ML17284A562

From kanterella
Jump to navigation Jump to search
Insp Rept 50-397/88-33 on 880906-09.Violation Noted. Major Areas Inspected:Organization & Mgt Controls,Followup, Gaseous Waste & Tours of Facility
ML17284A562
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 10/04/1988
From: Cicotte G, North H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17284A560 List:
References
50-397-88-33, NUDOCS 8810210612
Download: ML17284A562 (14)


See also: IR 05000397/1988033

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report

No. 50-397/88-33

Docket No. 50-397

License

No.

NPF-21

Licensee:

Washington Public Power Supply System

P.

0.

Box 968

Richland,

Washington

99352

Facility Name:

Washington Nuclear Project

No.

2

Inspection at:

WNP-2, Benton County, Washington

Inspection

Conducted:

September

6-9,

1988

Inspectors:

Approved by:

G.

R. Cicotte, Radiation Specialist

H.

S. North, Acting Chief

Facilities Radiological

Protection Section

ro sag

Date Signed

Pz

Date

igned

~Summar:

Ins ection durin

eriod of Se tember 6-9

1988

Re ort No. 50-397/88-33

Areas Ins ected:

Routine,

unannounced

inspection

by a regionally based

inspector of organization

and management

controls,

followup, gaseous

waste,

and tours of the facility.

Inspection procedures

30703,

83722,

92701,

84724,

and 83726 were addressed.

Results:

Of the four areas

addressed,

no violations were identified in three

areas.

In one area,

a violation of Technical Specification 3.3.7. 12 was

identified, regarding failure to sample the main plant vent for radioactivity

(see paragraph

4).

Additionally, it was noted that housekeeping

procedures

do

not appear to address

material condition of the primary containment during

plant operation

(see

paragraph

5).

Overall, the licensee's

programs

appeared

capable of meeting the safety objectives.

SS102i06i2

SSi006

ADOCK 05000397

PDR

PDC

Q

DETAILS

1.

Persons

Contacted

C.

M. Powers,

Plant Manager

"J.

W. Baker, Assistant Plant Manager

"J.

D. Arbuckle, Plant Compliance

Engineer'L.

Bradford, Health Physics Supervisor

"T. A. Brun, Plant guality Assurance

Engineer

A. I. Davis, Senior Radiochemist

"R.

G. Graybeal,

Health Physics/Chemistry

Manager

  • A. G. Hosier,

Licensing Manager

"R.

L. Koenigs, Technical

Manager

"D. A. Larson, Radiological

Programs/Instrument

Calibration Manager

"C.

H. McGilton, Manager Operational

Assurance

and Programs

S.

L. McKay, Operations

Manager

J.

D. Mills, Senior Health Physicist

D.

A. Pisarci k,

ALARA Supervisor

"V. E. Shockley,

Health Physics

Support Supervisor

Contractors

"W.

E.

Milbrot, Engineer,

Bonneville Power Authority

In addition to the individuals identified above,

the inspectors

met and

held'iscussions

with other

members of the licensee's

staff and

personnel.

"Denotes those present at the exit interview held on September

9,

1988.

2.

Or anization

and

Mana ement Controls

The following procedures

were reviewed

and aspects

thereof discussed

with licensee

personnel:

Procedure

PPM

Revision

Date

111

l. 1.2,

1.1.3,

1.1.6,

Management Organization

Plant Organization

Plant Responsibilities

Plant

ALARA Committee

3

6

10

3

3-2-87

3-23"87

3-23"88

3-31-87

The licensee

had

made several

recent

management

assignments,

including a new ALARA Supervisor,

a new Manager of the Nuclear

Safety Assurance

Group

(NSAG), a new Plant Technical

Manager,

and

a

new Assistant Maintenance

Manager.

The above

noted individuals

appeared

to meet the qualification requirements

of ANSI/ANS 3. 1,

Selection

uglification

and Trainin

of Personnel

for Nuclear

Power Plants, with respect to radiological safety responsibilities.

Those individuals with whom responsibilities

were discussed

were

observed to be aware of their responsibilities.

B.

~Staff in

Several

of the licensee's

Health Physics

(HP) staff stated that the

HP department

was understaffed relative to the unplanned

outage

then

in progress.

The inspector

noted that almost all the

HP technicians

had worked the maximum overtime hours allowed by the licensee's

procedures,

during the outage which had occurred

due to valve

leakage

exceeding

the Technical Specification

(TS) limit.

Although

some delays

were experienced

as

a result of technician assignments,

no examples of failure to provide adequate

HP surveillance

were

observed.

The licensee

normally hires

and trains contractor Health

Physics Technicians

(HPT) during extended

outages.

C.

Health

Ph sics/Chemistr

Mana er

(HP/CM)

The qualifications of the

HP/CM were observed to be consistent with

ANSI/ANS 3. 1.

Licensee

procedures

(such

as in paragraph

2.A, above)

address

the HP/CM's responsibility and authority to carry out the

Health Physics

and Chemistry Programs.

See also Inspection

Report

50-397/88-26,

paragraph

5.

The organization

appeared

capable of

meeting their safety objectives.

Other aspects

of the licensee's

organization

and management

controls will

be examined in a subsequent

inspection.

No violations or deviations

were identified.

3.

~fol 1 owo

50-397/88-22-03

(Open) Strip chart recorder operation

on ARM-RR-600, for

Area Radiation Monitors (ARMs), was observed

(see Inspection

Report

50-397/88-22).

The three ink colors

had again

begun to merge

such that

banks of ARMs were difficult to distinguish.

This matter will remain

open for review of pending maintenance/modifications

(50-397/88-22-03

Open).

50-397/88-22-06

(Closed) This matter concerns

an observed

tendency

by

plant personnel

to leave radiological postings

down after removal for

access.

The licensee

had proceduralized

a requirement that all personnel

accept responsibility for replacing postings after exiting or entering

a

posted

area.

One instance of workers leaving the posting

down for

a

radiation area

was observed.

This was immediately corrected

by the

individual responsible

when it was brought to their attention.

Since the

incidence of such posting removals

had declined significantly, this

matter is considered

closed

(50-397/88-22-06

Closed).

50-397/85-20-'4

(Unresolved) This matter refers to evaluation of iodine

plateout in plant effluent sampling lines under accident conditions.

The

licensee

had issued

a Request

for Proposal

(RFP) to a contractor

who had

previously done

some preliminary work on the issue.

The

RFP encompassed

testing which would require outage conditions.

The licensee

stated

they

expected to do the work during the 1989 refueling outage.

The licensee

further stated that computational

studies of iodine behavior within the

sample lines

and equipment would await an evaluation of the test data.

This matter will remain

open pending the licensee's

test results

(50-397/85-20-04

Unresolved).

An unresolved

item is one about which more information is required in

order to determine if it is an acceptable

item,

a deviation, or a

violation.

Inspection

Report 50-397/88-26,

paragraph

6,. discussed

the licensee's

respiratory protection training.

During the inspection,

the General

Employee Training (GET) Supervisor

discussed

a concern

expressed

by the

inspector in regard to special training for self-contained

breathing

apparati

(SCBA).

The discussion

resulted in the conclusion that the

footnote of 10 CFR 20 Appendix A, referred to in the report,

was

applicable for a type of SCBA not used

by the licensee,

and that the

licensee's

training meets

the minimum requirements

of 10 CFR 20. 103(c).

No violations or deviations

were identified.

Gaseous

Waste

S stems

On September

7, 1988, at approximately

6:ll P.M.

PDT, the Reactor

Building (RB) exhaust ventilation fan,

REA-FN-lB, failed and normal

RB

ventilation

was secured.

The Standby

Gas Treatment

System

(SGTS)

was

started at 6: 19 P.M.,

PDT on September

7,

1988, in order to partially

restore ventilation flow.

Discussion with the licensee

revealed

the

following:

The licensee identified a failure to initiate alternate

sampling

within four hours in accordance

with Technical Specifications (TS) 3.3.7. 12,

and stopped

the unmonitored release

at 4:48 A.M., PDT on

September

8, 1988.

o

The licensee

restored

normal

RB ventilation and sampling after

making repairs at approximately 5:00 A.M., PDT on September

8,

1988.

TS 3. 3. 7. 12 states,

in part:

"3.3.7. 12 The radioactive

gaseous, effluent monitoring instrumentation

channels

shown in Table 3.3.7. 12-1 shall

be

OPERABLE with their

alarm/trip setpoints

set to ensure that the limits of Specification

3. 11.2. 1 are not exceeded.

The alarm/trip setpoint of these

channels

shall

be determined in accordance

with the methodology

and parameters

described

in the

ODCM.

APPLICABILITY:

As shown in Table 3. 3. 7. 12-1.

ACTION: "

"b.

With less than the minimum number of radioactive

gaseous

effluent

monitoring instrumentation

channels

OPERABLE, take the

ACTION shown

i n Tab 1 e 3. 3. 7. 12-1. "

I'TABLE 3. 3. 7. 12-1

RADIOACTIVE GASEOUS

EFFLUENT MONITORING INSTRUMENTATION

INSTRUMENT

MINIMUM

CHANNELS

OPERABLE

APPLICABILITY ACTION..."

"3.

Main Plant Vent Release Monitor..."

~

IIb

C.

d.

e.

Iodine Sampler

Particulate

Sampler

Effluent System

Flow Rate

Monitor

Sampler

Flow Rate Monitor

"TABLE NOTATIONS"

112

112

113

113"

""At al 1 times. "

"ACTION 112

ACTION 113

With the number of channels

OPERABLE less

than

required

by the Minimum Channels

OPERABLE

requirement,

effluent releases

via this pathway

may

continue for up to 30 days provided that within 4

hours after the channel

has

been declared

inoperable

samples

are continuously collected with auxiliary

sampling equipment

as required in Table 4. 11-2.

With the

number of channels

OPERABLE less

than

required

by the Minimum Channels

OPERABLE

requirement,

effluent releases

via this pathway

may

continue for up to 30 days provided that the flow

rate is estimated at least

once per 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />."

The Senior Resident Inspector's

(SRI) discussion with the

on shift

operations

personnel

revealed that the chemistry department,

which is

responsible

for obtaining effluent samples

and for maintaining the

auxiliary sampling equipment

as called for by ACTION 112 of TS 3.3.7.12,

was not specifically informed that the main plant release

monitor,

REA-SR-37,

was inoperable.

The specific operator

involved stated to the

SRI that

he had missed the procedural

step to declare

REA-SR-37

inoperable.

Licensee

procedure

PPM 2. 10. 1, Reactor Buildin

HVAC,

Revision B,,dated 6-17-88, states

in part:

"2.10.1.4 Limitations..."

"...E. If Reactor Building ventilation is lost and

SGT is supplying

Reactor Building ventilation, declare

REA-SR-37

INOP (too low flow),

Technical Specification 3.3.7.12."

PPM 4. 10. l. 1, Reactor Buildin Ventilation Failure,

Revision 5, dated

8-2-88, states

in part:

"4. 10. 1. 1.4 Subse

uent

0 erator Action..."

"...C.

Declare

REA-SR-37

INOP.

(Not enough flow through the sample rack

with only SGT running.)"

Through discussion with the Senior Radiochemist

(SRC),

and review of

previous revisions of PPMs

2. 10. 1 and 4. 10. 1. 1, it was determined that

REA-SR-37

becomes

inoperable with only SGTS flow while in automatic flow

control.

The automatic function is designed to meet the requirement to

know the sample/effluent flow ratio,

as delineated

in TS Table 4. 11-2,

table notation "e.", by holding the ratio'onstant.

The automatic

function becomes

less accurate at lower flow rates,

such

as 10,000

CFM,

and apparently

does not function at a flow of 4,000

CFM, which is the

maximum

SGTS flow.

As a result of the occurrence,

the

SRC had submitted

a Technical

Evaluation Request

(TER) for evaluation of a proposed

modification that would hold sample flow rate constant

below a specified

effluent flow rate.

The ratio would then

have to be calculated for each

period in which the effluent flow varied, but would remain operable at

low effluent flow rates.

Further review revealed that the procedures

had

been revised

as corrective

action for Non-Conformance

Report

(NCR)

¹288-153,

dated 5-7-88.

During testing of

RB normal ventilation on May

7, 1988,

the licensee

secured

the ventilation

fans

and started

SGT to

maintain ventilation.

In this instance also,

the Chemistry Department

was not informed that REA-SR-37 was inoperable,

and main plant vent

release

continued for approximately six hours without continuous

sampling

with the auxiliary equipment.

The licensee

stated that the procedural

change

had been

intended to prevent recurrence.

Although in both events,

the noble gas low/intermediate

range monitoring channels

were also

inoperable,

the time limitation of eight hours to obtain

a grab

sample

was not exceeded.

The high range

noble

gas monitor is situated in the

effluent stream

and was thus not affected,

and very large releases

could

have

been detected.

The May 7, 1988, event was not reported in the January to June

1988

Semi-Annual Effluent Re ort

SAER

, dated August 10,

1988.

It was,

however,

reported in an addendum

dated

August 26,

1988, within the

60 day

time limit for the

SAER.

Also, in the July to December

1987

SAER, the

licensee

reported that on August 11, 1987, action

112 of TS Table

3.3.7. 12-1 for the

Radwaste

Building (RWB) was not met, in that the

sample rack was

removed from service for maintenance,

the auxiliary rack

was not used,

and

an unmonitored release

continued for seven

hours.

In accordance

with 10 CFR 2 Appendix C, Part V, Enforcement Actions,

Subpart

G, Exercise of Discretion, notices of violation are not normally

issued for licensee-identified

violations meeting certain criter ia.

However, criterion "e." thereof reads:

"e. It was not a violation that could reasonably

be expected to have

been prevented

by the licensee's

corrective action for a previous

violation."

As the corrective action for the

May 7, 1988,

event did not appear to be

effective in preventing the September

7, 1988, event,

which appears

to be

a violation of TS 3.3.7. 12 (50-397/88-33-01).

No other violations or deviations

were identified.

s.

Faci1 it

Tours

Tours of the

RWB,

RB, and Turbine Building (TB) were conducted.

Independent

radiation surveys

were performed with an

NRC ion chamber

survey instrument

model

R0-2, Serial

No.

009154, calibrated 8-12-88

and

due for calibration 11-12-88.

The licensee

stated that during power level increase

above

20K to 30K,

the

HPTs replace certain radiation area postings in the

TB with high

radiation area postings in anticipation of dose rate changes

as power

increases.

One sign,

on a locked door on a stair landing leading to the

reactor feedwater

heater

bay,

appeared

to have

been missed.

A survey of

the area to which the door lead,

however,

revealed that dose rates

had

not yet resulted in an actual

high radiation area outside posted

areas.

At 40K power,

readings at 18" from several

components

were approximately

95 mr/hr on both the

NRC and licensee

instruments.

Housekeeping,

with the exception of the matter discussed

below exhibited

evidence of continued attention

(see

Inspection

Report 50-397/88-28

paragraph

5).

Some areas

which had remained

contaminated for long

periods

had been decontaminated,

and the licensee

was in the process

of

repainting several

pump

rooms in the

RB.

Personnel

actions at the Primary Containment ("Drywell") (D/W) control

point were observed.

Three individuals just exiting the

D/W touched

their faces,

glasses,

or other exposed parts while undressing.

The

HPT

was informed,

and counseled

the workers.

None appeared

to be

contaminated

when performing whole body frisks.

One appeared

to be

suffering from heat stress,

and

was treated

by accepted

methods.

The

worker appeared

to improve slightly, but the Safety Department

was

informed and the worker was evacuated

on a stretcher.

The licensee later

stated that the worker had suffered

a mild heart attack.

Licensee

briefings

and measures

to control heat stress,

such

as ice vests,

heat

stress

stay times,

and careful observation

by HPTs and safety personnel

appeared

appropriate

to the level of hazard present.

The

HP Supervisor

later stated

to the inspector that the individual who had experienced

the

heart attack

had been briefed,

had been specifically counseled

by his

supervisor that his entry was inadvisable,

and

had objected to being

prevented

from making the entry on the basis that it would be

age

discrimination should

he be so prevented.

The licensee

had

removed the flashing yellow lights from the east

and

west valve galleries of the 467'levation

RWB, without removing the

scaffolding from above the locking gate (east) or installing the

anti-tamper device (west)

as discussed

in Inspection

Report 50-397/88-28,

and as committed to by the licensee

as corrective action for a violation

of TS 6. 12.

A survey conducted jointly by the licensee

and the inspector

determined that dose rates in the east valve gallery did not exceed

1000

mr/hr at 18" from the source.

Although a similar survey in the west

valve gallery revealed

a dose rate of 1200 mr/hr at 18" from the source

on both the licensee

and

NRC instruments,

the inspector determined

upon

entering

the

room that the lock was not of the

same type as in the east

valve gallery,

and

was of a design

such that it appeared

to adequately

prevent unauthorized entry (the lock could not be operated

from either

side without a key).

The

HPT accompanying

the inspector

and the

HP

Supervisor

had not previously been

aware of the type of lock used.

The matter described

above

was discussed

with the

HP Supervisor,

who

stated that the scaffolding would be removed

as

soon

as possible

and that

in spite of the non-tamper

nature of the lock on the west valve gallery,

a non-tamper

screen

would still be installed.

Licensee

procedure

PPM 1. 11.3, Health

Ph sics

Pro ram, Revision 4, dated

4-4-88, provides authority to HPTs to stop work or otherwise direct the

activities of others

under their surveillance.

During a walkdown

inspection

by the licensee,

performed to confirm material condition of

the primary containment

and to verify repairs to reactor

coolant

boundaries, it was observed that the Shift Support Supervisor

(SSS) did

not quickly respond to requests

by the

HPT assigned

as escort in the high

radiation area.

Several

times the

HPT requested

that he and another

individual pass

through or quickly exit very high radiation fields.

The

HPT repeated

one

such request

three times before the

SSS complied.

Efforts to work expeditiously appeared

to be affected

by a lack of

familiarity by the

SSS

and operator with the location of some of the

components

being inspected.

The inspector

expressed

concern to the Shift Manager

(SM) that personnel

appeared

to be unresponsive

to

HP requests

during work involving very

high radiation

dose rates.

The

SM stated that the matter would be

discussed

with the

SSS.

During the walkdown of the

D/W noted above,

on September

6, 1988, the

inspector

and

a resident

inspector

had accompanied

licensee

personnel.

The reactor

was at approximately

3X power in order to maintain

temperature

and pressure

consistent with the normal operating condition

of the components

which were repaired during the outage.

Access controls

and

HPT coverage

were observed

to be consistent with licensee

procedures.

While in the

D/W, the inspector

observed that

some equipment

and

materials

remained in the

D/W, apparently left over

from the outage

work.

The material

was brought to the attention of the

SM after the inspectors

exited the

D/W.

Subsequent

to that

D/W inspection,

the licensee

shut

down the reactor

and

performed minor corrective maintenance

in the

D/W, then started

the

reactor

and conducted

a subsequent

3X power (1000 psi reactor pressure)

entry and walkdown.

The inspector again accompanied

the licensee,

and

noted that most of the material previously observed

had remained in the

D/W.

As the

HP, the operator,

and the inspector were about to exit the

548'levation of the

D/W, the inspector

asked the operator if the

material visible on that elevation

was allowed to remain in the

D/W

during operation of the reactor.

He stated that it was not,

and the

following material

was

removed:

2 pieces of 3/4" rope approximately 25'ong

1 piece tangled bailing wire

1 desk telephone with approximately 100'f cable

1 piece of U-channel

bracket,

approximately

2" x 2" x 14"

1 extension light, bagged in yellow polyethylene plastic

2 small plastic bottles

(empty)

2 small plastic

bags containing debris

Additionally, a string of waterproof lights had been

observed at the

handrail

near

the

2A2 recirculation

pump motor.

This light string

appeared

capable of withstanding

D/W conditions during operation,

and was

attached

to the handrail with plastic tie-wrap type looms.

This was not

removed prior to reactor

power operation..

The matter

was discussed

with the licensee.

The licensee

stated at the

exit interview that they were aware of no specific analysis of material

left in the

D/W during operation, with respect to internal missile

hazards,

downcomer restriction, or equipment

impairment.

The Final

Safety Analysis Report

(FSAR) does

not address

the situation of unsecured

material

being left in the

D/W.

Given the small

volume of material,

and

based

on discussion with the Region

V Reactor Projects

Section Chief, it

was later determined that the safety significance

from the above noted

Revision 9, dated 5-29-87,

does

not address

specific areas

as to

responsibility.

It states

that responsibilities

are divided among work

groups

based

on normal

occupancy.

The

D/W is not a normally occupied

area during operation.

No other licensee

procedures

appeared

to address

the issue.

The resident

inspectors will continue to conduct routine

inspection of this area.

Surveys of material exiting the Radiologically Controlled Area

(RCA) were

observed.

Examples of equipment

being briefly surveyed

were observed.

The extent of each survey appeared

to be dependent primarily upon the

amount of material to be surveyed, i.e.,

more material

received less

surveying per item.

This was discussed

with lead

HPTs on shift at the

time of the observations,

who then issued instructions to be more

thorough.

With the exception of the matter discussed

in paragraph

3, radiological

postings

were observed to be in compliance with 10 CFR 20.203,

Caution

si

ns

labels

si nals

and controls.

The licensee's

program appeared

capable of meeting the safety objectives.

No violations or deviations

were identified.

Exit Interview

The inspector

met with those individuals denoted in paragraph

1 at the

conclusion of the inspection

on September

9, 1988.

The scope

and

findings of the inspection

were summarized.

The licensee

acknowledged

the apparent violation discussed

in paragraph

4, above.

The licensee

was

informed that the unsecured

material in the primary containment during

operation

was considered

to be an unresolved

item.

Subsequent

post-inspection

review resolved the matter

as noted in paragraph

5,

above.