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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17335A5201999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp Unit 1.With 990208 Ltr ML17335A5191999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Dccnp,Unit 2.With 990208 Ltr ML17335A4831998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 2.With 990108 Ltr ML17335A4841998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for DC Cook Nuclear Plant,Unit 1.With 990108 Ltr ML17335A3951998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 2.With 981207 Ltr ML17335A3941998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for DC Cook Nuclear Plant,Unit 1.With 981207 Ltr ML17335A3331998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Plant,Unit 1.With 981105 Ltr ML17335A3381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for DC Cook Nuclear Power,Unit 2.With 981105 Ltr ML17335A2931998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 2.With 981005 Ltr ML17335A2941998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for DC Cook Nuclear Plant,Unit 1.With 981005 Ltr ML17335A2131998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 2.W/980903 Ltr ML17335A2151998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for DC Cook Nuclear Plant,Unit 1.W/980903 Ltr ML17335A1741998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 2.W/980806 Ltr ML17335A1731998-07-31031 July 1998 Monthly Operating Rept for July 1998 for DC Cook Nuclear Plant Unit 1.W/980806 Ltr ML17334B8171998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Plant Unit 2.W/980706 Ltr ML17334B8131998-06-30030 June 1998 Monthly Operating Rept for June 1998 for DC Cook Nuclear Station,Unit 1.W/980706 Ltr ML17334A7511998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 2.W/980609 ML17334A7521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for DC Cook Nuclear Plant,Unit 1.W/980609 Ltr ML17334B7921998-04-30030 April 1998 Addendum to Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Station,Unit 2 ML17334B7721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for DC Cook Nuclear Plant,Unit 1.W/980506 Ltr ML17334B7911998-03-31031 March 1998 Addendum to Monthly Operating Rept for Mar 1998 for DC Cook Nuclear Plant,Unit 2 ML17334B7171998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980407 Ltr ML17334B7181998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980407 Ltr ML17334A6831998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 2.W/980309 Ltr ML17334A6811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Donald C Cook Nuclear Plant,Unit 1.W/980309 Ltr ML17334B7901998-02-28028 February 1998 Addendum to Monthly Operating Rept for Feb 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6481998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2.W/980209 Ltr ML17334B7891998-01-31031 January 1998 Addendum to Monthly Operating Rept for Jan 1998 for DC Cook Nuclear Plant,Unit 2 ML17334A6051997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 2 ML17334A6021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Donald C Cook Nuclear Plant,Unit 1.W/980108 Ltr ML17334B6711997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 2.W/971208 Ltr ML17334A6061997-11-30030 November 1997 Revised Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Station,Unit 2 ML17334B6651997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for DC Cook Nuclear Plant,Unit 1.W/971208 Ltr ML17333B1421997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Donald C Cook Nuclear Plant,Unit 1.W/971110 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
[Table view] |
Text
AVERAGE DAILYL; (17 POWER Led%.
DOC~Y~O. '0-315 DAM D ~ 3-1-79
~M..::666 Februar 1979 I
DAY A~AGE DAILYPOWER LEYEL DAY AVERAGE DAILYPOWWOW. LEYEL (MWe Net) (MWe.%et) 1041 1039 1045 1033 3
878 19 101 4 1044
'1039 31 1043 312 1042 679 1040 1041 1041 1035 1041 10 1035 1041 1046 1046 1047 13 1044 Og 1045 30 IS 1044 31 1044 IiMSTRU~~OH S Qn .!;is;orr-at. !is: " averav ='a!iy "n:t tttv r! t:e!;n! le se! d'or each "'av in t'nc r nvr.:na:nttntn. C.nnot;lc le'ne nea6 S'6 tt'nOIC .66 .an't'art.
V9032 i oofy
I I ~
OPERATING DATA REPORT 50 315 DOCKET NO.
DATE ~29
~~1 ett COMPLETED BY TELEPHONE ~~901 .
STATUS 'PERATING Donal d C. Cook 1 Notes Qnif Nam
- 2. Reporting Period: Februar
- 3. Licensed Thetmal Power (MWt)t 4.. Nameplate Rating, (Gross MNe)t 1 089 S. Design EIectti& Ratmg (Net MNe): 1,054 1 080
- 6. Maximum Dependable Capacity (Gross MSe):
- 7. Maximum De p mdabie Ca p acity (Net 5OVe) t 1 044 S. If Changes Occur in Capacity Ratings (Items Number S Through 7) Since Last R port. Give Reasons:
9
- 9. Power Level To Mich Restr~ed, If"Any Piit hWe)t IO. Reasons For Resuictions, IfAny:-
This Month Yr.ao-Date Cumuiative I I. Hours In Reporting Period 672 36,480.0
- 12. Number Of Hours Reactor Was Critical 655.2 1399. 2 IS. Re ctor Reserve Shutdown Bout 0 0 463
- 14. Hours Genemtor On~ 652. 8 1396.8 27 810.1
- 15. Unit Reserve Shutdown Houts 0 0 9, 1
. 9. 91 551 75 728 764 I7. Gross Electrics Enemy Generated {M>YH) 9
~4459 669 231 23 743 404
- 19. Unit Serac Factor 1.. 79. 2 ZO. Uric Availability Factor 91. 1 98.6 79. 2 "1. Unit C pacig .actor(Using MDCNet) 95. 1
- 22. Unit. Capacity Factor (Using DER Net) 94. 2 63. 7
~~". L'nit Forced Outage Rate 1.4 5.9
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date, and Duration of Each):
'5. If Shut Down *t End Of Report Period. Estimated Date of Startup:
- 5. Units In Test Status I Prior to Commercial Operation): Forecast Achieved INITIALCRITICALITY INITIALELECTRICITY CONDIERCIAL OPERATION (i)l77 )
I a IT IIV DO VNS N POI ER (ED ON DOCKET NO.
UNIT NAME D 'TE 50-315 D.C.Coo - ~
COMPLETED Y B. verls son hl ONTIIFeb ua y, 19 a TELEPI IO E 6!I6 469-590 fPa a
rI Q c Q ~
Llcco sec nl c~ Cause k, Corrcctlvc 0CnsEl p 0 p p Q1 l)alc an rj Eveot
~
an Q AcliIot lo U~ c Report ¹ oI'6 E~
p Prevent Rccurrcocc
~ Vs CJ CL 144 790203 4 N/A ZZ ZZZZZZ Reactor power reduced to 705 to per-form N. I.S. incore/excore cross cal-ibration. Power returned to 1005 780204.
145 790206 19.2 H 1 79-006/03L-0 ZZ ZZZZZZ: During a "feed and bleed" operation on the pressurizer relief tank a failure occurred of the pressurizer r'elief tank rupture disc. The pres-sure surge caused all ice condenser inlet doors to indicate open. The Unit was removed from service to permit closing the ice condenser inlet doors and replace the rupture discs. The Unit was returned to sei'.vice 790207 and loaded to 100%
the same day.
I I': Fore 0 Reason: hlctltod: Exhibit C - Instntctions S: SCIICIIoleII A.EIiuipment Failure (Explai>>) I Manual RIr Preparation ol Data II-hlalnlcnancc or Test 2 h(annal Scratn. Lolry Sheets for Licensee C.Rcfuellog 3-Aulootatic Scrato. Event Rcport (LI!RIFile (NIIRI G.
D Regulator)'(cslriclloo 4.01IIcr (Explain) 0l 6l )
E-Operator Training 8I Lice>>sc Examination F-Administrative 5 G Operational Error (Explainl 'Exhibit I - Sante Source I I.OIIIcr (Explain)
INSTRUCTIONS This report should describe all plant shutdowns during the in accordance with the table appearing on the report form.
report period. In addition. it should be the source of explan- Ifcategory 4 must be used, supply brief comments.
ation of significant dips in average power levels. Each signi-ficant reduction in power level (greater than 20% reduction LICENSEE EVENT REPORT . Reference the applicable in average daily power level for the preceding 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />) reportable occurrence pertaining to the outage or power should be noted, even though the unit may not have been reduction. Enter the first four paris (event year. sequential shut down completelyl. For such reductions in power level, report number, occurrence code and rapport type) of the five the duration should be listed as zero, the method of reduction part designation as described in Item 17 of Instructions for should be listed as 4 (Other), and the Cause and Correcuve Preparation of Data Entry Sheets for Licensee Event Report Action to Prevent Recurrence column should explain. The (LER) File (NUREG4161). This information may not be Cause and Corrective Action to Prevent Recurrence column immediately evident for all such shutdowns, of course, since should be used to provide any needed explanation to fully further investigation may be required to ascertain whether or describe the circumstances of the outage or power reduction. not a reportable occurrence was involved.) If the outage or power reduction will not result in a reportable occurrence.
NUMBER. This column should indicate the sequential num. the positive indication of this lack of correlation should be ber assigned to each shutdovm or significant reductionin power noted as not applicable (>>I/A).
for that calendar year. When a shutdown or significant power SYSTEM CODE. The system in which the outage or power reduction begins in one report period and ends in another.
an entry should be made for both report periods to be sure reduction originated should be noted by the two digit code of 3~1 shutdowns or significant power reductions are reported. Exhibit C - instructions for Preparation of Data Entry Sheets Until a unit has achieved its first power generation, no num- for Licensee Event Report (LER) File (NUREG4161).
ber should be assigned to each entry. Sysiems that do not fit any existing code should be designa-ted XX The code ZZ should be used for those events where DATF This column should indicate the date of the start a system is not applicable.
of each shutdown or significant power reducuon. Report as year. month, and day. August i4. 1977 would be reported COMPONENT CODE. Select the most appropriate component as 770814. When a shutdown or significant power reduction from Exhibit I - Instructions for Preparation of Data Entry begins in one report period and ends in another, an entry should Sheets for Licensee Event Report (LER) File (NUREC4161).
be made for both report periods to be sure ail shutdowns using the following critieriai or significant power reducuons are reported.
A. Ifa component failed, use the component directly involved.
TYPE. Use "F" or "S" to indicate either "Forced" or "Sche-duled," respectively, for each shutdown or significant power B. If not a component failure, use the related component:
reduction. Forced shutdowns include those required to be eg., wrong valve operated through error: list valve as initiated by no.,later than the weekend following discovery component.
of an oifwormal condition. It is recognized that some judg-ment is required in categorizing shutdowns in this way. In C. If a chain of failures occurs, the fiat component to mal-general. a forced shutdown is one that would not have been function should be listed. The sequence of events. includ-completed in the absence of the condition for which corrective ing the other components which fail, should be described acuon was taken. under the Cause and Corrective Action to Prevent Recur-rence column.
DURATION. Self~xplanatory. When a shutdown extends Components that do not fit any existing code should be de.
beyond the end ot a report period, count only the time to the signated XXXXXX. The code ZZZZZZ should be used for end of the report period and pick up the ensuing down time events where a component designation is not applicable.
in the following report periods. Report duration of outages rounded to the nearest tenth of anhour to facilitate summation.
CAUSE &, CORRECTIVE ACTION TO PREVE>VE RECUR-The sum of the total outage hours plus the hours the genera-RENCE. Use the column in a narrative fashion to amplify or tor was on line should equal the gross hours in the reporting explain the circumstances of the shutdown or power reduction.
period.
The column should include the specific cause for each shut ~
down or significant power reduction and the immediate and REASON. Categorize by letter >Iesi>gnatiun in accordance with the table appearing on the report form. If category H contemplated long term corrective action taken. if appropri ~
ate. This coluinn should also be used for a description of the must he used. supply briei'comments.
major safety-related corrective maintenance performed during METHOD OF SHUTTINC DOWN THE REACTOR OR the outage or power reduction including an identification of REDUCING POWER. Cateaorize by numher designation the critical path activity and a report of any single release oi radioactivity or single radiation exposure speciti<<ally asso<<i-1 Nioie that this diff'ers t'rom the Edison Ele tric Institute ated with the outage which accounts for more than 10 percent
<EEI) definitions oi'Forced Partial Outage" and -Sche. oi the allowable annual values.
duled Partial Outage." F>>r these tern>>. EEl uses a <<hange or'0 For long textual reports continue narrative on separate paper MW as the break i>>>int. For larger power reactors. ~0 MW an>I rer'eren<<e the shutdown or =power redu<<tiun for th>>
is I>><> small a <<hange ti> warrant <<xplanati>>i>. naf fa tive.
Docket No.: 50-315 Unit Name: D,.C. Cook Unct 81 Completed By: R. S. Lease Telephone: (616) 465-5901 Date: Harch 5, 1979 OPERATING EXPERIENCES FEBRUARY, 1979 Hi hli hts This Unit has operated at full power the entire reporting period except for one outage and other load reductions as required for maintenance.
Summar 02/03/79 Loading was reduced to 70K (780 tQe) starting down at 1130 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.29965e-4 months <br />. This was for Cross Calibration of Incore/Excore Nuclear Instrumentation. Power was returned to 1005 (~1080 NMe) by 0350 hour0.00405 days <br />0.0972 hours <br />5.787037e-4 weeks <br />1.33175e-4 months <br /> s 2/04/79.
02/06/79 One of two Pressurizer Relief Tank ruptured diaphragms ruptured at 0455 hours0.00527 days <br />0.126 hours <br />7.523148e-4 weeks <br />1.731275e-4 months <br />. This caused all Ice Condenser doors to indicate open. The Unit was started down at 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br /> and removed from service at 0816. All Ice Condenser doors were reclosed by 0920 hours0.0106 days <br />0.256 hours <br />0.00152 weeks <br />3.5006e-4 months <br />.
The ruptured disc failed during a feed and bleed maneuver to reduce the temperature of the water in the tank. Both ruptured discs were replaced on the tank.
02/07/79 The Reactor was returned to criticality at 0108 hours0.00125 days <br />0.03 hours <br />1.785714e-4 weeks <br />4.1094e-5 months <br /> and the Generator paralleled to the system at 0329 hours0.00381 days <br />0.0914 hours <br />5.439815e-4 weeks <br />1.251845e-4 months <br />. The Unit was loaded to 100K (1080- MWe) by 1545 hours0.0179 days <br />0.429 hours <br />0.00255 weeks <br />5.878725e-4 months <br />.
2/8 //I I d/ I d d 858 (888 81 / I'11 CWP from service for repair of a lube oil leak. Power was returned to lOOX (1080 NWe) by 0255 hours0.00295 days <br />0.0708 hours <br />4.21627e-4 weeks <br />9.70275e-5 months <br />, 2/10/79.
02/18/79 Loading was reduced to 905 (980 NWe) for testing of Turbine valves. Total time below 100Ã power was 2.25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br />.
DOCKET NO. 50 - 315 UNIT NAME ~brook - Unit No. 1 DATE 3-14-79 COMPLETED BY B. A. Svensson TELEPHONE 616 465-5901 MAJOR SAFETY-RELATED MAINTENANCE FEBRUARY, 1979 M-1: Unit 1 East centrifugal charging pump mechanical seal leaked. A new mechanical seal was installed and operational retest of the pump was satisfactory.
M-2 During inspection of aux. feedwater motor operated valves, FMO-231 was found to have a broken jumper wire at terminal ¹46. Repaired broken wire. Had valve tested and returned to service.
M-3 Cooling water safety valve on TDAFP oil cooler, SV-140 was leaking by.
Relapped seat and disc. Performed set point check.
C&I-1 Heat tracing circuit train 112, the emergency boration line, would not maintain temperature. The train B control thermostat set point was adjusted to increase the temperature of the line to 175 F.
C&I-2 DRV-150, the emergency drain valve from the reactor coolant drain tank to the pipe tunnel sump, failed to the closed position. The coil of the solenoid supplying air to the valve failed. The coil was replaced and proper operation verified.
C& I-3 The APDMS system actuated at 715 and 695 power levels. The required power level actuation is 84%. The isolation amplifiers of NIS chan-nels N41 and N42 sending the power level signal to the APDMS were
-recalibrated.
C&I-4 The control room cable vault fire detection system alarmed. A check of the fire detectors was performed. One detector was found alarming.
The detector was removed, cleaned and adjusted for the correct sen-
-sitivity. The system reset was actuated and the alarm cleared.
C&I-5 Radiation monitoring system channel R-2, containment area monitor, failed low. The connector was 'found loose at the containment pene-
.tration and an open connection. The connector and wire were repaired and the channel returned to normal operation.
C&I-6 Radiation monitoring channels R-ll and R-12, filters supply pump would fail. The air flow of the pump required adjustment to 10 SCFM.
The excessive air flow resulted in the filter pump trips.
C&I-7 ILS-950, refueling water storage tank level recorder, indicated 96.5%
when the tank overflow was reached. The calibration calculations were in error. Measurements were performed and the revised calcula-tions of 124" to 487" H20 were used in calibrating the level trans-mitter.