 60 '
90.4 95.1 58 '
0.0 0.0 13.4 Months (Type, Date,and Duration):
- 25. If Shut Down At End of Report Period, Estimated Date of Startup:
- 26. Units in Test Status (Prior to Commercial Operation):
Forcast INITIALCRITICALITY INITIALELECTRICITY COMMERCIAL OPERATION Achieved
AVERAGE DAILY POWER LEVEL (MWe-Net)
DOCKET NO.
50-316 UNIT TWO DATE 01-Mar-91 COMPLETED BY JD JANISSE TELEPHONE 616-465-5901 DAY 1
2 3
4 5
6 7
8 9
10 11 12 13 14 15 16 MONTH AVERAGE DAILY POWER LEVEL 1086 1092 1094 1096 1093 1092 1092 1092 1092 1093 1090 1092 1091 1093 1089 878 FEB.91 DAY 17 18 19 20 21 22 23 24 25 26 27 28 AVERAGE DAILY.
POWER LEVEL 594 596 606 609 683 1013 1063 1087 1084 1092 1086 1086
UNIT SHUIDOWNS AND POWER REDUCZIONS REPORZ MOTH:
February 1991 DOCKET NO:
UNIT NAME:
DATE:
COMIKZTED BY:
TEEZPHONE 50-316 D.C.
COOK UNIT 2-March 5, 1991 E.C. Schimmel (616) 465-5901 METHOD OF SHVITING LICENSEE DURATION DOWN EVEPZ NO DATE TYPE HOURS REASON REACTOR REPORT NO.
SYSZM COMPONENTS CAUSE AND CORRHCZIVE ACZION 'IO CODE CODE5 PREVIWZ RIXXJBMKCE 212 910216 213 910222 N/A N/A Unit power was reduced to 59% starting 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br /> on 910216 to permit cl of the east and west main feed pump turbine condensers.
The time period the unit was at the reduced pcver level was extended due to problems experi~ with the east main feeds~ turbine speed control during the pcarer reduction. unit pcarer was restored to 100% at 0144 hours0.00167 days <br />0.04 hours <br />2.380952e-4 weeks <br />5.4792e-5 months <br /> on 910222.
A forced power reduction to 70:
starting at 0750 hours0.00868 days <br />0.208 hours <br />0.00124 weeks <br />2.85375e-4 months <br /> on 912222 occurred due to Xenon buildup while the primary water makeup supply for RCS dilution was isolated to perform forced maintenance repairs on primary water valve PW-269. Reactor poorer was restored to 100% at 0639 hours0.0074 days <br />0.178 hours <br />0.00106 weeks <br />2.431395e-4 months <br /> on 910223.
1 F:
S 2
Forced Reason:
Scheduled A:
Hcpipment Failure (Explain)
B:
Maintenance or Test C:
Refueling D:
Regulatory Restriction E:
Operator Training and License E>amination F:
Administrative G:
Operational Error (Explain)
H:
Other (Explain) 3 Method 1:
Manual 2:
Manual Scram 3:
Other (Explain) 4 5
Exhibit G Instructions Exhibit I:
Same Source for preparation of data entry sheets for Licensee Event Report (LER) File (NUREG 0161)
DOCKET NO:
UNIT NAME:
COMPLETED BY:
TELEPHONE:
DATE'AGE0 50-316 D.C.
Cook Unit 2 E.C.
Schimmel (616) 465-5901 March 5, 1991 1 of 1 MONTHLY OPERATING ACTIVITIES Februar 1991 HIGHLIGHTS The unit entered the reporting period at 100% Rated Thermal Power.
Unit power was reduced to 594 RTP on 910216 to allow for east and west main feedpump turbine condenser cleaning.
The time period the unit was at the reduced power level was extended due to problems experienced with the east main feedpump turbine speed control during the power reduction. Unit power was restored to 100%
RTP on 910221.
A forced power reduction to 70% RTP occurred on 910222.
The power reduction was caused by the negative reactivity effect of Xenon buildup following the power increase to 100~o RTP on 910221.
The primary water system makeup to the RCS had to be isolated to perform maintenance on a failed primary water system valve which removed the ability to dilute the reactor coolant.
Repairs were completed and power increased to 1004 RTP starting 2025 hours0.0234 days <br />0.563 hours <br />0.00335 weeks <br />7.705125e-4 months <br /> on 910222.
The unit reached 100%
RTP at 0639 hours0.0074 days <br />0.178 hours <br />0.00106 weeks <br />2.431395e-4 months <br /> on 910223.
The unit exited the reporting period at 100%
RTP.
Gross electrical generation for the month of February was 693600 MWH.
DETAILS 02/16/91 1200 Commenced unit power decrease to 594 RTP for east and west main feedpump turbine condenser cleaning.
1650 The unit is at 594 RTP.
02/21/91 1440 Commenced unit power increase to 100% RTP.
02/22/91 0144 The unit is at 1004 RTP.
02/22/91 0750 The boration flowpath LCO is entered.
Reactor power drifts down to 70> RTP due to Xenon buildup while all dilution flowpaths are isolated for repair of the boration flowpath leak.
2025 The unit is at 704 RTP.
Commenced unit power increase to 1004 RTP.
02/23/91 0639 The unit is at 100~ RTP.
DOCKET NO:
UNIT NAME:
COMPLETED BY:
TELEPHONE:
~
DATE'AGE:
50-316 D.C.
Cook Unit 2 E.C.
Schimmel (616) 465-5901 March 5, 1991 1 of 1
MAJOR SAFETY-RELATED MAINTENANCE Februar 1991 The AB train emergency diesel generator fuel oil transfer
- pump, QT-106-AB2 was unable to meet its required flow. The defective pump was replaced with a new pump.
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