ML17304B405

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Insp Repts 50-528/89-34,50-529/89-34 & 50-530/89-34 on 890717-21.Violations Noted.Major Areas Inspected:Review of Sys Engineer Activities,Responsibilities & Authority
ML17304B405
Person / Time
Site: Palo Verde  
Issue date: 08/03/1989
From: Ang W, Andrea Johnson, Richards S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17304B402 List:
References
50-528-89-34, 50-529-89-34, 50-530-89-34, NUDOCS 8908290079
Download: ML17304B405 (14)


See also: IR 05000528/1989034

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report Nos.

50-528/89-34,

50-529/89-34

and 50-530/89-34

Docket Nos.

50-528,

50-529,

50-530

License

Nos.

NPF-41,

NPF-51 and NPF-74

Licensee:.

Arizona Nuclear

Power Project

P.

0.

Box 52034

Phoenix,

AZ

85072-2034

Facility Name:

Palo Verde Nuclear Generating Station Units 1,

2 & 3

Reactor

ProJects

Branch,

Sect>on

Ins ection Summar:

Inspection

Conducted:

July 17-21,

1989

Inspectors:

N~

roy ct

nspector

s

A. Jo

son,

Enforcement Off>cer

Approved By:

S.

Rl hard,

Ch>ef

II

g-3- EQ

ate

>gne

D te

signed

8-3- Qg

ate

S>gned

Ins ection

on Jul

17-21

1989.

Re ort Nos.

50-528/89-34

50-529/89-34

and 50-530 89-34

During this inspection

the following Inspection

Procedures

were utilized:

30703,

37700

and 35702.

Safe

Issues

Mana ement

S stems

(SIMS) Items:

None

Results:

Of the two areas

inspected

one violation was identified.

This

violation identified a lack of timely completion of post trip review

corrective actions,

paragraph

2.6.

General

Conclusions

and

S ecific Findin

s

Si nificant Safet

Matters:

Overdue post trip review corrective actions

was identified.

Summar

of Violations:

Summar

of Deviations:

0 en Items

Summar

None

Two new items identified.

R

Sl<<~~

.)r

()tc'sooo~s>'-'iIF'VOCA"'

~ IC

r.

DETAILS

1.

Persons

Contacted

Arizona Nuclear

Power Pro'ect

ANPP

B. Ballard, Quality Assurance Director

  • J. Reilly, Standards

and Technical

Support Director

  • C. Russo, Assistant Quality Assurance Director
  • T. Shriver,

Compliance

Manager

  • G. 'Sowers,

Engineering Evaluations

Manager

The inspectors

also met with other licensee

and contractor

personnel

during the course of the inspection.

  • Attended the Exit meetings

held

on July 20 and 21, 1989.

2.

Desi n, Desi

n Chan

es

and Modifications

37700

An inspection

was performed

on design

changes

and modifications to verify

licensee

compliance with NRC requirements

and licensee

commitments.

The

inspection

included

a review of system engineer activities, their

responsibilities

and authority.

Applicable portions of the following

licensee

procedures

and work documents

were reviewed.

Licensee

Procedures

42 OP-2ZZ04, revision 3, Plant Startup,

Mode

2 to Node

1

42 OP-2Z207, revision 2, Plant Shutdown,

Node

1 to Mode

2

70 PR-OAPOl, revision 0, System Engineer

Program

73 AC-OEE01, revision 0, Engineering

Evaluation

Request

73 AC-ONS01, revision 0, Plant

Change

Package

73 AC-ONS02, revision 0,

Change Control

Process

73 AC 9MS28, revision 0, Site Modification

Post Tri

Review

Re orts

PTRR

- PTRR 1-88-004 -

Unit

1 Auxiliary Transformer Fire and Reactor Trip

of July 6,

1988, report dated July 29,

1988

-

PTRR 2-88-001 -

Low Steam Generator

h'

Level Trip During

Downpowering of Hovember

16,

1988, report dated

November 22,

1988.

,

Site Modification

S-MODS

- S-MOD SM-EW-002,

July 14,

1988, Essential

Cooling Water to Nuclear

Cooling Water Crosstie

Valves Limitorque Operator

Rotor Assignments

- S-MOD 2-SM-SF-005,Completed

7/88,

Steam Generator

Feedwater

Control

System Electronic Setpoints

a 0

S-Mod SM-EN-002

-PTTR-1-88-004,

Concern

B. 1 noted that during the July 6,

1988

auxiliary transformer fire and associated

reactor trip, difficulties

were encountered

in attempting to cross-tie

nuclear cooling water

with essential

cooling water by remotely opening cross-tie

valve

EWA-UV-145.

Auxiliary Operators

were subsequently

able to partially

open the valve at the valve location.

The

PTRR further stated that

the suspected

cause of fai lure was that the valve limitorque

operator

torque switch bypass setting

was improperly set.

S-MOD

1-SYi-EW-002,

t>ad been

prepared

(5-11-88) to correct the suspected

problem.

This

S-MOD was however, in the approval

cycle at the time

of the trip (7-6-88).

The

PTRR recommended

corrective actions

were

to implement the

S-YiOD in Unit

1 prior to entering

Mode

4 and to

implement the

S-MOD in Units

2 and

3 during the first outage of

sufficient length but not to extend past

the next refueling outage.

At the time of this

NRC inspection,

the S-Mod had

been completed in

Unit 1,

was being performed in Unit 3 and

was scheduled

for

accomplishment

in Unit 2 during its next refueling outage.

The

licensee

considered

the Unit 2 valves to .be in conformance with

Technical Specification requirements.

The inspector

observed

from

a review of the licensee's

evaluation

and surveillance test results

that the valve would perform the required safety function of

closure if the valve was open.

The valve continues

to remain in

its closed position

as required

by the technical specification for

system operability.

During the review of S-MOD- SM-EW-002, the inspector

noted that part

of the reason for performing the

S-MOD was also to address

INPO

significant operating

experience

report

(SOER) 86-20.

The

SOER

reported

a

San Onofre experience "regarding Limitorque bypass

torque

switches that were

on the

same rotors

as the valve position

indication contacts

and resulted in valves

remote position

indicating shut,

when the valves

were not fully shut

due to bypass

torque switch settings

prematurely terminating valve closure motion.

This condition was not the

PTRR identified condition and did not

appear to have

been

a problem experienced

at Palo Verde.

The

S-MOD

corrects

both the

PTRR noted problem

and the potential for the

SOER

noted problem.

However, since the

S-MOD had not been

performed in

Unit 2, the inspecto'r

attempted to determine

how the licensee

confirmed that the

SOER condition did not exist for the

EW cross-tie

valves that still had both the bypass

torque switch and the closed

valve position indication on the

same rotor.

In addition,

the

inspector inquired

how the licensee fulfilled EW System Technical

Specification

(T/S) surveillance

requirement 4.7.3.b - at least

once

per

18 months during shutdown,

by verifying that each

automatic

I

I

valve servicing safety-related

equipment actuates

to its correct

position

on

a Safety Injection Actuation Signal

(SIAS) test.

This

would require verification that the

EW cross-tie'alves

shut during

a SIAS.

The System En'gineer

informed the inspector that the

surveillance

had

been

performed

by verifying the remote valve

position indication lights.

The System Engineer

agreed that if the

SOER noted condition existed,

depending

on remote valve position

indication, lights could be incorrect.

The system engineer further

stated

however, that significant leakage

past the valve would also

be noted, if the valve was not fully shut, but no such

leakage

had

been identified in the past.

During subsequent

discussions

with the

licensee,

the licensee

agreed

to perform an engineering

evaluation

to confirm that the

SOER valve misposition (i.e. not fully shut)

condition did not exist for the Unit 2

EW cross-tie

valves

and that

T/S 4.7.3.b,

surveillance

requirements

had

been met.

The licensee

performed this evaluation

on

EER 89-EW-014 and confirmed that the

Unit 2

EW cross-tie

valves

were shut.

S-NOD 2-SM-SF-005

Concern

5 of PTRR 2-88-001,

low steam generator

82 level trip durin9

downpower,

November

16,

1988,

noted that

S-NOD 2-SM-SF-005

changed

the feedwater control

system

(FWCS) electronic setpoints for main

feedwater turbine

speed control.

The

PTRR further noted that

necessary

revisions to the operating

procedures

governing feedwater

pump operation with the

new

FWCS program was not made subsequent

to

the

S-NOD ard before the plant trip.

The

PTRR also noted that the

administrative

procedure

(73AC-9MS28) for processing

of S-MODs had

been

changed

subsequent

to issuance

of S-NOD2-SN-SF-005

to require

cross-discipline

technical

reviews of S-MODs prior to issuance,

and

hence

precluae further repetition of S-MODs being completed without

necessary

changes

to affected

procedures

being issued.

The

PTRR, the

S-MOD administrative

procedure

and the noted

S-MOD

were reviewed

and discussed

with the system engineer.

The system

engineer

acknowledged

that

he misunderstood

the needed

procedure

changes,

and at the time considered

that the procedure

changes

needed

was for the I 8

C calibration procedure,

and

he did in fact

change

the

ISC calibration procedure.

The system engineer stated

that the affected operating

procedures

(42 OP-2ZZ04

and 42 OP-2ZZ07)

had since

been

changed

to provide operators

with additional

instructions related to the

FWCS setpoint changes,

and provided the

inspector

the procedure

changes.

The

PTRR provided additional corrective action to assure

that

significant similar occurrences

were also identified and corrected.

The corrective actions required evaluation of the site-mod

procedure,

the system engineer

program

and

system engineer

interface

responsibilities

with the procedure writers, Plant Standards,

to

"determine if they are designed

to prevent

a similar event in the

future."

The

PTRR further required the Engineering

Evaluations

Department

(EED) to perform

a "backfit" cross discipline review on

a

sample of current site-mods

to evaluate

the impact

on plant

operations.

The above

noted

PTRR corrective actions

were discussea

with the

EED Manager

and the Director of Standards

and Technical

Support.

They confirmed that, at the end of this

NRC inspection;

the noted

PTRR corrective actions

had not been completed

and would

not be completed for another

30 days.

At the

end of this

NRC

Inspection

the

PTRR corrective actions

were at least

5 months

overdue

past their original 90 day completion date.

In attempting

to determine

the promptness

of the above

PTTR corrective actions,

the inspector

reviewed the'Standards

and Technical

Support Directors

"PTTR/SPEER

Overdue Action Items" database.

The July 17,

1989

database

indicated that approximately

115 PTRR/IIR/SPEER action

items were overdue,

some of those

items being overdue

by

approximately

16 months.

10 CFR 50 Appendix "8" Criterion XVI

requires that measures

be established

to assure

that conditions

adverse

to quality are ~rom~tl

identified and corrected."

The lack

of timely completion of the above

noted post trip review corrective

actions,

which represent

potential contributors to future plant

trips,

was identified as Violation 50-528,

529, 530/89-34-01,

"Lack

of Timely Completion of Post Trip Review Corrective Actions."

Desi

n Chan

e and Modification Process

Various processes

for initiating design

changes

and modifications

were outlined in licensee

procedures

73 AC-OEE01 (EER's),

73AC-OMSOl

(PCP's),

73 AC-OMS02 (Change Control)

and

73AC-9MS28 (S-MOD's).

System engineers

functions in these

processes

are further outlined

in procedure

70PR-OAPOl.

These

procedures

and processes

were

reviewed

and discussed

with both the Engineering Evaluations

Department

(EED) Manager

and the Standards

and Technical

Support

Director.

These

reviews

and discussions

resulted

in the following

inspector observations.

System Engineers

perform

a central function in these

processes.

System Engineers

have significant responsibilities

in these

processes.

System Engineers

have

some authority but ultimate

authority for approving accomplishment of design

changes

and

modifications rests with Palo

Verde Management.

For example,

system engineers

recommend

design

changes

and modifications

and

provide an initial recommended priority for accomplishment of

the changes.

The

EED Manager

and

a Plant Change

Review

Committee decides

what changes

are to be made

and sets

the

final priority for accomplishment

of the changes.

The

Standards

and Technical

Support Director stated that System

Engineer authority will be increased

with the implementation of

a nonconformance

report=(NCR)

process

(scheduled for issue

8/1/89).

The

new

NCR process will require correction of NCR

conditions within the time frame specified

by the System

Engineer

and approved

by his/her supervision.

The Plant

Change

Review Committee

was

composed of the

EED

Yanager

(Chairman)

and the Plant Managers.

The Standards

and

Technical

Support Director stated that the licensee

is

currently studying changing

the Plant

Change

Review Committee

to

a Plant Modifications Review Committee

composed of the Site

Director (Chairman),

the Standard

and Technical

Support

Director, the Engineering

and Construction Director and the

Plant Managers.

The proc'edure for the

new process

was still in

draft form (scheduled for issue 9/1/89)

and

had not yet been

implemented.

No procedure outlining the composition

and

functions of the Plant

Change

Review Committee

was available.

The

EED Manager

informed the

NRC inspector of the following

statistics.

(1)

S-MODs designed

but not implemented or completed - Unit

1-35, Unit 2-34, Unit 3-33

(2)

Design

Change

Packages

issued

but not installed - Unit

1-151, Unit 2-67 and Unit 3-71

(3)

Design

Change

Packages

in preparation

stage - Unit 1-109,

Unit 2-98, Unit 3-97

These

design

changes

and modifications were of various

significance

and priority.

The design

change

and modification procedures

noted

above

contained

requirements

for establishment

of a priority for

implementation.

However, only the

EER procedure

defined the

priorities.

The

S-MOD procedure,

the

Change

Control

Process

procedure,

the Plant

Change

Package

procedure

and the System

Engineer

Program procedure

did not reference

the

EER procedure

for establishment

of priority.

The

EED Manager stated

that it

was the

EER procedure priority codes that was utilized for

definition of implementation priorities.

The

EED Manager

agreed that further clarification of the other procedures

to

.,reference

the priority codes

was in order.

Pending

issuance

of the Plant Modifications Review Committee

procedure

and clarification of the implementation priority code

requirements,

this

was identified as Unresolved

Item 50-528,

529,

530/89-34-02 -. Plant Modifications Procedures

Questions.

Ins ection of Qualit

Verification Function

35702)

a

~

A Hotline Investi ations

An inspection

was performed

on the licensee

QA Hotline process.

Hotline File Number 89-31

was reviewed

and discussed

with the

licensee.

The Hotline item consisted of approximately

32 employee

concerns

dealing primarily with industrial safety.

However, the

Hotline item also included concerns

dealing with ALARA, fitness for

duty and "seismic scaffolding".

Discussions

with the

QA Director

and the

QA staff indicated that Arizona State

OSHA had already

performed

an inspection

on

some of the industrial safety concerns.

However, the licensee's

QA Hotline staff had just started

preliminary investigations

and information gathering

on the Hotline

item.

The

NRC inspectors

encouraged

the licensee

to perform

a

thorough

and unbiased

investigation of the Hotline concerns.

This

Hotline concern will be examined

upon completion of the licensee's

investigation.

No violations or deviations

were identified during this inspection.

4.

Unresolved

Items

Unresolved

items are matters

about which more information is required to

determine

whether they are acceptable

or may involve violations or

deviations.

One

new unresolved

item identified during this inspection is

discussed

in paragraph 2.c.

5.

Exit Interview

The inspection

scope

and findings were summarized

on July 20 and 21,

1989, with those

persons

indicated in paragraph

one above.

The inspector

described

the areas

inspected

and discussed

in detail

the inspection

findings.

No dissenting

comments

regarding

the inspection findings were

received

from the licensee.

The following new items were identified

during this inspection.

Violation 50-528,

529, 530/89-01 - Lack of timely completion of Post Trip

Review Corrective Action.

Unresolved

Item 50-528,

529, 530/89-34-02

- Plant Modifications

Procedures

(}uestion,