05000315/LER-1979-003-03, /03L-0 on 790120:during Review of Completed Surveillance Tests,Discovered That Test on Solid State Protection Sys Train a Exceed 1-h Limit Imposed by Tech Specs.Caused by Technician Overlooking 1-h Limit

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/03L-0 on 790120:during Review of Completed Surveillance Tests,Discovered That Test on Solid State Protection Sys Train a Exceed 1-h Limit Imposed by Tech Specs.Caused by Technician Overlooking 1-h Limit
ML17317A960
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 02/27/1979
From: Beilman T
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17317A958 List:
References
LER-79-003-03L-01, LER-79-3-3L-1, NUDOCS 7903050302
Download: ML17317A960 (2)


LER-1979-003, /03L-0 on 790120:during Review of Completed Surveillance Tests,Discovered That Test on Solid State Protection Sys Train a Exceed 1-h Limit Imposed by Tech Specs.Caused by Technician Overlooking 1-h Limit
Event date:
Report date:
3151979003R03 - NRC Website

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