ML17318A268

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Monthly Operating Rept for Aug 1979
ML17318A268
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 09/05/1979
From: Gillett W
INDIANA MICHIGAN POWER CO.
To:
Shared Package
ML17318A267 List:
References
NUDOCS 7909200331
Download: ML17318A268 (10)


Text

AVERAGE DA(LYUN17 POb=R L:-VEL DOCK:-7 ~O.

50-316 9-5-79 CPMPLE~~D 8Y

.W.T. Gillett

~HOqrE '16 465 5901 gOgTH Au ust 1979 DAY AVERAG DAlLYPOWER LEVEL (MWe iiet) 1042 DAY AVERAGEDAlLYPOWER LEVEL (MWe.'ic! )

1043 17 1047 10 13 15 15 1021 1028 1029 1028 1017 1012 1023 1028 1057 1067 1040 1047 1050 1046 19 24

'l5

'75 ZS 30 31 1043 1044 1044 1044 1034 1040 1038 1034 1028 1033 1040 1039 1037 1857RUC iiOYS

'+i~:Qt...'2(. 5'. - '-'vc:"-2. ="-L'~'-'"!l-o<<'-: '-"-": ~ " '~-".~c'aaf..:2v I.. '..".:

"..',",":..s)qlh. Ci)<~ u:

tg (i):77 )

OPERATING DATAREPORT DOCKET aiO. ~16 Date ~>-

COMPLETED BY 3M~22att 616-465-5901 OPERATING STATUS I. Umc Name:

Donald C. Cook 2

3 L!censed Thermal Power (bOVt)z

4. Nameplate Rang (Gross MWe):
5. Design Electric R"ting (Nec ilOVe):
6. >faximum Dependable Capacity (Gross iIYie)t
7. Maximum Dependable Capacity (Nec MNe):

3391 1133 1100 1118 1082 Notes S. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:

9. Power Level To Mich Restricted, IfAny (Net M)Ve):
10. Reasons For Restrictions, IfAny!
11. Hours In Reporting Penod IZ. Number OfHours Reactor Was C.":tical
13. Re ctor Resezve Shutdown Houa
14. Hours Genezator On-Line
15. Unir Reserve Snutdown Houzs
16. Gross Thermal Energy Genemted Pf'AH)
17. Gross ElecuicJI Energy Genezaced ('I>YH)
18. ifec Electricai Ene~ Generated (ilDVH)
19. Unit.Serac Factor ZO. Urit Avaihbilicy Factor "I. Un!t Capacity Factor (Using MDC Net)

ZZ. Unit Caoacity Factor (Using DER Net)

~D. Unit Forced Outage Rate Z4. Shutdowns Scheduled Over Next 6 iMonths This Month 744 744 0

744 0

2,513,690 771 92 100 100 95.9 94.3 0

Yr.-to-Date 5 831 4,695.3 4,626.0 0

15 330 201 4 957 240 79.3 79.3 75.8 74.6 20.6 iType. Date. and Du:ation of Each):

CumuL!tive 14 591 9 926.0 0

9 353.6 28 435,308 8,942,770 8,598,988

78. 4
71. 3
70. 1 15.3 S. lfShut Dov'n At cnd Of Report Period. Estimated Date of Startup:

ZS. Units ln Test Status (Poor to Commercial Operation):

Force" st Achieved lNlTIALCRlTICALITY lNITlAL ELECTRICITY CO.'lMERCIALOPERATION

("F77)

VNiTSllUTDOWNS AND POWER REl)UCTlONS REPORT hlONfll DOCKET NO.

l*

A.

N)l.

Date P)

IAr)J I) 0 g C

~ V)

Licenscc Event.

Rcport 4

~I/l o ~U k g 0

Cansc & Correct ivc Action to Prcvcnt Rccllrfcncc There were no unit shutdowns or power reductions.

The unit operated at essentially 1005 reactor power for the ett (re month.

l': Forced S: Scllcdldcll l9/77)

Reason:

A.E<ioipmcnl Failorc (Explain) 0-hlaintcnl)ncc or Test C.Rcfocli>>g D Rcgnlaloly Restrict)on li.Operator Training & Uccnsc Exan)inaiion F-Admi>>istrativc G.Operational Error (Explain) ll.Other (Exi)lain) 3 Method:

I -Mannal 2.hiannal Scraln.

3.Antolnat lc Scrllnl.

4.01 ilcl'Exi)lain) 4 Exllibit C - Inst rnctions for Preparation of Data l;ntry Sl)ccls for Liccnscc rvc>>t Rcpor<<LER) Flic iNuREC-Oi6I)

'Lxhibit I - Sanlc Son)'cc

Docket No.:

Unit Name:

Completed By:

Telephone:

Date:

Page:

50-316 D.

C.

Cook Unit 5'2 R.

S.

Lease (616) 465-5901 September 6,

1979 1 of2 MONTHLY OPERATING EXPERIENCES.-- AUGUST, 1979 Hi hli hts The Unit operated at 100% power the entire month except as noted in the summary.

Total electrical generation for the month was 799,950 Nwh.

I

~Summa r 08/03/79 -- Loop 1 Overtemperature and Overpressure 6 T Protec-tion was placed in the "trip" mode due to a low flow alarm on Loop 81 RTD Bypass.

Trouble was located in the alarm rather than low flow.

The alarm was repaired and the instrumentation was removed from the "trip" mode.

Total time in trip mode was 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />.

The North half of "B" Condenser was out of service for a 9.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period for checking of tube leaks.

No leaks were located.

08/05/79 -- Control Rods became inoperable in the "Automatic" mode due to an urgent failure alarm.

The rods were still capable of being driven manually.

Repairs were made and the automatic feature became operable 8/6/79.

08/06/79 -- The South half of "C" Condenser was out of service for a 3.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period for checking of tube leaks.

No leaks were located.

08/07/79 -- The South half of "C" Condenser was out of service for an 8.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period for checking of tube leaks.

No leaks were located.

The North half of "C" Condenser was out of service for a 1.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period for checking of tube leaks.

No leaks were located.

The k'1 seal leakoff flow to Reactor, Coolant Pump 823 has been fluctuating since the last unit start-up.

This flow varied from a low of 1

gpm to as high as

~%I'

Docket No.:

Unit Name:

Completed By:

Telephone:

Date:

Page:

50-316 D. C.

Cook Unit P2 R.,S.

Lease (616}

465-5901 September 6,

1979 2of2 08/07/79 (Cont'd) 08/08/79 5.5 gpm.

The flow went to full 'scale on the recording chart (6 gpm).

The flowmeter was bypassed reducing indicated flow to 3 gpm.

Since then the indicated flow has varied from a high of 3.'43gpm to a low of 2.7 gpm.with an estimated 3

gpm through the bypass.

This leakoff flow is being carefully observed.,

The South half of "B" Condenser was out of service for a

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> period for a leak test.

The North half of "B" Condenser was out of service for a

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> period for a leak test.

The South half of "A" Condenser was out of service for a

9 hour1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> period for checking of tube leaks.

No leaks were located.

08/13/79 08/20/79 The North half of "B" Condenser was out of service for a

7 hour8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> period to plug leaking tubes.

The North half of "A" Condenser was out of service for 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> to plug leaking tubes.

The low level alarm 5'23 RCP motor upper oil reservoir annunciated.

The oil level in the sight glass of this reservoir is being monitored by closed circuit tele-vision and the bearing"temperatures are being trended on the computer.

08/23/79--

08/24/79 08/27/79 08/28/79 The North half of "A" Condenser was out of service for a 5.75 hour8.680556e-4 days <br />0.0208 hours <br />1.240079e-4 weeks <br />2.85375e-5 months <br /> period for plugging of tube leaks.

Generator loading suddenly dropped"and recovered(

"approximately,250 Mw while testing >>Turbine valves.

~ The "C" Main Stop and Control,Valve was being tested.

The test sequence is for the control valve to close first and then the stop valve.

As the control valve started to close, the stop valve immediately closed causing the load spike.

The test circuit for this set of valves was thoroughly checked but no problem was found.

A subsequent test of these valves on 8/25/79 was normal.

The North half of "A" Condenser was out of service for a 5.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, period for plugging of tube leaks.

The North half of "C" Condenser was out of service for a 6.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period for checking of tube leaks.

No leaks were located.

4, Pl,>>,

)l

DOCKET NO.

UNIT NAME DATE COMPLETED BY TELEPHONE 50-316 D.

C.

Cook Unit No.

2 9-14-79 B. A. Svensson 616 465-5901 MAJOR SAFETY-RELATED MAINTENANCE AUGUST, 1979 2E essential service water pump discharge strainer misaligned.

Backwash valve retainer nut tightened and staked.

Operation is satisfactory.

No.

1 steam generator blowdown containment isolation valve, DCR-310 closed for no apparent reason.

A hole was discovered in the diaphragm of the valve operator.

Replaced the diaphragm and had valve retested.

HARV-422, primary water to the boric acid blender, failed closed.

A capacitor in the controller failed and was replaced with a spare capacitor.

The controller calibration was performed and operationally tested.

The loop ¹1 RTD Bypass Return Flow Low Alarm was received in the control room.

The associated bistables were placed into the trip mode during the investigation of the problem.

A ground condition was identified in the pull box located near the indica-ting alarm switch NFA-210.

The ground was cleared and the bistables returned to normal.

The Fire Protection actuation alarm on 2 HV-AES-1 was received in the control room.

Water was found in the manual actuation switch box.

The switch box was dried and a small drain hole in the bottom of the box was added to prevent future water accumulations.

The source of the water could not be determined.

The limit switch on the main turbine control valve A was indicating arcing of the contacts.

The burned contacts were replaced and the switch operation verified.

Main Turbine Stop Valve A would not operate during weekly surveillance testing.

After repairing a broken wire in the limit switch the valve was tested satisfactorily.

Pressure channels 1 and 2 of loop 2 steam generators differed by 30 psi.

Pressure channels 1 and 4 of loop 4 steam generator differed by 30 psi.

In both cases, the 28 psi differential notification limit was exceeded.

Outputs of all loop 2 transmitters were checked and were found to be within 15 psi.

Indicators were then calibrated.

Outputs of all loop 4 transmitters were checked and were found to be within 7 psi.

Channel 1 indicator and cu'rrent repeater were calibrated.

I 4