05000315/LER-1979-005-03, /03L-0 on 780624:unit Was Operated W/Positive Moderator Temp Coefficient for 3-h.Caused by Rod Withdrawal & Consequent Xe Build Up.Procedure Being Revised

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/03L-0 on 780624:unit Was Operated W/Positive Moderator Temp Coefficient for 3-h.Caused by Rod Withdrawal & Consequent Xe Build Up.Procedure Being Revised
ML17317A984
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 03/07/1979
From: Beilman T
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317A983 List:
References
LER-79-005-03L-01, LER-79-5-3L-1, NUDOCS 7903130364
Download: ML17317A984 (2)


LER-1979-005, /03L-0 on 780624:unit Was Operated W/Positive Moderator Temp Coefficient for 3-h.Caused by Rod Withdrawal & Consequent Xe Build Up.Procedure Being Revised
Event date:
Report date:
3151979005R03 - NRC Website

text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION LICENSE E EVEN T R E PORT CONTROL BLOCK:

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