ML17325A719
| ML17325A719 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 01/31/1988 |
| From: | Michaelson INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| To: | |
| Shared Package | |
| ML17325A636 | List: |
| References | |
| NUDOCS 8803040140 | |
| Download: ML17325A719 (10) | |
Text
N.R.C.
OPERATING DATA REPORT DOCKET NO.
50-316 DATE 2/1/88 COMPLETED BY Michaelson TELEPHONE 616-465-5901 OPERATING STATUS 1.
Unit, Name D.
C.
Cook Unit 2
- 2. Reporting Period JAN 88
,'notes 3.
Licensed Thermal Power (MWt) 3411 I
4.
Name Plate Rating (Gross MWe) 1133
- 5. Design Electrical Rating (Net MWe) 1100 6.
Maximum Dependable Capacity (GROSS MWe) 1100 7.
Maximum Dependable Capacity (Net MWe) 1060
- 8. If Changes Occur in Capacity Ratings (Items no.
3 through 7) Since Last Report Give Reasons 9.
Power Level To Which Restricted. If Any (Net MWe) 10.
Reasons For Restrictions. If Any:
This Mo.
Yr. to Date Cumm.
11 'ours in Reporting Period 744.0 744.0 88392.0 12.
No. of Hrs.
Reactor.
Was Critical 744.0 744.0 61623.6
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 0.0 14.
Hours Generator on Line 744. 0 744.0 60238.9
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0 16.
Gross Therm.
Energy Gen.
(MWH) 2039814 2039814 184195211 17.
Gross Elect.
Energy Gen.
(MWH) 667470 667470 60144090 18.
Net, Elect.
Energy Gen.
(MWH) 641192 641192 57902592 19'nit Service Factor 100.0 100. 0 70.1
- 20. Unit Availability Factor 100.0 100.0 70.1
- 21. Unit Capacity Factor (MDC Net) 81.3 81.3 63.6
- 22. Unit Capacity Factor (DER Net) 78.3
- 78. 3 62.0 23'nit Forced Outage Rate 0.0 0.0 14 F 9 24.
Shutdowns Scheduled over Next Six Months (Type, Date and Duration):
Stea~menerator replacement o~uta e to begin on April 23, 1958 for an estimated duration of 225 d~a s.
- 25. If Shut Down At End of Report Period, Estimated Date of Startup:
- 26. Units in Test Status (Prior to Commercial Operawion):
Forcast INITIAL CRITICALITY INITIALELECTRICITY COMMERCIAL OPERATION Achieved PDR ADOCW.05000316.
QI 1,g
~..I 4
AVERAGE DAILY POWER LEVEL (MWe-Net)
DOCKET NO.
50-316 UNIT TWO DATE 2/1/88 COMPLETED BY M1chaelson TELEPHONE 616-465-5901 DAY 2
3 5
6 7
8 9
10 11 12 13 14 15 16 MONTH AVERAGE DAILY POWER LEVEL 865 863 86,5 863 861 861 863 864 858 861 862 866 861 861 861 863 JAN 88 DAY 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 AVERAGE DAILY POWER LEVEL 864 863 861 864 858 863 862 863 862 860 862 861 855 857 864
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Q cl OQu Cause k Collcclivc Acli)HIlo Plcvcos Itecullco).c NONE There were no Unit shutdowns or significant power reductions during the month.
The unit has operate'd at a nominal 80%. power limit admin-istratively imposed to minimize steam qenerator tube degradation.
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DOCKET NO:
UNIT NAME:
COMPLETED BY:
TELEPHONE:
DATE:
PAGE:
50-316 D.C.
Cook Unit 2 A. S. Puplis (616) 465-5901 February 5, 1988 1of 1
HIGHLIGHTS MONTHLY OPERATING ACTIVITIES - JANUARY 1988 The reporting period began and ended with the unit in Mode 1 at 80% of rated thermal power.
Gross electrical generation was 667,470 MWH for the month.
SUMMARY
01-18-88 At 0321, 2AB Emergency Diesel failed to start from the Control Room and was declared inoperable.
Evaluation of the investigation findings determined the cause of the failure to start was a stuck open starting air valve(s).
All starting air valves were replaced since it was not known which cylinder(s) the engine was lined up to initially.
Upon removal, all 12 starting air check valves were checked and found to be operating satisfactorily.
It is likely that the stuck valve(s) was/were freed when the engine was started on a
different cylinder (due to the pressure buildup).
2 AB Emergency Diesel Generator was declared operable at 2225 on 1-18-88.
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DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE PAGE 50-316 D.C.Cook-Unit No.
2 Februar 5,
1988 S.
Pu is 616 65-5901 lof 1 MAJOR SAFETY-RELATED MAINTENANCE JANUARY 1988 18C ¹1 027567--ECR-536, the post accident sampling containment gas space isolation valve, would not open.
Found the coil in ASCO solenoid valve XSO-1536 to be defective.
Replaced defective coil with new coil and verified proper valve operation.
ISC ¹2 013213 Pressurizer pressure channels NPP-151 and NPP-152 indicated a 20 psig difference between channels I and II.
Channel reading in protection racks revealed that channel I read 20 PSI lower than channel II.
Found amplifier in pressure transmitter NPP-151 to be defective.
Replaced defective amplifier with new amplifier and recalibrated as per 2 THP 6030 IMP.215.
Found indicator NPP-152 to be out of specifications 10 PSIG high.
Recalibrated indicator as per 2
THP 6030 IMP.215.
Found pressure transmitter NPP-152 to be out of specifications high 3. 1%.
Recali-brated pressure transmitter PP-152 as per 2 THP 6030 IMP.215.
All three channels of pressurizer pressure now read within allowable specifications.
013531--2-VCR-10 (Ice Condenser Refrigeration Glycol Supply Header Train 'A'ontainment Isolation Valve) would not operate due to a
ruptured diaphragm.
The diaphragm was replaced and the valve tested satisfactorily.
M-2 013734 The AB Diesel Generator failed to start for a surveillance run.
A starting air valve was found to be stuck open.
All the starting air valves were replaced and the engine started satisfac-torilyy.
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