ML17319A748

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IE Insp Repts 50-315/80-21 & 50-316/80-17 on 801201-31. Noncompliance Noted:Two Containment Spray Sys Inoperable During Mode Changes & Automatic Feedwater Pump Trip on Low Suction Pressure Not Installed
ML17319A748
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 02/02/1981
From: Boyd D, Dubry N, Swanson E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17319A745 List:
References
50-315-80-21, 50-316-80-17, NUDOCS 8103120487
Download: ML17319A748 (11)


See also: IR 05000315/1980021

Text

'

U.S.

NUCLEAR REGULATORY COMMISSION

OFFICE

OF INSPECTION AND ENFORCEMENT

REGION III

Reports

No. 50-315/80-21;

50-316/80-17

Docket Nos. 50-315;

50-316

Licenses

No. DPR-58;

DPR-74

Iicensee:

American Electric Power Service Corporation

Indiana

and Michigan Power

Company

2 Broadway

New York, NY

10004

Facility Name:

D.

C.

Cook Nuclear Power Plant, Units

1 and

2

Inspection At:

D.

C.

Cook Site,

Bridgman,

MI

Inspection Conducted:

December

1-31,

1980

Inspectors:

E.

R.

Swanson

Approved By:

D.

C. Boyd, Chief,

Projects

Section

4

Ins ection

Summa

Ins ection on December

1-31

1980

(Re orts No. 50-315/80-21.

50-316/80-17)

Areas Ins ected:

Routine, onsite regular

and backshift inspection by the

resident inspector.

Areas inspected

included operational safety verification,

inspection during long term shutdown, surveillance observation,

maintenance

observations,

IE Bulletin and IE Circular followup, licensee

event report reviews,

plant trips,

and independent

inspection efforts.

The inspection involved

a total

of 178 inspector-hours

onsite by two NRC inspectors

including 49 inspector-hours

on the off-shifts.

Results:

Of the nine areas

inspected,

no items of noncompliance

or deviations

were identified in eight areas.

Two items of noncompliance

were identified in

two areas

(violation, level IV - exceeding

an action statement,

paragraph

8;

violation level VI - failure to meet commitment - paragraph

10d).

DETAILS

Persons

Contacted

R. Hunter, Vice President,

AEP

+D. Shaller, Plant Manager

  • B. Svensson,

Assistant Plant Manager

+E. Townley, Assistant Plant Manager

R. Keith, Operations

Superintendent

~E. Smarella,

Technical Superintendent

>R. Dudding, Maintenance

Superintendent

<J. Stietzel,

QA Supervisor

+D. Duncan,

CRI Supervisor

+D. Palmer, Radiation Protection Supervisor

. Kriesel, Environmental Supervisor

R. Jurgenson,

Assistant Vice President,

AEP

The inspectors

also conducted

a number of interviews with operators,

technicians,

and maintenance

personnel

during the inspection.

+Denotes

those present at the exit interview.

0 erational Safet

Verification

The inspector

observed control room operations,

reviewed selected

logs and

records to identify significant changes

and trends; to assure

required entries

were being made;

to verify operating

memos

and instructions

conform to Tech-

nical Specifications;

to check correctness

of communications

about equipment

operational status;

and to verify conformance to limiting conditions for

operation during the month of December

1980.

The inspector also conducted

discussions

about selected

annunciators

with the control room operators

and

supervision to assure

they were knowledgeable

of plant conditions

and that

corrective action, if required,

was being taken.

Tours of the Unit 2 reactor

compartment

(lower level), the auxilary building, and turbine buildings were

conducted

to observe plant equipment conditions, including potential fire

hazards, fluid leaks,

and excessive vibrations

and to verify that maintenance

requests

had been initiated for equipment in need of maintenance.

The in-

spector by tours of the montoring stations,

observations,

and direct interview

verified that the physical security plan was being implemented in accordance

with the station security plan.

The inspector

observed plant housekeeping/cleanliness

conditions

and verified

implementation of radiation protection controls.

During the month of December

1980, the inspector walked down the accessible

portions of the Unit 1 high

head

and boron injection portion of the

CVCS which is part of the ESF systems

to verify operability.

These

reviews

and observations

were conducted to

verify that facility operations

were in conformance with the requirements

established

under technical specifications,

10 CFR,

and administrative pro-

cedures.

Ins ection Durin

Lon

Term Shutdown

The inspector

observed

the continued

shutdown control room operations

of

Unit 2, reviewed applicable

logs and conducted

discussions

with operators

and others during early December

1980.

The inspectors

checked

the oper-

ability of selected

emergency

systems

and verified proper return to service

of affected

components.

The inspectors

observed portions of the mutliple

restarts

of Unit 2.

The inspectors

also observed

the shutdown operations

of Unit

1 in late

December

1980.

Monthl

Surveillance Observation

The inspector

observed technical specifications

required surveillance testing

on the Pressurized

Pressure

Protection Set II (2 THP 4030

STP 112)

and

Steam

Generator

Water Level Protection Set III (2 THP 4030

STP 117)

and verified

that testing

was performed in accordance

with adequate

procedures,

that test

instrumentation

was calibrated,

that limiting conditions for operation

were

met, that removal

and restoration of the affected

components

were accomplished,

that test results

conformed with.technical specifications

and procedure re-

quirements

and were reviewed by personnel other than the individual directing

the test,

and that any deficiencies identified during the testing were pro-

perly reviewed

and resolved by appropriate

management

personnel.

The inspector also witnessed portions of the following test activities:

Procedure

No.

2 THP 4030

STP

104

Title

Overtemperture

and Overpower Protection

Set I.

2 THP 4030

STP

118

Steam Generator

Water Ievel Protection

Set IV.

12 THP 6030

IMP 142

Cardox System Surveillance.

Monthl

Maintenance

Observation

Station maintenance activities of safety related

systems

and

components

listed below were observed/reviewed

to ascertain that they were conducted

in accordance

with approved procedures,

regulatory guides

and industry codes

or standards

and in conformance with technical specifications.

The following items were considered

during this review:

the limiting condi-

tions for operation were met while components

or systems

were removed from

service;

approvals

were obtained prior to initiating the work; activities

were accomplished

using approved procedures

and were inspected

as applicable;

functional testing and/or calibrations

were performed prior to returning

com-

" 3-

'

ponents or systems

to service; quality control records

were maintained;

act-

ivities were accomplished

by qualified personnel;

parts

and materials

used

were properly certified; radiological controls were implemented;

and, fire

prevention controls were implemented.

Work requests

were reviewed to determine status of outstanding jobs

and to

assure that priority is assigned

to safety related

equipment maintenance

which

may.affect

system performance.

The following maintenance activities were observed/reviewed:

Procedure

No.

Title

2 THP 6030

IMP 229

12

MHP 4050 FDF 001

Source

Range NI Calibration on N-32.

Receipt,

Storage,

and Preliminary

Inspection of New Fuel Assembly

Shipping Container.

6.

IE Bulletin Followu

For the IE Bulletins listed below the inspector verified that the written

response

was within the time period stated in the bulletin, that the written

response

included the information required to be reported, that the written

response

included adequate

corrective action commitments

based

on information

presentation

in the bulletin and the licensee's

response,

that licensee

manage-

ment forwarded copies of the written response

to the appropriate onsite

manage-

ment representatives,

that information discussed

in the licensee's

written

response

was accurate,

and that corrective action taken by the licensee

was

as described in the written response.

IEB No.

Title

80-21

Valve Yokes Supplied by Malcolm

Foundry Company, Inc.

80"23

Failures of Solenoid Valves Manu-

factured by Valcor Engineering

Corp.

The inspectors

are still following the licensee's

re-evaluation of IEB 79-21

"Temperature Effects on Level Measurements".

7.

IE Circular Followu

For the IE Circulars listed below, the inspector verified that the Circular

was received by the licensee

management,

that

a review for applicability was

performed,

and that if the circular were applicable to the facility, appropri-

ate corrective actions

were taken or were scheduled

to be taken.

IEC No.

Title

79-17

Contact Problem in SB-12 Switches

on G.E. Metalclad Ckt B.

80-23

Potential Defects in Beloit Emergency

Diesels.

Also, IE Circular 79-05, "Moisture Leakage in Stranded

Wire Conductors,"

has been closed out. It was noted that there

have been similar occurrences

when water leaked through

a conduit and contaminated

the turbine building

sub-basement

in July 1980.

8.

Licensee Event Re orts Followu

Through direct observations,

discussions

with licensee personnel,

and review

of records,

the following event reports

were reviewed to determine that

reportability requirements

were fulfilled, immediate corrective action was

accomplished,

and corrective action to prevent recurrence

had been

accomp-

lished in accordance

with technical specifications.

Unit

1

Unit 2

80-20/03L-0

79-26(Sup)/03x-1

80-25/03L-0

80-27/03L-0

LER 80"033/01-T-0

(Unit 2)

During preparations

for changing operational

modes

on December

4,

1980

Surveillance Test ~02-OHP 4030 STP.007

was performed

on the containment

spray

(CTS) system.

This required valve aligments including closure of

CTS-124E

and

CTS-128E

on the discharge

of the East

CTS Heat Exchanger.

These valves were found to be closed during a tour of the Auxiliary

Equipment Operator

on December

14,

1980.

The two valves

were opened re-

storing operability by 0700 on the 14th.

Investigation revealed

these valves

had been shut on December 4,

1980 at

about

1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> to perform the surveillance test

on East

CTS Pump.

The

valves are shut to prevent inadvertent

spray to the containment while test-

ing the pump.

After pump testing

was complete,

an Auxiliary Equipment

Operator

was assigned

to restore

the flow path to normal.

CTS-124E

and

CTS-128E are required to be locked and sealed

open in the flow path.

The

Auxiliary Equipment Operator locked and sealed

CTS-124E

and

CTS-128E in

the shut position, but initialled the Checkoff Sheet

as having locked and

sealed

the two valves in the open position.

Numerous

mode

changes

(9) were made during the period of December

4-14 each

of which constitutes

a violation of Technical Specification (T.S.)

3 '

'

which requires

the system to be operable prior to entering the next higher

mode.

Also, exceeded

was the T.S. 3.6.2.1 which allows one of the two CTS

headers

to be inoperable for 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> before taking specified actions.

This

is an item of noncompliance violation category IV as specified in Appendix A.

The inspector

reviewed the licensee's

corrective actions

and determined

them

to be adequate

to prevent further recurrence.

Additionally, Plant Manager Instruction,

PMI-2110, had been revised

by tem-

porary sheet

on December 9,

1980 to require independent verification of

restoration of valve lineups

on all ECCS equipment prior to declaring oper-

able after maintenance

or surveillance testing.

Had this been in effect

1/

on December 4,

1980, this event would have been

much less likely to occur.

Following the plant trips on December

14,

1980 due to a malfunction in the

Unit 2 main generator pilot exciter the inspector ascertained

the status of

the reactor

and safety systems

by observation of control room indicators

and

discussions

with licensee

personnel

concerning plant parameters,

emergency

system status

and reactor coolant chemistry.

The inspector verified the

establishment

of proper communications

and reviewed the corrective actions

taken by the licensee.

All systems

responded

as expected,

and the plant was returned to operation

on December

16,

1980.

10.

Inde endent Ins ection

(a)

Bomb Threat:

A bomb threat

was received by the licensee via

a telephone.

The inspector

observed

the licensee's

implementation of their security

plan which included notification of local law enforcement

agencies,

coordination of plant wide search,

communications

during the event,

and

decision making.

The threat

was determined to be

a hoax, no bomb was

found.

t)

1980 of the Unit, 2 Residual Heat Removal System

Check Valves:

RH-133,

RH-134, SI-170 L2, SI-170 L3.

The procedure

used

(12-THP-SP.003)

was

reviewed with it's temporary

changes

TP-1 and TP-2.

The inspector

verified that calibrated

equipment

was used in performing the test.

An effort was not made to quantify isolation valve leakage

since the

initial test met the acceptance

criterion of~ 5

GPM total leakage.

The test

was performed at

a primary system pressure

of 400 psig.

The

results

were

as follows:

1/

A managment

enforcement

meeting

was held in the Region III offices on

January

13,

1981 to discuss this event.

Details of this meeting will be

discussed

in a seperate

report.

Valve

Desired

Actual

Rh-122 6 RH 134

SI-170 L2

SI"170 L3

All 4

2

GPM

1

GPM

1

GPM

5

GPM

.10 observable

2.02

gpm

1.12

gpm

3.24

gpm

Steam Generator

Tube Wear:

On November 4, 1980, the Resident Inspector

was notified of visible damage to several

inner-row tubes in a Unit 2

steam generator.

Eddy current testing

was in progress

to detect

a minor

tube leak on this steam generator,

and when the secondary

side hand

holes were opened

the tube lane blocking device

was found loose.

Four

tubes

were found to have 50$ wastage

and 'one tube with 20'j wastage.

These

were adjacent to the tube lane blocking devices

which had

apparently

been moving due to the flow.

Subsequent

checks of the

Unit 1 steam generators

in late December revealed similar wear in two

steam generators.

The blocking devices

were found properly secured

indicating they had been loose during a previous operating period.

All tubes with significant wear were plugged

and the procedure

revised

to pervent further recurrence.

Salem Unit 1 has experienced

similar wear in three of four steam

generators

and

as

a result plugged all of the tubes adjacent to the

tube lane blocking devices.

A draft IE Circular was submitted

on

this subject.

Auxiliar

Feedwater

S stems:

As tasked by the Safety Evaluation Report

related to Amendment

42 to Iicense

No. DPR-58 and Amendment

24 to

License

No. DPR-74, the inspector

reviewed various procedures

and modi-

fications affecting the Auxiliary Feedwater

System

as discussed

below:

Recommendation

GS-4:

Procedure

OHP-4022.055.003

is the abnormal

operating procedure titled "Loss of Condensate

to Auxiliary Feedwater

Pumps".

The inspector

'determined that it adequately

delineates

the

coordination

and actions required to align Essential

Service Water

to supply the three Auxiliary Feedwater

Pumps.

Recommendation

GS-5:

OAP-4023.001.007

including Temporary Sheet

No.

1

was found to specify actions

necessary

for manual initiation of the

Turbine Driven Auxiliary Feedwater

Pump

(TDAFP).

The inspector also

found that emergency lighting was installed in the

TDAFP rooms

and

that emergency

radios are available in the Shift Operating Engineer's

office for use during AC power loss.

Recommendation

GS-6:

Verification of valve alignment after testing

and

maintenance

is required by Temporary Sheet

No.

8 to OHP-4030.

STP.017

dated August 4, 1980.

OHP-4021.001.002

"Plant Startup from Hot Standby

to Minimum Load" was reviewed

and it was found that the procedure

did

not call for operating all auxiliary feedwater

pumps.

During the

-

7 "

Unit 2 startup

on December

7,

1980 the

TSAFP was not used to provide

water to any steam genertors,

though it was otherwise

demonstrated

operable

by the surveillance test.

When the disparity between the

licensee's

December ll, 1979 letter and current operating procedures

was pointed out to the licensee

a Temporary Sheet

was added to the

procedure requiring the flow verification described in recommendation

GS-6.

Recommendation

GL-4:

The licensee's

December

11,

1979 letter

(AEP:NRC:

trip on low suction pressure

which will alarm in the control room. It

states

that "This modification will be made by January

1, 1981."

The

associated

design

change

RFC-12-2460

has not been completed

as scheduled.

As a result of these

discussions

the licensee

issued

a letter,

dated

January

27,

1981, to H. Denton, indicating their intention to complete

this modification by April 30,

1981.

This is

a deviation from a commitment and is

a severity level VI

vidation as stated in Appendix A.

16.

Exit Interview

The inspector

met with licensee

representatives

(denoted in Paragraph

1)

throughout the month of December

1980 and summarized

the scope

and findings

of the inspection activities.