Similar Documents at Cook |
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217J4721999-10-15015 October 1999 Forwards NRC Physical Security Insp Repts 50-315/99-27 & 50-316/99-27 on 990920-24.Two Violations Noted & Being Treated as Ncvs,Consistent with App C of Enforcement Policy. Areas Examined Exempt from Disclosure,Per 10CFR73.21 IA-99-379, First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety1999-10-0808 October 1999 First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety ML20217D9241999-10-0808 October 1999 First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety ML17335A5511999-10-0707 October 1999 Forwards LER 99-023-00, Inadequate TS Surveillance Testing of ESW Pump ESF Response Time. Commitments Identified in LER Listed ML20217D9361999-09-30030 September 1999 FOIA Request for Document Re Section 9.7 of SE by Directorate of Licensing,Us Ae Commission in Matter of Indiana & Michigan Electric Co & Indiana & Michigan Power Co,Dc Cook Nuclear Plan,Units 1 & 2 ML17326A1541999-09-20020 September 1999 Provides Notification of Change in Senior Licensed Operator Status.Operating Licenses for CR Smith,License SOP-30159-4 & Tw Welch,License SOP-30654-2 Are No Longer Required & Should Be Withdrawn ML17326A1441999-09-17017 September 1999 Submits Trace on Second Shipment of Two Plant,Unit 2 Steam Generators.Info Re Shipment Submitted ML17326A1261999-09-17017 September 1999 Forwards LER 99-022-00 Re Electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads.Listed Commitment Identified in Submittal ML17326A1531999-09-16016 September 1999 Submits Info Pertaining to Plant Proposed Operator Licensing Exam Requirements Through Yr 2003.NRC Form 536, Operator Licensing Exam Data, Which Provides Required Info Encl ML17326A1101999-08-27027 August 1999 Forwards LER 99-021-00, GL 96-01 Test Requirements Not Met in Surveillance Tests. List of Commitments Identified in LER Provided ML17326A0991999-08-26026 August 1999 Forwards LER 99-020-00,re EDGs Being Declared Inoperable. Commitments Made by Util Are Listed ML17326A1221999-08-23023 August 1999 Forwards Revised Page 2 to 1998 Annual Environ Operating Rept, for DC Cook Nuclear Plant,Correcting Omission to App I ML17326A0981999-08-23023 August 1999 Forwards fitness-for-duty Program Performance Data for Period of 990101-0630 for DC Cook Nuclear Plants,Units 1 & 2,per 10CFR26.71(d) ML17326A0891999-08-16016 August 1999 Forwards LER 99-019-00,re Victoreen Containment High Range Monitors Not Beign Environmentally Qualified to Withstand post-LOCA Conditions.Commitments Made by Util Are Listed ML17326A0811999-08-10010 August 1999 Notifies NRC of Changes in Commitments Made in Response to GL 98-01,supplement 1, Yr 2000 Readiness of Computer Sys Ar Npps, Dtd 990623 ML17326A0821999-08-0606 August 1999 Informs That Util Is Submitting Encl Scope & Objectives for 991026 DC Cook Nuclear Plant Emergency Plan Exercise to G Shear of NRC Plant Support Branch.Exercise Will Include Full State & County Participation ML17326A1451999-08-0404 August 1999 Requests Withholding of WCAP-15246, Control Rod Insertion Following Cold Leg Lbloca. ML17326A0751999-08-0404 August 1999 Forwards LER 98-029-01, Fuel Handling Area Ventilation Sys Inoperable Due to Original Design Deficiency. Supplemental Rept Represents Extensive Rev to Original LER & Replaces Rept in Entirely.Commitment Listed ML17326A0721999-07-29029 July 1999 Forwards LER 99-018-00 Re Refueling Water Storage Tank Suction Motor Operated Valves Inoperable,Due to Inadequate Design.Listed Commitments Were Identified in LER ML17326A0711999-07-27027 July 1999 Responds to 980123 RAI Re NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issue (USI) A-46. ML17326A0601999-07-22022 July 1999 Forwards UFSAR, IAW 10CFR50.71(e) & Rept of Changes,Tests & Experiments as Required by 10CFR50.59(b)(2) for DC Cook Nuclear Plant,Units 1 & 2.Without UFSAR ML17326A0631999-07-22022 July 1999 Forwards LER 98-014-03, Response to High-High Containment Pressure Procedure Not Consistent with Analysis of Record. Revised Info Marked by Sidebars in Right Hand Margin. Commitments Made by Util,Listed ML17326A0311999-07-0101 July 1999 Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed ML20196K5961999-06-30030 June 1999 Ltr Contract:Task Order 40, DC Cook Extended Sys Regulatory Review Oversight Insp, Under Contract NRC-03-98-021 ML17326A0281999-06-28028 June 1999 Provides Response to 981116 & 960228 RAIs Re GL 92-01. Revised Pressurized Thermal Shock Evaluation Based on New Weld Chemistry Info & Copy of W Rept WCAP-15074, Evaluation of 1P3571 Weld Metal from Surveillance Programs... Encl ML17326A0241999-06-23023 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant & List of Commitments Encl ML17326A0121999-06-18018 June 1999 Forwards LER 99-014-00 Re Requirement of TS 4.0.5 Not Met for Boron Injection Tank Bolting.Commitments Identified in Submittal Listed ML17326A0111999-06-11011 June 1999 Provides Response to NRC RAI Re GL 97-01, Degradation of Crdm/Cedm Nozzle & Other Vessel Closure Head Penetrations. ML17325B6281999-06-0101 June 1999 Forwards LER 99-S03-00,re Nonconforming Vital Area Barriers.Commitments Made by Util Are Listed ML17325B6401999-06-0101 June 1999 Forwards LER 99-013-00 Re Safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Lead to ECCS Pump Failure.Listed Commitments Identified in Submittal ML17325B6331999-05-28028 May 1999 Forwards LER 99-S02-00,re Vulnerability in Safeguard Sys That Could Allow Unauthorized or Undetected Access to Protected Area.Commitments Made by Util Are Listed ML17265A8201999-05-24024 May 1999 Forwards LER 98-037-01,representing Extensive Rev to Original LER & Replacing Rept in Entirety.Listed Commitments Identified in Submittal ML20207A9201999-05-21021 May 1999 Ack Receipt of 990319 Response to Notice of Violation & Proposed Imposition of Civil Penalty .On 981124, Licensee Remitted Check for Payment of Civil Penalties. Licensee Requests for Extension for Response,Granted ML17325B6111999-05-21021 May 1999 Forwards Annual Radioactive Effluent Release Rept for 980101-1231 for DC Cook Nuclear Plant,Units 1 & 2. Transmittal of Submittal Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17325B6031999-05-21021 May 1999 Provides Response to NRC GL 98-04, Potential for Degradation of ECCS & Containment Spray Sys After LOCA Because of Const & Protective Coating Deficiencies & Foreign Matl in Containment. ML17325B5971999-05-20020 May 1999 Forwards LER 99-012-00,re Auxiliary Building ESF Ventilation Sys Not Being Capable of Maintaining ESF Room Temps post-accident.Commitment,listed ML17335A5281999-05-12012 May 1999 Forwards DC Cook Nuclear Plant Fitness for Duty Program Performance Dtd for six-month Period of 980701-1231,IAW 10CFR26.71(d).Info Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17335A5271999-05-11011 May 1999 Forwards Details Re Sources & Levels of Insurance Maintained for DC Cook,Units 1 & 2,as of 990401,per 10CFR50.54(w)(3). Info Was Delayed Beyond Required Date Due to Internal Oversight ML17325B5841999-05-10010 May 1999 Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed ML17325B5871999-05-0707 May 1999 Forwards Current Revs of Expanded Sys Readiness Review (Essr) Implementing Procedures,For Info Purposes to Support Current NRC Insps.Current Esrr Schedule Provided for Info Purposes,Reflecting Revised Target Dates ML17325B5791999-05-0404 May 1999 Forwards LER 99-011-00,concerning Air Sys for EDG Not Supporting Long Term Operability.Commitments Made by Util Listed ML17325B5821999-05-0404 May 1999 Provides Addl Background,Description & Clarification of Previous & Revised Commitments Re UFSAR Revalidation Effort. Commitment Change Involved Alignment of UFSAR Revalidation Program Methodology to Strategy Contained in Current Plan ML17325B5741999-05-0303 May 1999 Forwards LER 99-010-00 Re RCS Leak Detection Sys Sensitivity Not in Accoradnce with Design Requirements.Listed Commitments Identified in Submittal ML17325B5631999-04-22022 April 1999 Forwards Results of Independent Chemical Evaluations Performed from Sept 1997 Through Feb 1999,re Resolution of Issues Related to License Amend 227 ML17325B5561999-04-16016 April 1999 Forwards LER 99-006-00, Fuel Crane Loads Lifted Over SFP Could Impact Energies Greater than TS Limits, IAW 10CFR50.73.Submittal Was Delayed to Allow for Resolution of Questions.Commitment Made by Licensee,Listed ML20205P0591999-04-14014 April 1999 Ninth Partial Response to FOIA Request for Documents.App Records Already Available in Pdr.Records in App T Encl & Being Made Available in Pdr.App U Records Being Released in Part (Ref FOIA Exemption 7).App V Records Withheld Entirely ML17325B5451999-04-12012 April 1999 Forwards LER 99-009-00 Re as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit.Commitments Identified in Submittal Listed ML17325B5301999-04-0707 April 1999 Forwards LER 99-S01-01, Vulnerability in Locking Mechanism of Four Vital Area Gates, Per 10CFR50.73.Commitments Made by Util,Listed ML17325B5241999-04-0505 April 1999 Forwards Revs 0 & 1 to Cook Nuclear Plant Restart Plan, Dtd 980307 & 0407.Rev 5 Is Current Cook Nuclear Plant Restart & Supercedes Previous Revs in All Respects ML17325B5121999-04-0101 April 1999 Forwards LER 99-007-00, Calculations Show That Divider Barrier Between Upper & Lower Containment Vols May Be Overstressed. Commitments Made by Util Are Listed 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML17335A5511999-10-0707 October 1999 Forwards LER 99-023-00, Inadequate TS Surveillance Testing of ESW Pump ESF Response Time. Commitments Identified in LER Listed ML20217D9361999-09-30030 September 1999 FOIA Request for Document Re Section 9.7 of SE by Directorate of Licensing,Us Ae Commission in Matter of Indiana & Michigan Electric Co & Indiana & Michigan Power Co,Dc Cook Nuclear Plan,Units 1 & 2 ML17326A1541999-09-20020 September 1999 Provides Notification of Change in Senior Licensed Operator Status.Operating Licenses for CR Smith,License SOP-30159-4 & Tw Welch,License SOP-30654-2 Are No Longer Required & Should Be Withdrawn ML17326A1261999-09-17017 September 1999 Forwards LER 99-022-00 Re Electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads.Listed Commitment Identified in Submittal ML17326A1441999-09-17017 September 1999 Submits Trace on Second Shipment of Two Plant,Unit 2 Steam Generators.Info Re Shipment Submitted ML17326A1531999-09-16016 September 1999 Submits Info Pertaining to Plant Proposed Operator Licensing Exam Requirements Through Yr 2003.NRC Form 536, Operator Licensing Exam Data, Which Provides Required Info Encl ML17326A1101999-08-27027 August 1999 Forwards LER 99-021-00, GL 96-01 Test Requirements Not Met in Surveillance Tests. List of Commitments Identified in LER Provided ML17326A0991999-08-26026 August 1999 Forwards LER 99-020-00,re EDGs Being Declared Inoperable. Commitments Made by Util Are Listed ML17326A1221999-08-23023 August 1999 Forwards Revised Page 2 to 1998 Annual Environ Operating Rept, for DC Cook Nuclear Plant,Correcting Omission to App I ML17326A0981999-08-23023 August 1999 Forwards fitness-for-duty Program Performance Data for Period of 990101-0630 for DC Cook Nuclear Plants,Units 1 & 2,per 10CFR26.71(d) ML17326A0891999-08-16016 August 1999 Forwards LER 99-019-00,re Victoreen Containment High Range Monitors Not Beign Environmentally Qualified to Withstand post-LOCA Conditions.Commitments Made by Util Are Listed ML17326A0811999-08-10010 August 1999 Notifies NRC of Changes in Commitments Made in Response to GL 98-01,supplement 1, Yr 2000 Readiness of Computer Sys Ar Npps, Dtd 990623 ML17326A0821999-08-0606 August 1999 Informs That Util Is Submitting Encl Scope & Objectives for 991026 DC Cook Nuclear Plant Emergency Plan Exercise to G Shear of NRC Plant Support Branch.Exercise Will Include Full State & County Participation ML17326A1451999-08-0404 August 1999 Requests Withholding of WCAP-15246, Control Rod Insertion Following Cold Leg Lbloca. ML17326A0751999-08-0404 August 1999 Forwards LER 98-029-01, Fuel Handling Area Ventilation Sys Inoperable Due to Original Design Deficiency. Supplemental Rept Represents Extensive Rev to Original LER & Replaces Rept in Entirely.Commitment Listed ML17326A0721999-07-29029 July 1999 Forwards LER 99-018-00 Re Refueling Water Storage Tank Suction Motor Operated Valves Inoperable,Due to Inadequate Design.Listed Commitments Were Identified in LER ML17326A0711999-07-27027 July 1999 Responds to 980123 RAI Re NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issue (USI) A-46. ML17326A0601999-07-22022 July 1999 Forwards UFSAR, IAW 10CFR50.71(e) & Rept of Changes,Tests & Experiments as Required by 10CFR50.59(b)(2) for DC Cook Nuclear Plant,Units 1 & 2.Without UFSAR ML17326A0631999-07-22022 July 1999 Forwards LER 98-014-03, Response to High-High Containment Pressure Procedure Not Consistent with Analysis of Record. Revised Info Marked by Sidebars in Right Hand Margin. Commitments Made by Util,Listed ML17326A0311999-07-0101 July 1999 Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed ML17326A0281999-06-28028 June 1999 Provides Response to 981116 & 960228 RAIs Re GL 92-01. Revised Pressurized Thermal Shock Evaluation Based on New Weld Chemistry Info & Copy of W Rept WCAP-15074, Evaluation of 1P3571 Weld Metal from Surveillance Programs... Encl ML17326A0241999-06-23023 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant & List of Commitments Encl ML17326A0121999-06-18018 June 1999 Forwards LER 99-014-00 Re Requirement of TS 4.0.5 Not Met for Boron Injection Tank Bolting.Commitments Identified in Submittal Listed ML17326A0111999-06-11011 June 1999 Provides Response to NRC RAI Re GL 97-01, Degradation of Crdm/Cedm Nozzle & Other Vessel Closure Head Penetrations. ML17325B6401999-06-0101 June 1999 Forwards LER 99-013-00 Re Safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Lead to ECCS Pump Failure.Listed Commitments Identified in Submittal ML17325B6281999-06-0101 June 1999 Forwards LER 99-S03-00,re Nonconforming Vital Area Barriers.Commitments Made by Util Are Listed ML17325B6331999-05-28028 May 1999 Forwards LER 99-S02-00,re Vulnerability in Safeguard Sys That Could Allow Unauthorized or Undetected Access to Protected Area.Commitments Made by Util Are Listed ML17265A8201999-05-24024 May 1999 Forwards LER 98-037-01,representing Extensive Rev to Original LER & Replacing Rept in Entirety.Listed Commitments Identified in Submittal ML17325B6111999-05-21021 May 1999 Forwards Annual Radioactive Effluent Release Rept for 980101-1231 for DC Cook Nuclear Plant,Units 1 & 2. Transmittal of Submittal Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17325B6031999-05-21021 May 1999 Provides Response to NRC GL 98-04, Potential for Degradation of ECCS & Containment Spray Sys After LOCA Because of Const & Protective Coating Deficiencies & Foreign Matl in Containment. ML17325B5971999-05-20020 May 1999 Forwards LER 99-012-00,re Auxiliary Building ESF Ventilation Sys Not Being Capable of Maintaining ESF Room Temps post-accident.Commitment,listed ML17335A5281999-05-12012 May 1999 Forwards DC Cook Nuclear Plant Fitness for Duty Program Performance Dtd for six-month Period of 980701-1231,IAW 10CFR26.71(d).Info Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17335A5271999-05-11011 May 1999 Forwards Details Re Sources & Levels of Insurance Maintained for DC Cook,Units 1 & 2,as of 990401,per 10CFR50.54(w)(3). Info Was Delayed Beyond Required Date Due to Internal Oversight ML17325B5841999-05-10010 May 1999 Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed ML17325B5871999-05-0707 May 1999 Forwards Current Revs of Expanded Sys Readiness Review (Essr) Implementing Procedures,For Info Purposes to Support Current NRC Insps.Current Esrr Schedule Provided for Info Purposes,Reflecting Revised Target Dates ML17325B5821999-05-0404 May 1999 Provides Addl Background,Description & Clarification of Previous & Revised Commitments Re UFSAR Revalidation Effort. Commitment Change Involved Alignment of UFSAR Revalidation Program Methodology to Strategy Contained in Current Plan ML17325B5791999-05-0404 May 1999 Forwards LER 99-011-00,concerning Air Sys for EDG Not Supporting Long Term Operability.Commitments Made by Util Listed ML17325B5741999-05-0303 May 1999 Forwards LER 99-010-00 Re RCS Leak Detection Sys Sensitivity Not in Accoradnce with Design Requirements.Listed Commitments Identified in Submittal ML17325B5631999-04-22022 April 1999 Forwards Results of Independent Chemical Evaluations Performed from Sept 1997 Through Feb 1999,re Resolution of Issues Related to License Amend 227 ML17325B5561999-04-16016 April 1999 Forwards LER 99-006-00, Fuel Crane Loads Lifted Over SFP Could Impact Energies Greater than TS Limits, IAW 10CFR50.73.Submittal Was Delayed to Allow for Resolution of Questions.Commitment Made by Licensee,Listed ML17325B5451999-04-12012 April 1999 Forwards LER 99-009-00 Re as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit.Commitments Identified in Submittal Listed ML17325B5301999-04-0707 April 1999 Forwards LER 99-S01-01, Vulnerability in Locking Mechanism of Four Vital Area Gates, Per 10CFR50.73.Commitments Made by Util,Listed ML17325B5241999-04-0505 April 1999 Forwards Revs 0 & 1 to Cook Nuclear Plant Restart Plan, Dtd 980307 & 0407.Rev 5 Is Current Cook Nuclear Plant Restart & Supercedes Previous Revs in All Respects ML17325B5121999-04-0101 April 1999 Forwards LER 99-007-00, Calculations Show That Divider Barrier Between Upper & Lower Containment Vols May Be Overstressed. Commitments Made by Util Are Listed ML17325B5141999-03-30030 March 1999 Forwards Rept on Status of Decommissioning Funding.Attached Rept Includes Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML17325B5191999-03-29029 March 1999 Forwards LER 99-001-00,re Degraded Component Cw Flow to Containment Main Steam Line Penetrations.Commitment, Listed ML20204F6401999-03-19019 March 1999 Responds to NRC 981013 NOV & Proposed Imposition of Civil Penalty.Violations Cited in Subject NOV Were Initially Identified in Referenced Five Insp Repts.Corrective Actions: Ice Condensers Have Been Completely Thawed of Any Blockage ML17325B4751999-03-18018 March 1999 Forwards LER 99-004-00,re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitment Made by Util,Listed ML17325B4721999-03-18018 March 1999 Forwards LER 99-005-00,re Reactor Trip Breaker Manual Actuations During Rod Drop Testing Not Previously Reported. Listed Commitments Identified in Submittal ML17325B4641999-03-17017 March 1999 Withdraws Response to Issue 1 of NRC Cal,Dtd 970919. Comprehensive Design Review Effort in Progress to Validate Resolution of Issue for Future Operation 1999-09-30
[Table view] Category:UTILITY TO NRC
MONTHYEARML17328A4481990-09-21021 September 1990 Requests Withdrawal of Mode 6 Proposed Tech Spec Change Since Issue Currently Being Addressed by New STSs ML17328A4331990-08-27027 August 1990 Informs of Preliminary Assessment of 900713 Electrical Contact Accident at Facility.Investigation Concludes That No Safety Rules Violated ML17328A4001990-08-24024 August 1990 Responds to 900725 Ltr Re Commitments Made in Response to Generic Ltr 88-14 on Instrument Air Supply Problems Affecting safety-related Equipment.Simulator Training to Be Provided as Stated ML17334B3781990-08-24024 August 1990 Forwards Info to Certify Plant Simulator Facility.Results of Evaluation of Dual Unit Simulation Facilities Demonstrate That Plant Simulator Performance Compares Favorably W/Units ML17328A4231990-08-21021 August 1990 Forwards Under Separate Cover,Semiannual Radioactive Effluent Release Rept for Jan-June 1990 ML17328A3901990-08-17017 August 1990 Responds to NRC 900720 Ltr Re Violations Noted in Onsite Audit of Spds.Corrective Actions:Apparent Disparity in Selection of Reactor Trip & Sys Capacity or Anticipatory Values Rectified ML17328A3891990-08-15015 August 1990 Forwards Performance Data Sheets for Plant fitness-for-duty Program for Period Jan-June 1990,per 10CFR26.Encl Includes Statistics on Various Categories of Testing,Substances Tested for & cut-off Levels Used ML17328A3571990-08-0202 August 1990 Responds to Open Items in Safety Evaluation of Util Response to Unresolved Issues on post-fire Safe Shutdown Methodology. Open Items 1 & 21 Will Be Closed by Implementing Plant Procedures Providing Equivalent Degree of Protection ML17328A3431990-07-23023 July 1990 Requests Withdrawal of 890830 Proposed Tech Spec Changes Re Sections 3.0 & 4.0.Util Will Resubmit Generic Ltr 87-09 Recommended Improvement Items on Case by Case Basis ML17328A3421990-07-23023 July 1990 Provides Results of Offsite Dose Calculation for Reactor Coolant Pump Locked Rotor Event for Facility Cycle 8.Util Identified Previously Issued SERs Addressing Short Term Containment Analysis & LOCA Containment Integrity ML20055G7551990-07-18018 July 1990 Responds to NRC Re Violations Noted in Insp Repts 50-315/90-10 & 50-316/90-10.Corrective Actions:Required Review Performed & Updated Procedure 12 Mhp 5021.019.001 Revised & Issued ML17328A3191990-07-12012 July 1990 Responds to NRC 900601 Ltr Re Violations Noted in Insp Repts 50-315/89-31 & 50-316/89-31.Corrective Actions:Electrical Testing Techniques Improved & Surveillance Procedures for Feedwater Pumps Will Be Rewritten ML17328A3181990-07-0909 July 1990 Responds to Generic Ltr 90-03,Suppl 1, Relaxation of Staff Position in Generic Ltr 83-28,Item 2.2,Part 2, 'Vendor Interface for Safety-Related Components.' Licensee Will Contact safety-related Vendors on Annual Basis ML17328A3111990-07-0303 July 1990 Provides Certification of Funding Plan for Decommissioning of Plant,Per 10CFR50.33 & 50.75 ML17328A2961990-06-25025 June 1990 Forwards Response to Generic Ltr 90-04 Re Closeout of Generic Safety Issues.Util Supports Concern & Desire to Close long-standing Generic Safety Issues ML17328A2921990-06-22022 June 1990 Forwards WCAP-12483, Analysis of Capsule U from American Electric Power Co DC Cook Unit 1 Reactor Vessel Radiation Surveillance Program. ML20044A3521990-06-22022 June 1990 Submits Info Re Sensitivity Study Performed on Number of Fuel Axial Intervals,Per Topical Rept, American Electric Power Reactor Core Thermal-Hydraulic Analysis Using Cobra III-C/MIT-2 Computer Code. ML17328A2821990-06-15015 June 1990 Submits Ltr Re Proposed Control Room Habitability Tech Spec Changes & Supporting Analyses,Per 900521 Discussion.Revised Calculations of Control Room Thyroid Doses Will Be Submitted within 60 Days of Receipt of Proposed Generic Ltr ML17328A2741990-06-12012 June 1990 Submits Followup,Per 900205 & 0308 Ltrs & Provides Update Re Inoperable Fire Barrier.Fire Seal Repaired & Restored to Operability on 900419 ML17328A2551990-06-0505 June 1990 Forwards Addl Info Re Util 900126 Revised Response to NRC Bulletin 88-002,per NRC 900509 Request ML17328A7361990-06-0101 June 1990 Forwards Addl Info Re 890825 & 1212 Applications for Amends to Licenses DPR-58 & DPR-74,per Request.Amends Make Changes to Administrative Controls ML17328A7331990-05-29029 May 1990 Forwards Nonproprietary WCAP-12577 & Proprietary WCAP-12576, Westinghouse Revised Thermal Design Procedure Instrument... Methodology for American Electric Power DC Cook Unit 2 Nuclear Power Station, Per 900419 Commitment ML17328A7321990-05-24024 May 1990 Responds to NRC Bulletin 90-001, Loss of Fill Oil in Transmitters Mfg by Rosemount. No Rosemount Model 1153 Series B or D or Model 1154 Transmitters Installed at Facility.Transmitters Purchased as commercial-grade Units ML17328A6991990-05-0909 May 1990 Provides Suppl to 900103 Response,Certifying That Fitness for Duty Program Implemented at Plant.Change Also Clarifies When More Stringent cut-off Levels Adopted at Plant Program Apply ML17328A7001990-05-0909 May 1990 Responds to NRC 900406 Ltr Re Inadequacies of Spds,Per Audit on 900221-22.Corrective Actions:Software Mod Will Prevent User from Accessing Displays Other than Iconic Displays from SPDS Dedicated Terminal ML17328A7071990-05-0707 May 1990 Forwards Monthly Operating Rept for Apr 1990 & Corrected Rept Mar 1990 for Donald C Cook Nuclear Plant Unit 1 ML17328A7031990-05-0707 May 1990 Forwards Monthly Operating Rept for Apr 1990 & Corrected Rept for Mar 1990 for DC Cook Nuclear Plant Unit 2 ML17328A6951990-04-30030 April 1990 Certifies That Training Programs for Initial Licensing & Requalification Training of Operators & Senior Operators at Plant Accredited by Inpo,Per Generic Ltr 87-07 ML17328A6861990-04-30030 April 1990 Forwards Annual Environ Operating Rept,Jan-Dec 1989, & DC Cook Nuclear Plant Units 1 & 2 Operational Radiological Environ Monitoring Program 1989 Rept Jan-Dec 1989. ML17328A6801990-04-23023 April 1990 Responds to NRC Bulletin 88-004, Potential Safety-Related Pump Loss. Study Planned to Evaluate Alternative Actions to Be Taken for Protecting RHR Pumps ML17328A6771990-04-23023 April 1990 Forwards DC Cook Nuclear Plant 1990 Annual Emergency Preparedness Exercise. Exercise Scope & Objectives & Detailed Scenario Documentation Encl ML17334B3641990-04-11011 April 1990 Responds to NRC 900301 Ltr Re Violations Noted in Insp Repts 50-315/89-31 & 50-316/89-31.Corrective Actions:Reliability Centered Maint Program Initiated ML17328A6601990-04-11011 April 1990 Forwards Updated QA Program Description for Cook Nuclear Plant, Incorporating Editorial,Organizational & Position Title Changes ML17328A6551990-04-0909 April 1990 Responds to NRC 900309 Ltr Re Violations Noted in Insp Rept 50-316/90-08.Corrective Actions:Procedure for Steam Generator Stop Valve Operability Test Revised to Require That MSIV Be Declared Inoperable After Failing Stroke Test ML17334B3601990-04-0606 April 1990 Forwards Revised Figures for Loss of Load Event Previously Submitted in Attachment 4,App B of Vantage 5 Reload Transition Safety Rept Supplied by Westinghouse in Jan 1990. Update Is Editorial in Nature ML17334B3621990-04-0606 April 1990 Forwards 1989 Annual Rept & Projected Cash Flow ML17328A6341990-03-30030 March 1990 Forwards Application for Renewal of Plant NPDES Permit,For Info,Per Section 3.2 of App B to Plant Tech Specs.W/O Encl ML17328A6331990-03-30030 March 1990 Responds to NUMARC 900104 Request for Addl Info Re Station Blackout Submittals.Target Reliability for Emergency Diesel Generator of 0.0975 Established for 4 H ac-independent Coping Category Will Be Maintained ML17328A6321990-03-30030 March 1990 Forwards Response to Generic Ltr 90-01, NRC Regulatory Impact Survey. Util Ack Recommendation by NUMARC ML17328A6221990-03-27027 March 1990 Responds to 900226 Ltr Transmitting Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $75,000. Corrective Actions:Flow Retention Circuitry Setpoints Set to Compensate for Missized Process Flow Orifice ML17328A6191990-03-27027 March 1990 Forwards Payment in Amount of $75,000 for Civil Penalty Imposed Through Notice of Violation Issued in Insp Rept 50-316/89-02 on 891016-20,24-26 & 1204.Response to Violation & Corrective Actions Provided in Separate Submittal ML17328A6161990-03-20020 March 1990 Responds to Generic Ltr 89-19 Re Safety Implications of Control Sys in LWRs (USI A-47).Both Units Have Steam Overfill Protection Sys That Would Automatically Prevent Water Carryover Into Steam Lines If Control Sys Failed ML17328A6121990-03-13013 March 1990 Forwards Monthly Performance Monitoring Rept,Jan 1990. ML17325B3901990-03-0606 March 1990 Forwards Annual Rept to NRC Per 10CFR50.54(W)(2) Re Nuclear Property Insurance ML17325B3921990-03-0606 March 1990 Modifies Application for Amend to License DPR-74 Re Cycle 8, Per 900228 Telcon ML17325B3781990-02-28028 February 1990 Forwards Response to NRC Info Notice 89-056 Re Questionable Certification of Matl Supplied to Dod by Nuclear Suppliers. Matl Capable of Performing Design Function & Acceptable for Continued Use ML17328A5971990-02-27027 February 1990 Withdraws 890203 Application for Amend to License DPR-74, Modifying Tech Spec Table 3.2-1 Re DNB Parameters to Express RCS Flow Rate on Volumetric Rather than Mass Basis ML17334B3511990-02-22022 February 1990 Submits Annual Rept of Changes to or Errors in Acceptable LOCA Evaluation Models or Application of Models for Plants. Wflash Analyses Will Be Superceded by Notrump Analyses for Unit 2,Cycle 8 Reload ML17328A5881990-02-21021 February 1990 Responds to NRC 890914 Request for Addl Info Re Safe Shutdown Methodology.App R Fire Barriers Being Maintained & Surveilled Under 3/4.7.10 for Units 1 & 2 ML17328A5861990-02-16016 February 1990 Provides Revised Comments in Response to NRR Comments During 891213 Telcon Re Allowable Stresses for Piping & Piping Supports 1990-09-21
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REGULATOP INFORMATION DISTRIBUTION TEM (RIDS)
P ACCESSION NBR:8411060158 DOC ~ DATE: 84/10/30 NOTARIZED; NO DOCKET FACIL'!50 "315 Donald C, Cook Nuclear Power Pl anti Unit 1i Indiana 8 05000315 50-316 Donald C, Cook Nuclear Power Pl anti Unit 2~ Indiana 8 05000316 AUTH INANE AUTHOR AFFILIATION ALEXICH,M,P~ Indiana 8 Michigan Electr ic Co, RECIP.NAME RECIPIENT AFFILIATION DENTONiHiRe Office of Nuclear Reactor Regulationi Director SUBJECT; Forwards Westinghouse evaluation of impact of reduced auxi liat y feedwater flow for Uni t 1 L results of reanalysis performed for Unit 2. Feedwater sys acceptable fot both units, DISTRIBUTION CODE: A001D COPIES RECEIVED :LTR ENCL SI E!
TITLE: OR Submittal: General Distribution NOTES: 05000315 OL! 10/25/74 05000316 OL:12/23/72 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAYiE LTTR ENCL NRR ORB 1 BC 01 7 7 INTERNAL: ADM/LFMB 1 0 ELD/HDS3 NRR/DE/MTEB 1 NRR/DL.DIR NRR/DL/ORAB 1 0 N
" ETB NRR/DSI/RAB 1 1 F 0$
RGN3 1 1 EXTERNAL: ACRS 09 6 6 LPDR 03 2 2 NRC PDR 02, 1 1 NSIC 05 1 1 NTIS 1 1 TOTAL NUMBER OF COPIES REQUIRED: LTTR 27 ENCL 24
e
<<4 IR H
IN DIANA 8 N ICHIGAN ELECTRIC CON PAN Y P.O. BOX 16631 COLUMBUS, OHIO 43216 October 30, 1984 AEP:NRC:0300H Donald C. Cook Nuclear Plant Unit Nos. 1 and 2 l Docket Nos. 50-315 and 50-316 @/
License Nos. DPR-58 and DPR-711 REVISED AUXILIARY FEEDMATER FLOM ANALYSES
~~@9 her. Harold R. Denton, Director ~o~oa 1ggyg Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission mc Mashington, D. C. 20555
Dear Hr. Denton:
Indiana 5 Michigan Electric Company (IldECo) letter No. AEP:NRC:0300C, dated November 3, 1980, provided information with regard to the flow design basis of the Donald C. Cook Nuclear Plant auxiliary feedwater system. It has recently been discovered, however, that an error was made in the input to the calculations supporting that earlier letter. The discrepancy has now been corrected, and the results of the revised flow calculations are expected to be transmitted to the NRC in the near future.
It is noted, however, that the revised calculations predict that for a feedwater line break in Unit 1 (for which the feedwater line break was not part of the original licensing basis), approximately 365 gallons per minute (gpm) of auxiliary feedwater flow could be delivered to the intact steam generators prior to operator action; the corresponding auxiliary feedwater flow value for Unit 2 is 375 gpm. Since these flow values are lower than those used in the Final Safety Analysis Report (FSAR) for Unit 2, we have contracted with Mestinghouse Electric Corporation (E) to perform a reanalysis of the feedwater line break accident. g's evaluation of the impact of reduced auxiliary feedwater flow for Unit 1, and the results of the reanalysis performed for Unit 2, are presented in the Attachment to this letter.
Based on the reanalysis performed for Unit 2 with the LOFTRAN computer code, g has concluded that the plant meets the FSAR acceptance criteria assuming the auxiliary feedwater system delivers 375 gpm to the intact steam generators. More specifically, the analysis indicates that the Reactor Coolant System (RCS) and main steam system will remain below 110$ of their respective design pressures, and that the RCS water level will not drop below the top of the core. Ther efore, core integrity would be maintained and the radiological consequences would be only a small fraction of the 10 CFR 100 guidelines.
84.1030
8+f1.pb01580>pppg15 pDR ADOGl pgR P
4 A
Mr. Harold R. Denton AEP:NRC:0300H The K evaluation performed for Unit 1 indicates that operator action (i.e.,
action 81) at ten (10) minutes following a postulated feedwater line break would restore heat removal capability. This heat removal capability would be provided via an incr ease in auxiliary feedwater flow to approximately 460 gpm, assuming the availability of control air to the emergency leakoff valves.
Operator actions taken in accordance with actions g1 and g2 of the g evaluation will ensure auxiliary feedwater flow well in excess of 060 gpm (approaching approximately 1200 gpm at the first safety valve setpoint). It is noted that although the feedwater line break is not part of the original Unit 1 licensing basis, the licensing basis does assume operator action at ten (10) minutes following a high energy line break for the purposes of maintaining containment integrity, With this action, g believes that the consequences of a Unit 1 feedwater line break would be bounded by the conclusions provided in the FSAR of plants similar to Cook Plant.
Additionally, it is noted that IMECo has taken the conservative step of temporarily reducing Cook Plant thermal power for both Units while the analysis and evaluation was being performed by W., The enclosed information from gl indicates that the licensing basis for Unit' was not exceeded and, for Unit 2, the public health and safety would not be endangered by a return to full power operation, based upon an assumed auxiliary feedwater flow of 375 gpm to the intact steam generators following a postulated feedwater line break. We expect to return Unit 2 to full power operation upon concurrence of the staff of the Office of Nuclear Reactor Regulation. We believe the attached evaluation Justifies the return of Unit 1 to full power operation.
This document has been prepared following Corporate procedures which incorporate a reasonable set of controls to ensure its accuracy and completeness prior to signature by the undersigned.
Very truly yours, P. Al xichg'U'ice President MPA/dam cc: John E. Dolan W. G. Smith, Jr. - Bridgman R. C. Callen G. Charnoff NRC Resident Inspector at Cook Plant - Bridgman G., Bruchmann
A
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F r 1
Mr. Harold R. Denton AEP: NRC:0300H bo: J. G. Feinstein/P. A. Barrett/H. Y. Fouad'/D. A. Medek H. N. Scherer, Jr.'.
J. Markowsky T. 0. Argenta S. H. Steinhar t/J. A. Kobyra R. N. Jurgensen J. B. Shinnock R. F. Kroeger T. P. Beilman - Bridgman J. F. Stietzel - Br idgman,, ,,
D. L. Migginton - NRC DC-N-6015. 1 DC-N-6110
T C SE C 0
(g
~
OCT.29 jj. 6 Srs id'usioaer
'84 18:88 ASTI WCWIRE RON AWS- 162 Refereree Ko(s) ..
P. 82 o
Qast<nohous>> Reference No(s).
{Change Control oe'Fg As Applicable) lKSTINNXSE INaZW SAFrrY EVALVATIN CHECX LIST
- 1) XUCaAR ~rr(S)
- 2) CRCK LIST APPLICAN.E TO-'t of Red d AFM Flow on thetfcal Feedl)ne Braik Trans]ent at D. G. Cook Unht
- 3) The ~tten safety evaluation of the reHsed procedure< design change or aodhfkcathon required by 10CFR50.59 has been prepared to the extent required and 3s attached. If a safety evaluation $ s not requIred or fs kncoeplate for any reason, explain on Page 2.
Para A and 8 of this Safety Evaluation Check 11st are to be caapleted only on the bashs of the safety evaluat(on perfonred.
Cmr. LIST - War A (3.1)
(3.2)
Yes Yes No Na
~
~
A change A
to the plant change to procedures as described <n the FSAR2 as described $ n the FSAR2 (3.3)
(3.4)
Yes Yes No No
~
~
A test or.experf~t tet described $ n ihe FQR?
A change to the plant'technical spec1flcathons (Appendix A to ihe Operating Uceme)2
- 4) CHKCX LIST - PART B (Justtffcat<on for Part B answers ~t be {ncluded on Page 2.)
=
(4.1) Yes No x H11 the probabflf+ of an accident prev)ously evaluated 3n the FSAR be fncreased2
'It 22 Y 2 ~tillthe ti wwNIUNc FSAR he fncreased2 H tt I ~i ly I t it (4.3) Yes % ~ Nay the possibility of an accident A5ch $ s different than any already evaluated $ n the FSAR be creatad2 (4.4) Yes No X All the probabllfty f a aalfunctlon of equipment $ aportant io safety ~ousb'valuated <n the FSAR be All the consequences of a ealfunctlon of equ<paent 1aportant
)ncreased3'4.5)
Yes Na X to safety preHously evaluated $ n the FSAR he fncreasad?
(4 6) Yes Na X +g the poss~b<14ty Df a salfLecMon of equ$ yaent <sportant to safety different than a~ already evaluated $ n the FSN be created2 (4.7) Yes No X N11 ttle mrgfn of safety as defined $ n the bases to any tedefcal specfficat<on he reduced2 Page 1 of 2
WMI RXN P. 83 OCT.29 '84 18si2 MCGUIRE If the and answtm to any of the above queat$
explain below.
ons are ~~, ~~~~t ~~) ~
If the area+ to any of the abve ~t<on<<n 4) camet b adam~ ]n Mttln safety haslcl Nl tion for 1$ c40$ 0 evalg4tgon> QQ sssfllh+nt sg~tt4ad to gg pggs~nt to le~ 90 W foll'gs~H>ls th 3Mstfffcatfon Mpon the ultan safe~ Ova]oat~on (l) for Liars given $ n Part 5 of the $ aga+ Evaluation C~ List See letter NS-RAT-PTA-84-111
)Raference to document(s) conta<n1ng rattan safety evaluat<o:
for/Description 4con Pave(s): Table(s): F~gMr (s):
mason of Change:
NOT APPLICABLE
~red
'oo&fnatecf hy (Nuclear Rth Safety):
Engineer (s):
bate: l~
Date: l0
~fnat<ng Croup Nenaeer(s): Date: /~ +2 vclear Safety 6roup Nanager: Date:
Paoe 2 nf 0
OCT.29 '$4 18:15 ASTI MCGUIRE RKN P.$ 4 NS-QKS-OPl-N-113 0-BhT-PTLSl-111 OCKBKR 27, 154 3); DoPo XNZNZZS L 8JDk RE: Impact of Reduced Ahf Flew on FeedlirM; Break Transient for D. C. Cook Unit 1.
~can Electric Powe'nfused Mesti~xese of an error in the &uxilia~
feecheater flat calculations for the feedlira break analysis of D. C, Cook Unit
- 2. Ttds error w&s faed to apply to both mits; however, Unit 1 does not have a feedlirN break analysis as part of its licensing basis and ezplicit csloulatices are not required. The fallming provides & safety evaluation of what action waQd be accessary to Mtigate the consequences of & hypothetical feecGim break at Unit 1i
?he D.C. Cook Unit 1 design basis for operator action fallcadng a high energy 1ire break is 10 mrinlrtes (of. AEP--). Thus credit for the operators to irritiate the appropriate actions at 10 aLnutes is justified.
Should a feedlire break occur at Unit 1 the reactor protection system would respond as fciLlcws:
?be reacta'c+id trip on a steaa generatcc'ow water level ooirNident with stea/feed water f1'ismatch a stae generator low-lac water level.
Hen the stean generator 1~lcm level is reached in aa stein general',
the aotor driven auxiliar7 feed pmps (NP) start. ?he worst single failure for a feecRim break is a failure of the NP which feeds two intact stean generators. FollarLng reaotcl'rip and subsequent turbine+ trip, the lcM lcm'ater level in a second stein generate would be reached and the turbim driven auxQiary feed paap (?DQVP) is starMd. Ls the steaa generators depressurize, the steea supyly to the ThLMP is reduced and eveatua11y la4. Thus caoe ice stean supply to the TMPMP is loot, cnly a ainiaal Ilant af auxQiar7 fee4rater fXar wculd be ave,able fa. heat pcRcv &1 a Operator &ation should be perfcmed to restore beat remcrval capability, i.e.
450 gpa to the intact stean generators, kraQ&ble operator actions are as fciLlms:
- 1. He oan Relate kFbl flee to the faulted SG and defeat the Q.car retention logio for the intact steaa generahx fed by the sane MDP. This results in orM, NP delivering 4R gpn to the intact stean gener&ter. This action is SiaQar tO actiOn required by other ylantS Sindlar tO D.C. COOk Unit 1 that here a feeQine br'eak analysis as part af their'esign basis.
- 2. He can restore stean supply to the TMRfP. This oan be eccccnplished ty closing the aein steaQ.inc isolatioe valve ce the faulted stean the NSIVs for the lires that connect to the TDQVP.
general'r
OCT.29 '84 18:i8 ASTI NVCWIRE RQN P. 85
</y Mith the asempt;ion of action 1 above et 10 minutes, Westinghouse believes the feedlfm break coreequenoes would be bounded by the eonolusions (RCS pressure less than 130S of the design pressure, core integrity maintained, and dose releases are a saall fractXea of the 10 CFR Part 100 guidalitss) provided in the FShR of plots s~iar to D. C. Cook stree the D. C. Cook hht syeten design assures iN flat to the intaot steaa generators price to the 10 alake operator aotion time. Thus provided operator action results in an adequate beat sink, Mestfn~e sees no safety issue regarding the reduced hN flex fcc' hypothetical feecQ.fre break.
Di S QXE Pl>et Trinsfent hnelysis Operating Plant AmQysis K. P. M855E, Manager P. A. , Ravager Pleat Transient kaQysis Operating Plmt inalysis
OCT.29 '84 i8:2Z ASTI ~IFK RXN P. 86 MS-RAT-P7h-Sl-112 FRN: NS PTh MIN 2%~5 DATF.l 0 tober 29 1884 KIBJECT: D, C. COOK UNIT 2 (AMP) FHUX INK BKAK REhRhLYSIS D. P.
4 Daafnicis P. Suda MHC ~
701- 25 CC: A. L. Sterdis Lofts NC ~
NC 0-09k P. A J. L. Little J. Parvtn NNC ~k Mesti~ouse Site Malaya D. S. Love MHC 0-09h D. C. Richardson HNC 0-15 Please find attached the report docmenting the feedline br eak reanalysis assuming ~5 gxn of auxiliary feeckater flex to the 3 intact stean generators fa D. C. Cook Unit 2. As sham in the attached, the FSAR acceptance criteria of no substantial overpressurization of the reaehcr coolant systan and the core readns covered are met, Sbould ycv have any questions the mdersigned may be contacted.
This expedited effcrt was charged to sbop order AKKP-485.
M. R Adler Hant Tmnsient kalysis Approved:
tl. P. Osborne, Hanager Plmt Transient kalysis
OCT.P3 '84 i8:25 &ST OJSE WCWIRE RON P. 87 OCT.29 '84 18:28 WST t&CWIRE RXN P. 83 The PBkR feedlira break analysis fcr D. C. Cook Unit 2 was perfumed assming
%0 gpn of auxiliary fee%ater (hFM) flat is delivered to the intact steer.
generators. The follcwing demonstrates that the plant meets the FBAR acceptance criteria (described on ~ge 14.2.8-2 of the FSAR) assuming the LN aystan delivers 375 gpm to the intact steai generators.
-This analysis was perfcrmed using the same methodology and assuagions as stated in the FShR with the foDcwing exceptions, The LOFTS computer code was used, Zhfs code simulates the g.ant thermal kinetics, reacta'oolant system (RCS) including natural circulation, pressurizer, steaa generators, and feechrater systen, and computes pertitant variables including the pressurizer pressure, pressurizer ~ater level, ard reactor coolant temper at<'re.
Reaotcr trip and auxiliary fee%ater initiation are assuaed to occur on l~lcac water level in the faulted stean gener ator.
The lnost restrictive singe failure ih the AN systaa is assLzoed. This is the loss of the motor driven aw&iary feeckater pmp that rem:.My wculd have supp'.iei.'. fee&ster to taro intact stean 'eterators in one a.inute faDcwing reactor trip. The other tIotcc driven auxiliary fee4tater puap and the turbid driven auxiliary fee&ater pmp deliver a total of 375 gxn to the three intact:tean generators witt.i>> one migrate follming the resets trip.. Ln additiorel 280 is assessed befcc e the feed liras are purged and the relatively coldseconds (1K F) auxiliary fee%ater enters the intact stean generators.
Figures 1-7 Qluatrate the key plant paraneters calculated follcwing a fmdline rupture. The calculated sequence of events are listed in Tah1e 1i Results presented in Figures 4 and 6 sheet that pressures in the RCS and main stean systen ramdn belcw 11(5 of the respective desig r.ra sure.. Fressuri~u pressure irerease util reactor trip ce i~lcm stean generator level.
Prmsure then decreases, due to the loss of heat input, LatD steailine isolation occurs on lcm'teaQine pressure in the faulted loop. Coolant expansion occurs due to reduced beat transfer capabGity in the steau 6enerators; the [~surizer ~ety valvule open to maintain primary coolant systan pressure at an acceptahle valw.
OCT.29 '84 i8:32 (ASTI ~RE NXN P. 89 Re reaata'ore ranains covered with water throughout the transient, as water relief due to themal ~asion is limited by the beat ranoval capability of 4e avxiliary frater ayatan.
Kx a~steec'uxiliary fee&ster flm rate is capable of reaovi~ all af the decay heat "3200 seconds after reactor tzf.p. After this ~, core decay heat 4wreases bales the auxiliary frater hes5 ranoval capacity and reactor ooolaat tan~ra~~es and pressure decrease, Results of the analysis axe that fcr the postulated feedlim rupture, the assigned auxQiary feeAater aystca~ capacity (375 gpn) ia adequate to r above
~'.ecay heat and to prevent the water 3 arel in the RCS from dropping to the top of the core, REFQKHCE 1: Bunatt, T.M.T,, et al., 4LOFQUN Code Deso<ption,"
VQP-7g07-k, LprQ, 19%.
TABLE 1: TQK SEVEN(X OF EVEh'IS EVERT TDK Feedline R~ture Occurs 10.0 Reactor trip on L~Lcv 15.4 stean generator water level Rod motion and power lost 17 4 to the reactor coolant pmps Auxiliary feehrater is de'ivered 75.4 to 3 intact stean generators Lm stem'ra pressure 149.4 setyoint reached Steanl ine isolation occurs 157.4 Pressurizer safety valve 612.0 setpoint reached Stean generator safety va've 700.0 setpoint reached ir intact stean generators reached Core decay heat decreases to 3200 aux'l iary feeOcater heat removal capacity
P. 18
'84 18:35 ASTI t&CWIRE FKXN OGT.P3 S,use 00Ã0 g
$ ,i(co N
i++> n~ 0 ~~
- " ~'e
~ ~ ~ ~
<@iNij N85$ g TOE Fl.N VERSUS TINE FIGURE 1: HAIR FEEDLINE RUPTURE ACCIDENT CORE HEAT
OCT.29 '84 i8:38 (ASTI WCWIRE NXN ii e 4Ã04 g
40
~ ~ ~ ~
0 gggQJ m gpss FIGURE 2: MAIN FEEDLINE RUPTURE ACCIDENT REACTOR COOLANT FLSt VERSUS TINE
~ 29 '84 i8 4Z '4ESTI NVCWIRE RCXN P. 0 f85~
QSOe 750 L00 I
ae 0 44~i a NsSig NASL ORO
'IGURE 3: NIN fEEOt.IHE RUPTURE ACCIDENT PRESSURIZER ltATER VOL!9K VERSUS TIKE
OCT.29 '84 i8:45 ASTI l&CWIRE RCKN P. 13 NN,O Q. O
~
~
w~~~ i$ggjg m@gg g$
FIGURE 4: HAIN FEEDLINE RUPTtif ACCIDENT PRESSURIZER PRESSURE VERSUS TIME
sat P ~
m.a 85 l0 HOT I~ ~N 8 St$ e N COLD UJ I gg}
RLN me 0% N sat, I~ NLm Tm ML Vl
%% N TCOLO MN 4 ec~lcg 5 MNg ~ jQ+
FIGURE S; MAIN FEES.IHE RUPTURE ACCIDENT FAULTED AND INTACT LOOPS RCS TEMPERATURES VERSUS TIHE
'84 18:52 ASTI t&CWIRE KXN P,15
~
- OCT.29 tNOi0 INTACT YEAH GENE RATORS i%i.N y
FAlKTED STEN GENERATOR
~ i 4~ NN5gfg me g~
aalu
~ ~ ~ ~ a FIGURE 6: HAIN FEED.INE RUPTURE ACCIQEHT STEAM GENERATOR PRESSURE VERSUS TI%
l&CWIfK
~.29 '84 i8:55 ASTI ROC'NTACT STPN GfHERATOR$
FAULTEQ STQg 'GEgEy LD FIGURE 2: MAIN FEEDLINE RUPTURE ACCIlKNT STEN GENERATOR NSS VERSVS 75%
Distribution CDocket fileiwo/encl.
ORB81 Rdg. wo/encl.
CParrish w/encl.
DWigginton w/encl..
October 25, 1984 DOCKET NO(S). 50-315 and 50-316 Mr John Dolan, Vice President Indiana and Michigan Electric Company c/o American Electric Power Serwlce CorporOihon 1 Mverside Plaza
SUBJECT:
Columbus, Ohio 43215 Co COOK NU(XZAR PLANT,
'ONALD UNITS 1 AND 2 The following documents concerning our review of the subject facility are transmitted for your information.
IC Cj Notice of Receipt of Application, dated D Draft/Final Environmental Statment, dated D Notice of Availability of Draft/Final Environmental Statement, dated CI Safety Evaluation Report, or Supplement No. , dated Cj Notice of Hearing on Application for Construction Permit, dated C3 Notice of Consideration of Issuance of Facility Operating License, dated C3 Monthly Notice; Applications and Amendments to Operating Licenses Involving no Significant Hazards Considerations, dated C3 Application and Safety Analysis Report, Volume CI Amendment No. to Application/SAR dated D Construction Permit No. CPPR- , Amendment No. dated O Facility Operating License No. , Amendment No. , dated.
CI Order Extending Construction Completion Date; dated EK Other (Specify/ Monthl Notice aoverin eriod -throu h October 24 1984 iration date for hearin re uests and comments Novdmber 26, 1984.
~ \
Division of Licensing Office of Nuclear Reactor Regulation
Enclosures:
As stated cc w/enclosure oui>cm> ORB/I 1:DL suRNA'ML~ CParrish/ s DATE+ 10/ /jI/84 NRC FORM 318 {1/84)'NRCM 0240
I