ML17317A940

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Monthly Operating Rept for Jan 1979
ML17317A940
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 02/12/1979
From: Gillett W
INDIANA MICHIGAN POWER CO.
To:
Shared Package
ML17317A939 List:
References
NUDOCS 7902220046
Download: ML17317A940 (11)


Text

AVERAGE DAILYUNIT POWER L~EL DOCV=-T ~O. 50-315 LNIT 1 D~TE W.T. Gillette CPgPLETED IIY 616-465-5901 TQ.EPHOiiE January 1979 DAY AVERAGE DAlLYPOWER LEVEL (MWe-> let )

I 498 DAY AVERAGE DAILYPOWER L VEL (M

We-Wet

)

1040 17 10 12 13 l5 16 792 931 936 922 927 966 987 1001 1043 1025 1040 1037 1040 1041

]8 19 21 l5 26 27 2S 29 i 30 3l 1041 1040 1041 1041 1039 1041 1040

. 1040 1025 1041 1034 1040 1041 li(STRUCTIONS On this format.!ist;h aver 8

da!Iy >,.".i: p>>ii'er ieve! tn M~~'e Net for each ca>; in the reovr:tnc m>>nth. C >mp>rt tu'ne nearest >>'hole m Saint t.

790 2220 4 /4

~

~ H L ~

OPERATING DATAREPORT DOCmTNO. ~~-~

DATE OOHPEETEOBY ~N.T

.'llett TEL'EPHOHE ~616-

-6 901 OPERATING STATUS Donald C.

Coo

l. Unit Name:
2. Reporting Period:
3. Licensed Thermal Power PfÃt):

4., Nameplate Rating (Gross 1%f4'e) t S. Design Electrical Rating (N s AINe):

6. hfaximum Dependable Capacity (Gross Myse)r
7. ~lfaximum Dependable Capacity (Net MNe):.

1089 1054 Notes

8. IfChanges Occur in Capacies Ratings (Items Number 3 Thro&o
7) Since Last Report. Give Reasons:
9. Power Level To %lhi& Restrict<, IfAny (Net MNe):
10. Reasons For Restrictions. IfAny:

This Month Yr:to Date Cumulative

11. Hours In Reporting Period I'Z. Number Of Hours Reactor Vr'as Critical
13. Reactor Reserve Shutdown Hours
14. Hours Generator On-Line IS. Unit Reserve Shutdown Hours
16. Gross Thermal Energy Genemted (MWH)
17. Cross Electrical Energy Generated (MNH)
18. Net Electrical Energy Gen wted {M)'iH)
19. Unit Service Factor
30. Urit AvailabilityFactor 2I. Unit Capacity Factor {Using MDC Net) 2". Unit Capacity Factor (Using DER Net)

~M. Unit Forced Outage Rate

24. Shutdowns Scheduled Over Next 6 Months 744 744 744 744 0

76'4 100 736 996 100 100 9.4. 9 94.0 0

744 2

299 406 736 996 100 94.0

{Type. Date. and D ~tion of Each):

27 955. 7 463 27 1

73 637 1

24 23 7

78.8 78.8 65.1 6.0

~5. IfShut Down At End Of Report P riod, Estimated Date of Sta.tup:

~

'6. Units ln Test Status lprior to Commercial Operation):

Forecast Achieved IÃITIAL CR IT ICALITY INITlALELECTRICITY CO.'iDIERCIALOPERATiON V~ll7)

1 ~

1

~ ~

UNITSIIUTI)0'lUNS AND PO)UER REDUCTIONS REPORT h(ONfll january, 1979 l)OCKETNO.

hJ219 COh(PLETED DY B.~. >>ensson Nil.

Date

~- L 0 o BK r>

~A r>

u ~

g Q

~ III g A

LICI'.oscc I!vent Rcpllrt 4 El~Vl o

EJ Q

C>

E~

O(J Cause h, Corlcctivc Actioo to Prcvcnt Rceuffcnec The Unit entered the reporting period operating at 50K power.

Reactor power was increased to 90%

790102 and held at this power level due to one circulating water pump being out of service.

Reactor power was at 1005 790112.

The Unit operated for the remainder of the month with no significant power reductions.

0:

I': Forced S: Sclledulcd

(')/77)

I(cas>nl:

A-fquipu>en> Failure (Explain)

II hlaiutcoancc oi Tesl C.Rcfueliug D Regulatory Restriction I!.Operator Traioiui, Ec l.iccosc llxan>inalion F.Adn>inistlative (I Operational Error (Iixplail>)

I I Otllcr (Explain) 3'lctl>od:

I Manual 2 h(annal Scraul.

3-Au>on>alic Scraln.

4-Olllcr (Explain) 4 Exhibit G - Inst r oct ious for Preparati>n> III Data I:otry Sllcets for I.iecusee Evcol Rcport (I.I!R) File (NURI!(i.

OI6l )

'IixilibitI - Saole Source

Docket Unit Name :

Compl eted By:

Telephone :

Date :

50-315 D.

C.

Cook Unit 5'1 R.

S.

Lease (616) 465-5901 February 8, 1979 OPERATING EXPERIENCE -- JANUARY 1979 Hi hli hts This Unit entered the reporting period operating at 505 Power.

Loading was being held at 50'A Power (525 NWe) due to high inven-tory of waste gas in the plant.

Weather instrumentation was frozen at this time not allowing any release of waste gas.

Loading was increased to 905 January 2,

1979 and held and main-tained between this and 1005 power the rest of the reporting period.

Summar 01/02/79 Waste Gas Inventory was rearranged and the weather instrumentation freed up allowing the release of two gas decay tanks.

The Unit was loaded to 90K power (980 NWe) by 2020 hours0.0234 days <br />0.561 hours <br />0.00334 weeks <br />7.6861e-4 months <br />.

Loading was held at this point due to approachinq maximum temperature rise across the Condenser;wh>le only having two Circulating Water Pumps.

01/06/79--

01/08/79--

01/10/79--

01/11/79--

01/12/79 The Turbine Driven Auxiliary Feedwater Pump was inoperable for a 16 hour1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> period to replace the Governor.

A water leak had developed in the Gover-nor oil cooler.

Unit loading was increased to 95K power (1030 NWe) by 1016 hours0.0118 days <br />0.282 hours <br />0.00168 weeks <br />3.86588e-4 months <br />.

//2 Steam Generator Stop Valve Trip Valve MRV-221 was inoperable for a 3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> period to replace

'eaking gaskets.

II3 Steam Generator Stop Valve Trip Valve MRV-232 was inoperable for a 3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> period to replace leaking gaskets.

Discharge Valve of the /f12 Circulating Water Pump WMO-12 was repaired and the valve opened allowing use of this pump.

Power was increased to 1005 (1080 NWe) by 1826 hours0.0211 days <br />0.507 hours <br />0.00302 weeks <br />6.94793e-4 months <br />.

b4 Steam Generator Stop Val ve Trip Val ve MRV-242 was inoperable for a 2.75 hour8.680556e-4 days <br />0.0208 hours <br />1.240079e-4 weeks <br />2.85375e-5 months <br /> period to replace leaking gaskets.

A 4

Docket N Unit Name:

Completed By :

Tel ephone :

Date :

Page :

50-315 D.

C.

Cook Unit ¹1 R.

S.

Lease (616) 465-5901 February 8, 1979 (2)

Ol/12/79 ¹2 Steam Generator Stop Valve Trip Valve MRV-221 was (cont) inoperable for a 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> period to adjust a limit switch and repair an air leak.

Loading was reduced to 955 power (1030 MWe) for a 6 hour6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> period for a Moderator Coefficient Test and then returned to 100Ã power.

01/17/79 The West RHR Train was inoperable for a 6 hour6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> period to repack Valve RH-128W.

01/18/79 Radiation Monitor R-ll was inoperable for a 5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period for repairs to the paper drive.

01/22/?9--

The West Component Cooling Water Pump had difficulty meeting the requirements for minimum discharge pres-sure.

The suction strainer was checked and found to contain resin beads and some pieces of rubber.

The strainer was removed and the pump retested satisfac-torilyy.

01/26/79 Power was reduced to 85K (890 MWe) for testing of Turbine valves.

Time span from unloading back to 1004 power was two hours.

The "AB" Emergency Diesel Generator was inoperable

~for a 7.75 hour8.680556e-4 days <br />0.0208 hours <br />1.240079e-4 weeks <br />2.85375e-5 months <br /> period for changing of lubricating oil in the Governor and the Turbo Charger.

Replacement, of the North Condensate Booster Pump motor was started and was completed January 28, 1979.

01/29/79 -- The North half of "A" Condenser was out of service for 10.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> for location and plugging of leaking tubes.

Annual inspection and overhaul of the plant air compressor was started and this job was completed

Thursday, February 1,

1979.

01/30/79 The East Centrifugal Charging Pump was inoperable for a 21,.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period for replacement of a mecha-nical seal and cleaning of the lube oil filter.

All motor operated Auxiliary Feedwater Valves were removed from

service, one at a time, for inspection of electrical connections and checking of tightness of terminals.

One of the Pressurizer Safety Valves is leaking through at the rate of 2 GPM.

The water in the Pressurizer Relief Tank is being kept cool by the feed and bleed method.

This is adding to evaporator requirements.

DOCKET NO.

UNIT NAME DATE COMPLETED BY TELEPHONE MAJOR SAFETY-RELATED MAINTENANCE 50 - 315 D.

C.

Cook - Unit No.

1 2-12-79 B. A. Svensson 616 465-5901 JANUARY, 1979 M-2 M-3 M-4 M-5 M-6 C&I-1 C&I-2 C&I-3 C&I-4 CVCS holdup tank three-way valve, HARV-303, was stuck.

Disassembled valve and found the cage galled.

Replaced

cage, reassembled valve and verified operability.

The oil in lUnit 1 turbine driven aux.

feed pump turbine governor appeared to have water in it.

The governor was replaced and the tur-bine rechecked satisfactorily.

MRV-221, ¹2 steam generator stop valve dump valve was leaking by.

The valve was disassembled, seat

checked, and new gaskets installed.

Timed retest was satisfactory.

MRV-232, ¹3 steam generator stop valve dump valve was leaking by.

Valve gaskets were replaced.

Timed retest was satisfactory.

Inlet pipe to normal blowdown flash tank was leaking.

Replaced section of pipe downstream of inlet orifice.

Radiography and hydrostatic testing was successfully completed.

No.

4 steam generator stop valve dump valve, MRV-242 was leaking by.

Dis-assembled valve, cleaned internals, replaced seat and gaskets.

Timed retest was satisfactory.

The scan sequencer of the axial power distribution monitoring system failed.

The sequencer 1 printed circuit board was repaired.

An op-erational test was performed and verified the systems operability.

The rod position indication for control rod F-6 was out of specifications.

The position signal for rod F-6 was measured and recorded as 2.885 vdc.

The secondary coil voltage was verified and the calibration of the signal conditioning module was performed.

The axial power distribution monitoring system failed to perform the eight hour scan.

The time sequencer digital display also failed.

The timer sequencer printed circuit board required replacement.

The panel. rod position indication for control rod F-6 was out of speci-fications.

The LVDT secondary coil voltage was measured and verified correct.

The signal conditioning modules output signal was recorded as 2.885 vdc.

The modules calibration was performed and the output voltage measured 3.425 vdc corresponding to a position of 228 steps.