ML17264A186

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Insp Rept 50-244/95-15 on 950730-0909.No Violations Noted. Major Areas Inspected:Plant Operations,Maint,Engineering, Plant Support & Safety Assessment/Quality Verification
ML17264A186
Person / Time
Site: Ginna Constellation icon.png
Issue date: 09/29/1995
From: Lazarus W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17264A185 List:
References
50-244-95-15, NUDOCS 9510110047
Download: ML17264A186 (28)


See also: IR 05000244/1995015

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION I

Inspection Report 50-244/95-15

License:

DPR-18

Facility:

Inspection:

Inspectors:

R.

E. Ginna Nuclear

Power Plant

Rochester

Gas

and Electric Corporation

(RG&E)

July 30,

1995 through September

9,

1995

P.

D. Drysdale,

Senior Resident

Inspector,

Ginna

E.

C. Knutson,

Resident

Inspector,

Ginna

E.

H. Gray, Chief, Non-Destructive Engineering Section,

Region I

A. R. Johnson,

Ginna Project Manager,

NRR

Approved by:

az~rus

ie

,

eac or

roJects

ection

P8~

~s

Kaae

INSPECTION SCOPE

Plant operations,

maintenance,

engineering,

plant support,

and safety

assessment/quality

verification.

95iOii0047 95i003

PDR

ADQCK 05000244

6

PDR

INSPECTION EXECUTIVE SUNMARY

Operations

The plant operated

at full power (approximately

97 percent) for the majority

of the inspection period.

During this period,

a lightning strike caused

a

momentary loss of two of the four class

1E electrical

buses.

Corrective

maintenance

had

been performed

on the associated

emergency diesel

generator

(EDG) earlier that day; although administratively inoperable at the time of

the event,

licensee

management

had earlier made the decision to defer

acceptance

testing

and to place the

EDG in automatic

standby

due to impending

storm conditions.

As a result,

the

EDG was available during the event.

The

EDG started

and loaded normally,

and all other engineered

safety features

equipment functioned

as required.

The event

had

no effect on reactor

power.

The operators

responded

well to the event.

management's

decision to make the

EDG available prior to performance of acceptance

testing

was prudent.

Later in this period, the shift supervisor directed that the reactor

be

manually tripped from approximately

70 percent reactor

power due to a

secondary

plant transient that was caused

by the loss of power to

a main

circulating water

(CW) pump.

All engineered

safety features

equipment

functioned

as required

and operators

promptly stabilized the plant in hot

shutdown.

The shift supervisor's

decision to manually trip the reactor

was

appropriate.

Operator response

to the transient

and reactor trip was good.

management effectively integrated resolution of

CW pump motor failure and

other secondary plant technical

issues with plans for plant restart.

The

licensee's

decision to also inspect the unaffected

CW pump was prudent

and led

to identification of a malfunction that would otherwise

have gone undetected.

Naintenance

As a result of maintenance activities to correct low fuel oil pressure

on the

B-emergency diesel

generator,

the licensee

determined that the replacement

fuel

pump model that was specified in the vendor manual

required modification

to produce the desired

discharge

pressure.

Although the required value of

fuel oil pump discharge

pressure

is engine-spe 'fic, the licensee

issued

an

interim notice to the

NRC of the problem in accordance

with 10 CFR Part 21.

RG&E had obtained

spare

replacement

pumps through

a commercial

procurement

process

and later dedicated

them for nuclear service.

All of the

pumps that

had

shown reduced

performance

when installed

on the

EDG had

been successfully

tested

by RG&E prior to being released

to the spare parts

system,

raising

questions

regarding the adequacy of commercial

grade dedication testing.

The

licensee

indicated that

a review of the procurement

and dedication

processes

will be conducted

as part of the root cause evaluation.

During routine surveillance testing of the undervoltage

(UV) protection

system,

the practice of testing

a malfunctioning indicating light by using

a

nearby "working" indicating light bulb produced

an alarm indication of a

possible loss of undervoltage protection for safeguards

bus

17.

The

B

EDG was

started

and connected

to bus

17 to assure

the continued availability of

undervoltage

protection during troubleshooting.

The cause

was subsequently

determined to be that the indicating light in question

had

been tested with an

(EXECUTIVE SUNNRY CONTINUED)

incompatible light bulb, which caused

a fuse in the indicating light circuitry

to blow.

The undervoltage protection function of the cabinet

had not been

affected,

and therefore,

operability of the

UV cabinet

had not been lost as

a

result of this event.

Corrective action included listing all the various indicating lamps of all 480

VAC UV relay and control cabinets

under the applicable

equipment

identification numbers

(EINs).

The licensee

also conducted training on this

incident for all Results

and Test Department

personnel

to review its causes

and corrective actions.

The inspector considered

that the potential for a

problem similar to this incident existed in other electrical

maintenance

and

test areas.

The licensee

subsequently

agreed to review the standard

practices

for troubleshooting

indicator light faults

and to expand training on the event

to include

I&C technicians

and electrical

maintenance

personnel.

The licensee

has experienced

water leakage into the residual

heat

removal

system

pump room for several

years.

The inleakage is currently too small to

represent

any operational

safety concern for the plant.

All potential

sources

of the leakage

have not yet been positively identified by the licensee.

Ground water appears

to be entering the room; however,

RG&E's analyses

also

indicate the presence

of boric acid and radionuclides that are also present

in

the spent fuel pool.

The licensee is removing the scale buildup from the area

of inleakage to facilitate better collection.

The inspector will continue to

monitor licensee efforts to quantify the water inleakage rate

and to

positively identify all sources.

The licensee is planning to replace

both steam generators

(SGs) during the

next refueling outage,

currently scheduled

to begin in Harch

1996.

The

inspectors

are monitoring the licensee's'reparations

for SG replacement

and

are reviewing the effectiveness

of RG&E's project management

controls, the

safety evaluations

prepared for the project,

and the engineering

specifications

associated

with the

new SGs.

During this period, the

NRR and

Region I-based Project Managers visited the site to obtain

an overview of the

SG replacement

project

(SGRP)

and to coordinate

inspection plans.

No areas of

concern

were identified during review of the

SGRP.

The licensee

was well

prepared

to address

questions

posed during the discussions.

Engineering

During a routine start of the D-service water

(SW) pump, the motor began to

emit smoke

and flames.

The licensee

determined that the likely cause of

failure was

a phase-to-ground

short circuit that developed

due to vibration-

induced degradation of the winding insulation.

A similar failure had occurred

with this motor several

years earlier,

and the motor had

been refurbished

by a

vendor

and returned to service.

On this occurrence,

the licensee

decided to

replace

the motor with a commercial-grade

motor that had

been

intended for

installation

and dedication during the next refueling outage.

The licensee

initiated

an internal engineering

action to review all of the

known new motor

characteristics,

to determine

the extent of dedication testing necessary,

and

'(EXECUTIVE SUMMARY CONTINUED)

to perform

10 CFR 50.59 safety evaluations of any necessary

plant

modifications necessary

to perform dedication testing during plant operations.

The inspector considered that the licensee

made

a sound decision to replace

the

D-SW pump motor and restore

the

pump to operability in a timely manner

through installed dedication testing.

" The new motor's performance

was

thoroughly modeled

and reviewed, with conservative

engineering

assumptions

and

ample consideration

for the existing plant design

and safety evaluations.

Plant Support

During recent months,

several

incidents

have occurred

where personnel

entering

a radiologically controlled area

(RCA) in the plant did not log into the

licensee's

radiation work permit

(RWP) access

control system,

and/or did not

have the secondary

alarming dosimetry required for entry.

None of the

incidents involved entry without the primary personnel

exposure monitoring

devices

(thermoluminescent

dosimeters);

however, all represented

a failure of

qualified radiation workers to adhere to the procedure

requirements

pertaining

to

RCA access,

RWP work controls,

and possession

of alarming dosimetry.

Although of minor radiological

consequence,

these

incidents represent

a

relatively high occurrence

over

a seven

month period of a lack of adherence

to

procedure

requirements

for radiological

work controls

and access

to radiation

and high radiation areas.

This item is unresolved

pending

NRC review of the

licensee's

human performance evaluation report

and the licensee's

implementation of permanent corrective actions.

TABLE OF CONTENTS

EXECUTIVE SUMMARY .

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ii

TABLE OF

CONTENTS

.

~

~

~

v

1.0

OPERATIONS

1.1

Operations

Over view...

1.2

Operational

Experiences

.

1.2. 1 Loss of One Offsite

1.2.2 Manual Reactor Trip

Water

Pump

~

~

~

~

~

~

~

~

~

~

~

Power Supply

due to Loss of a Main

~

~

~

~

~

~

Circul ating

1

1

1

1

2

2.0

MAINTENANCE .

2. 1

Maintenance Activities

2. 1. 1 Routine Observations

2.2

Surveillance

and Testing Activities

.

.

.

.

.

.

.

.

.

.

.

.

2.2. 1 Routine Observations

2.2.2 B-Emergency Diesel Generator

Low Fuel Oil Pressure

and

10 CFR 21 Report

2.2.3

Bus

17 Undervoltage

Cabinet Indicating Light Failure

2.3

Water Leakage Into the Residual

Heat

Removal

System

Pump

oom

R

4

5

5

5

6

7

3.0 ENGINEERING............................

8

3.1

Service

Water

Pump Motor Failure

and Subsequent

Upgrade

.

.

.

8

3.2

Steam Generator

Replacement

Project

.

.

.

.

.

.

.

.

.

.

.

.

.

9

4.0

5.0

6.0

PLANT SUPPORT

.

4. 1

Radiological

Work Controls

and External

in Radiologically Controlled Areas

SAFETY ASSESSMENT/OUALITY VERIFICATION

5. 1

Periodic Reports

5.2

Licensee

Event Reports

ADMINISTRATIVE

6. 1

Senior

NRC Management

Site Visits

.

6.2

Exit Meetings

.

~

~

~

~

~

~

~

~

~

~

~

11

Exposure Monitoring

~

~

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~

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~

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~

~

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11

13

13

13

14

14

14

DETAILS

1.0

OPERATIONS (71707)

1.1

Operations

Overview

At the beginning of the inspection period, the plant was operating at full

power (approximately

97 percent).

On August 3,

1995,

one of the two offsite

electrical

power supplies

deenergized

due to

a lightning strike.

This

resulted in a momentary loss of two of the four class

lE electrical

buses

until the associated

emergency diesel

generator

started

and

assumed electrical

loads.

All engineered

safety features

equipment functioned

as required

and

the event

had

no effect on reactor

power.

On August 25,

1995, the shift supervisor directed that the reactor

be manually

tripped from approximately

70 percent reactor

power due to a secondary

plant

transient that was caused

by the loss of a main circulating water pump.

All

engineered

safety features

equipment functioned

as required

and operators

promptly stabilized the plant in hot shutdown.

Following resolution of

several

balance-of-plant

issues,

a plant startup

was performed

on August 26,

1995.

Plant power was escalated

to 48 percent

and held pending repair of the

failed main circulating water pump.

Before this was completed,

a through-wall

pipe leak was discovered

in a moisture separator

drain line to the main

condenser.

A controlled steam plant shutdown

was conducted

on August 28,

1995, to support replacement

of the affected piping.

During this shutdown,

repairs

were also completed to the main circulating water pump.

A steam plant

star tup was conducted later the

same

day and the plant returned to full power

operation

on August 30,

1995.

There were

no other significant operational

events or challenges

during the inspection period.

1.2

Operational

Experiences

1.2.1 Loss of One Offsite Power Supply

On August 3,

1995,

the B-emergency diesel

generator

(EDG) was declared

inoperable to investigate

a decreasing

trend in fuel oil pressure;

the

maintenance activity is discussed

in detail in section 2.2.2 of this report.

By that afternoon,

maintenance

was complete

and the

B-EDG was prepared for

operation to conduct acceptance

testing.

However, licensee

management

decided

to defer testing

and to align the

B-EDG for normal operation

due to lightning

storm activity.

At 3:26 p.m.

on August 3,

1995,

a lightning strike occurred offsite on one of

the plant's

two offsite electrical

power circuits (circuit 751).

As a result

of the transient, circuit 751

was deenergized

by protective relays at offsite

station

204.

This resulted in a loss of power to the two class

1E 480-volt

electrical

busses

that were being supplied

by circuit 751

(busses

16 and 17).

In response

to the power loss,

the

B-EDG automatically started

and reenergized

the two busses.

Operators

responded

in accordance

with abnormal

procedure

AP-

ELEC. 1, "Loss of 12A and/or

12B Busses,"

to stabilize affected

systems.

All

engineered

safeguards

equipment functioned

as required

and plant power was not

affected

by the transient.

At 4:28 p.m., the electrical distribution system

was realigned

such that the

unaffected offsite electrical

power circuit (circuit 767)

was supplying all

four class

lE 480-volt electrical

busses.

The

B-EDG was shut

down and

returned to standby.

Circuit 751 was returned to service at 4:44 p.m.;

however,

the circuit was not placed in service

due to continued

storm

activity.

Based

on control

room observations,

review of logs,

and discussions

with plant

personnel,

the inspector determined that operators

had responded

appropriately

to the loss of circuit 751.

The inspector

observed

good procedural

adherence

during plant restoration.

Operator communications

were formal

and concise.

The Control

Room Foreman provided excellent oversight of the restoration

activities.

Additionally, licensee

management's

decis'ion to defer

EDG

acceptance

testing

due to storm activity was prudent.

The technical

specification requirements for one

EDG being inoperable

had

been satisfied

prior to the event,

and loss of one offsite power supply does not alter these

requirements.

A four-hour

non-emergency

report was

made to the

NRC as

required

by 10 CFR 50.72.

1.2.2 Manual Reactor Trip due to Loss of a Main Circulating Water

Pump

The main circulating water system supplies cooling water to the main

condensers

to condense

exhaust

steam

from the two low pressure

turbines.

The

system consists of two headers,

each of which is supplied

by a circulating

water

(CW) pump.

Each header

supplies

a main condenser.

The headers

are

cross-connected

upstream of the main condensers

to allow for reduced

power

operations with a single operating

CW pump.

After passing

through the main

condensers,

main circulating water is returned to the lake via a common

discharge

canal.

At 5:41 a.m.

on August 25,

1995, the

B-CW pump tripped.

Control

room

operators

were alerted to the problem by the associated

main control board

annunciator.

Turbine load was rapidly reduced to approximately

50 percent in

accordance

with abnormal

procedure

AP-CW. 1,

"Loss of a Circulating Water

Pump."

Operators

then noted that turbine backpressure

in the condenser

associated

with the failed

CW pump (B-main condenser)

was increasing,

and that

the normally equal levels in the main condenser

hotwells were diverging;

specifically, hotwell level in the B-main condenser

was decreasing,

while

level in the other hotwell (associated

with the operating

CW pump)

was

increasing.

These

abnormal

conditions were developing

because

the

B-CW pump had tripped

rather

than having

been

secured

as part of an orderly transition to single

CW

pump operation.

Although the plant can operate

at up to 50 percent

power on

a

single

CW pump, the. system must first be reconfigured; specifically, the

discharge isolation valve for the

pump to be secured

must be closed before the

CW pump is stopped.

In this case,

the discharge

isolation valve was initially

open

when the

B-CW pump stopped.

The valve is motor operated

and

automatically

began to close

when the

B-CW pump tripped;

however,

closure of

this large valve takes

on the order of minutes.

As

a result,

cross-connected

flow from the

A-CW pump discharged

back to the idle B-CW pump rather than

being forced through the B-main condenser.

The loss of cooling water caused

pressure

in the secondary

side of the B-main condenser

to increase.

The two

main condensers

connect to a

common suction header for the main condensate

pumps;

consequently,

hotwell level in the B-main condenser

dropped rapidly as

condensate

was either forced into the lower pressure

A-main condenser

hotwell

or supplied to the main condensate

pumps.

As level in the B-main condenser

hotwell approached

empty, the condensate

pumps

began to cavitate

and discharge

pressure

began to drop.

This translated

to low suction pressure

to the main feedwater

pumps.

Given the potential for

damage to secondary

plant equipment

and

a possible loss of main feedwater

flow, the shift supervisor directed that the reactor

be manually tripped.

With reactor

power at approximately

70 percent

and decreasing,

operators

tripped the reactor at 5:43 a.m.,

approximately

two minutes after loss of the

B-CW pump.

Plant response

to the trip was normal.

All safety systems

and

equipment

responded

as required.

Operators

promptly stabilized plant

conditions in hot shutdown.

Investigation revealed that the

B-CW pump breaker

had tripped due to actuation

of the

power factor relay.

The relay trip setpoint

was checked

and found to

be correctly set.

Inspection of the

8-CW pump motor revealed that

a diode in

the synchronizing circuit had

become disconnected.

The licensee

determined

that this failure would have produced

a power factor trip.

Additionally, one

of the mounting bolts for the baseplate

that attaches

synchronizing circuitry

components

to the motor rotating assembly

was found sheared

at the head.

Localized minor insulation

damage

on the stator windings was also noted.

The

licensee

theorized that when failure of this bolt occurred,

the bolt head

had

struck and broken the diode conductor;

as it continued out, the bolt head also

produced the stator winding insulation damage.

Ultrasonic testing

was

performed

on the remaining baseplate

bolts for the

B-CM pump,

and

no

indications of incipient failure were detected.

Additionally, the

A-CW pump

was shut

down for examination of the baseplate

bolts, with no problems noted.

Licensee efforts to determine

the cause of the belt failure were continuing at

the end of the inspection period.

Following replacement

of the failed bolt and diode,

and repair of the stator

winding insulation,

an operational

test of the

8-CW pump was attempted.

This

test

was unsuccessful,

with the motor breaker

again tripping on actuation of

the power factor relay.

Additional troubleshooting

revealed that

a modul'e in

the synchronizing circuit was defective.

Following replacement

of this

module, the

B-CW pump was tested satisfactorily

and returned to service.

Although no problems

had previously been experienced

with the

A-CW pump, it

also failed to start following completion of the bolt inspection.

Troubleshooting

revealed that the

same synchronizing

module that had failed in

the

B-CW pump was also malfunctioning in the

A-CW pump.

Both pump motors

had

been refurbished during the

1995 refueling outage,

and the licensee

suspected

that heating during application of varnish to the rotors

may have contributed

to failure of the synchronizing modules.

A second

replacement

module was not

immediately available.

Licensee

management

decided that the plant would be

returned to operation,

with power limited to 50 percent until the

A-CW pump

could be returned to service.

A reactor startup

was

commenced

on August 26,

1995,

and criticality was

achieved at 1:53 p.m.

The main generator

was closed

on the grid at 5:56 p.m.,

and plant power was raised to approximately

50 percent

by morning of the

following day.

On August 28,

1995,

a steam plant shutdown

was performed to

support repair of a through-wall pipe leak in a moisture separator

reheater

drain line.

The reactor

was maintained critical during this maintenance.

Coincident with the shutdown,

a replacement

module for the

A-CW pump motor

synchronizing circuit was obtained

and installed.

A steam plant startup

was

conducted later the

same day,

and full power was achieved at 2:44 a.m.

on

August 30,

1995.

The inspector considered that the licensee's

action to manually trip the

reactor following loss of the

B-CW pump was appropriate.

Through discussions

with licensee

personnel,

review of archived plant data,

and attendance

of the

post trip review meeting,

the inspector

concluded that operators

had responded

well to the reactor trip and that the plant had responded

normally.

No

technical specification requirements

had

been violated,

and

no technical

issues

related to the reactor plant were identified.

A four-hour non-

emergency report was

made to the

NRC as required

by 10 CFR 50.72.

Licensee

management effectively integrated resolution of the

B-CW pump motor failure

and other secondary

plant technical

issues with plans for plant restart.

The

licensee's

decision to also inspect the

A-CW pump was prudent

and led to

identification of a malfunction that would otherwise

have gone undetected.

2.0

NAINTENANCE (62703,

61726)

2. 1

Naintenance Activities

2. 1.1 Routine Observations

The inspector

observed

portions of plant maintenance activities to verify that

the correct parts

and tools were utilized, the applicable industry code

and

technical specification requirements

were satisfied,

adequate

measures

were in

place to ensure

personnel

safety

and prevent

damage to plant structures,

systems,

and components,

and to ensure that equipment operability was verified

upon completion of post maintenance

testing.

The following maintenance

activities were observed:

~

Placement of the

new D-SW pump motor (observed

August 15,

1995),

motor

power cable junction box modification (observed

August 21, 1995),

and

motor/pump commercial

grade dedication

and acceptance

testing

(observed

August 24,

1995).

The inspector

concluded that the above activities were performed in a well

controlled manner

and that the maintenance craft actions to install the

new

pump motor

and to perform the required

acceptance

test represented

good

quality performance.

2.2

Surveillance

and Testing Activities

2.2. 1 Routine Observations

Inspectors

observed portions of surveillances

to verify proper calibration of

test instrumentation,

use of approved

procedures,

performance of work by

qualified personnel,

conformance to limiting conditions for operation

(LCOs),

and correct system restoration

following testing.

The following surveillances

were observed:

~

PT-12.2,

"Emergency Diesel

Generator 8," observed

August 6,

1995

~

PT-36M-D, "Standby Auxiliary Feedwater

Pump

C - Honthly," observed

August 16,

1995

~

PT-12. 1,

"Emergency Diesel

Generator

A," observed

September

5,

1995

The inspector determined

through observing the above surveillance tests that

operations

and test personnel

adhered

to procedures,

test results

and

equipment operating

parameters

met acceptance

criteria,

and redundant

equipment

was available for emergency

operation.

Additionally, during

an inspection of the

8-EDG following the performance of

PT-12.2

on September

7,

1995,

the inspector noted that the prelubricating oil

pump was not running.

This pump runs at all times when the

EDG is shutdown in

standby,

and provides engine lubrication during startup

and shutdown.

The

inspector reported the problem to the shift supervisor,

and the

8-EDG was

declared

inoperable.

Troubleshooting

revealed that the

pump motor start relay

had failed.

This suggested

that the motor may never have started after the

EDG had

been

secured

at the conclusion of PT-12.2.

The relay was replaced

and

the

EDG was returned to service later that day.

As corrective action, the

licensee

is modifying PT-12. 1 and -12.2 to include

a verification that the

prelubricating oil pump is running after the 'EDG is secured.

2.2.2 B-Emergency Diesel

Generator

Low Fuel Oil Pressure

and

10 CFR 21 Report

On August 3,

1995, the 8-emergency

diesel

generator

(EDG) was declared

inoperable to investigate

a decreasing

trend in fuel oil pressure.

Normal

fuel pressure

is 38-45 psig, but pressure

had decreased

in July 1995 to the

licensee's

alert range alert limit of 35 psig.

In August 1995, pressure

decreased

below the action limit of 32 psig at full diesel

load.

The licensee

completed

maintenance

on the fuel oil system the

same afternoon

by replacing

system filters, check valves,

the pressure regulating/relief valve,

and

flexible fuel lines.

The inspector witnessed

the post maintenance

acceptance

testing

and observed that fuel oil pressure

remained

below the action limit

with the diesel fully loaded.

During the test,

the licensee's

attempts to

adjust the pressure

higher w'ere not successful.

Consequently,

the licensee

replaced

the fuel

pump with a new spare

from stock and retested

the diesel.

No pressure

improvement

was observed with the

new pump.

The licensee

again

replaced that

pump with another

new spare

pump,

and repeated

the test,

but no

improvement in fuel pressure

resulted.

The licensee

held discussions

with the diesel

vendor to confirm that the fuel

pump was the correct

model (Tuthill Hodel

2CF-CC)

and to investigate other

possible

causes

for the low pressure.

However, the vendor technical

manual

indicates that fuel

pump performance

can

be improved by removing shims from

the

pump cover gasket.

The licensee

investigated this option and determined

that end play in both of the replacement

pumps

was larger than the minimum

specified in the vendor manual,

and larger than the end play in another

spare

pump

known to have

good pressure.

Cover gasket

shims were removed

from the

replacement

pumps to reduce

end play,

and the diesel

was retested.

The test

was successfully

completed

when fuel pressure

was restored to 55 psig at no

load and 44 psig at full load.

On August 28,

1995, the licensee

issued

an interim notice to the

NRC of the

problem in accordance

with 10 CFR Part 21, indicating that

a full written

report would be forthcoming by September

25,

1995.

The preliminary

information supplied

by

RG&E indicated that the fuel

pump was

an exact

replacement

(by model

number) for the original

pump that the licensee

had

tested to meet the performance

requirements

established

by the original

manufacturer.

The safety concern

noted

by

RG&E that warranted

a

10 CFR Part 21 report was that the diesel

may not have

been able to maintain its design

loading with reduced

fuel pressure

from similar pumps

on

EDGs at other nuclear

facilities.

Although the diesel

manufacturer

does not specify

a minimum fuel

pressure

for operability, the actual

lower limit varies

from diesel

to diesel

and

had not been established

for the

EDGs at Ginna.

RG&E obtained their spare

replacement

pumps through

a commercial

procurement

process

and later dedicated

them for nuclear service with a shop test using the pumps'riginal

performance specifications.

All of the

pumps that

showed

reduced

performance

when installed

on the

EDG had

been successfully tested

by RG&E prior to being

released

to the spare parts

system.

The reason for this discrepancy

has not

yet been determined.

The inspector discussed

with the licensee

the potential for procurement or

commercial

grade dedication

issues that may have contributed to the degraded

fuel

pump performance.

The licensee

shared

these

concerns

and indicated that

a review of the procurement

and.dedication

processes will be conducted

as part

of the root cause

evaluations

performed through the action report process that

was used to pursue the

pump pressure

problem.

2.2.3

Bus

17 Undervoltage Cabinet Indicating Light Failure

On August 9,

1995, the licensee

was performing

a regularly scheduled

surveillance test

(PT-9.1. 17),

"480

VAC Undervoltage Protection,"

on

safeguards

bus

17.

During the test,

Results

and Test Department technicians

noted that the lamp for the "125

VDC Normal" indication on the undervoltage

(UV) relay cabinet

panel

was not lit as expected.

A technician put

a spare

bulb into the socket,

which lit up momentarily,

but then blew out.

The

technician

then

used

an adjacent

working bulb from the

"120 VAC Normal"

indicator on the cabinet

panel to again "test" the socket.

This bulb also

blew out and caused

a

DC control voltage failure alarm for the bus

17

UV

cabinet to annunciate

in the plant's control

room.

The technicians

and plant operators

immediately notified their supervision of

this condition,

who in turn discussed

the situation with the Plant Production

Superintendent,

the Operations

Hanager,

and the System Engineer.

Loss of UV

protection

on safeguards

bus no.

17 for greater

than

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> requires

an entry

into technical specification

LCO 3.0. 1,

and immediate initiation of a plant

shutdown.

The Plant Superintendent

concluded that the operability of the

UV

cabinet

was not assured

under the existing conditions

and determined that the

B-EDG should

be started

and connected

to bus

17 as

a conservative

action to

assure

the continued availability of normal

power and undervoltage protection

to bus 17.

An entry into the action statement for TS 3.0.1

was therefore not

required.

The licensee

generated

action report

AR 95-0249 to review the causes

of this

incident

and to initiate maintenance

actions to troubleshoot

and repair the

faulty indicator lamp problems.

It was determined that the control

room

trouble alarm resulted

from a blown cabinet fuse (F-1) after arcing in the

AC

socket

was caused

by the installation of a

DC bulb.

The F-1 fuse conducts

120

VAC from instrument

bus

16 to the bus

17

UV cabinet

and energizes

the panel

indication lamps only, without affecting the 480

VAC UV protection function of

the cabinet.

Oper ability of the

UV cabinet

was therefore not lost as

a result

of this event.

However, the F-1 fuse

was replaced,

the proper bulb was

installed in the "125

VDC Normal" socket,

and

PT 9. 1. 17 was completed

satisfactorily before the

B-EDG was secured

and normal

power restored to the

bus

17

UV cabinet.

The licensee dispositioned

AR 95-0249

by listing all the various indicating

lamps of all 480

VAC UV relay and control cabinets

under the applicable

equipment identification numbers

(EINs).

This was done to assure that bulbs

drawn from spare parts

and used to replace faulted bulbs

on

UV cabinets

would

have the required electrical characteristics

confirmed by Procurement

Engineering.

The licensee

also conducted training on this incident for all

Results

and Test Department

personnel

to review its causes

and corrective

ac'ions.

The inspector discussed

with the licensee

the apparent fact that it

was not unusual

for

ILC technicians

and electrical

maintenance

technicians

(both at

RG&E and industry-wide) to "borrow" light bulbs from adjacent

locations to test whether indicator light problems

were "bulb-related" or

"socket-related."

The licensee

agreed that the potential for a problem

similar to this incident existed in other electrical

maintenance

and test

areas,

and stated that

a review would be performed

and any appropriate

changes

made to the standard

practices for troubleshooting indicator light faults.

Training on the bus

17

UV cabinet incident was subsequently

planned for I&C

technicians

and electrical

maintenance

personnel

to preclude this practice.

2.3

Mater

Leakage Into the Residual

Heat Removal

System

Pump

Room

The licensee

has experienced

water leakage into the residual

heat

removal

(RHR) system

pump room (located in the sub-basement

of the Auxiliary Building)

for several

years.

Water has

been leaking from the

seam

between

the top of

the

RHR pump room west wall and the bottom of the Auxiliary Building basement

floor.

The leakage rate is very low, i.e., less than O.l gallon per day;

however,

as

a result of the long term leakage,

hard scale deposits

(several

inches thick) have

formed

on the wall.

The inleakage is currently too small

to represent

any operational

safety concern for the plant.

All potential

sources of the leakage

have not yet been positively identified.

by the licensee.

Ground water appears

to be entering the room; however,

RGSE's

analyses

also indicate the presence

of boric acid and radionuclides

that are also present

in the spent fuel pool.

The licensee is removing the

scale buildup from the area

around the

seam to facilitate better collection of

the water before it flows down the wall.

The inspector will continue to

monitor licensee efforts to quantify the water inleakage rate

and to

positively identify all sources.

(IFI 50-244/95-15-01).

3.0

ENGINEERING (71707,

37551)

3. 1

Service Water

Pump Rotor Failure and Subsequent

Upgrade

On August 9,

1995, the licensee

performed

a normal biweekly transfer of

operating service water

(SW)

pumps to place the

D-SW pump

(one of four

installed) in service

and to remove the

B-SW pump (both connected

to the

same

power supply).

Approximately 10-15 seconds

after starting the

D-SW pump, the

auxiliary operator stationed

at the

pump noticed

smoke

and flames emanating

from the motor and immediately notified the control

room operators

to secure

the pump.

The

pump was effectively secured,

and the

smoke

and flames at the

motor ceased.

No apparent effects resulted

from this event in other plant

equipment

connected

to the

same

power supply,

and

no apparent

damage resulted

to any equipment located adjacent to the

D-SW pump.

The Ginna technical

specifications

do not require entry into an

LCO action statement after the

loss of one service water pump, or until one complete train of service water

is lost.

By design,

only one service water

pump and train is required for

accident mitigation at Ginna.

The licensee's initial root cause

analysis

indicated that

an internal short

apparently resulted

from excessive

vibration of the motor windings that

degraded

the winding insulation

and caused

localized overheating to spread

through the winding coils.

The overheating eventually cause

an internal short

to ground in the motor.

The incident represented

a near identical electrical

short

and failure of the

D-SW pump motor that occurred approximately

two years

earlier.

In that instance,

a short occurred in nearly the

same location, but

resulted

in a phase-to-phase

motor winding burnout.

Both instances

were

among

a series of service water

pump and motor failures that have occurred at Ginna

over several

years.

The licensee initially intended to return the motor to

the original manufacturer

(Westinghouse)

for an in-depth root cause

analysis

since

a problem was suspected

with the materials

and processes

used the last

two times the motor was rewound

(1993

and 1994).

However, the motor remains

onsite pending

a management

decision to rewind the failed motor or purchase

a

new one.

The licensee

did not have

a spare

motor that was immediately available for

replacement,

and

a search for motors nationwide resulted

in no suitable motors

available in a short time period.

A rewind of the failed motor would have

taken

a few weeks,

and purchase of a new safety-related

motor was expected

to

take several

months.

The licensee

had previously procured

an alternate

replacement

motor that was located in the site warehouse.

However, the motor

was

a commercial

procurement

item intended for installation

and dedication

during the next refueling outage in Harch/April 1996.

The licensee

determined

that the spare

motor could be inspected,

installed,

and dedicated to safety-

related service

as

a replacement for the failed motor.

Since limited test

data that could be validated

was available

from the motor vendor (U.S.

Motors),

and since the

new motor was not identical to the failed motor (350

H.P.

and 460

VAC new vs.

300 H.P.

and 440

VAC old), the licensee initiated

internal engineering

actions to analyze all of the

known new motor

characteristics,

to determine the extent of dedication testing necessary,

and

to perform

10 CFR 50.59 safety evaluations of any plant modifications

necessary

to connect the

new motor to safeguards

bus

17 and perform dedication

testing during plant operations.

The licensee

developed

Plant

Change

Request

95-046

and Design Analysis

DE-EE-95-129-06 to evaluate the potential effects

on installed plant equipment

of the

D-SW pump replacement.

The analysis

reviewed the critical motor

characteristics

such

as the inrush, full load,

and fault currents;

motor

acceleration

time; steady state

and dynamic responses

during safeguards

sequencing;

and degraded

voltage performance

during normal

and accident

conditions.

The analysis

also considered

the effects of the

new motor on the

existing power circuit breaker,

the safeguards

bus

17,

and the

B-EDG under

worst case loading scenarios.

RG&E concluded

hat the

new motor's expected

performance

under accident conditions

was

bounded

by existing safety analyses,

and was based

on thorough analysis that was validated through testing.

The

inspector considered

the analysis to be in-depth,

and comprehensive

in

addressing

concerns

related to the safe installation

and testing of the motor

with the plant at power.

After a seismic analysis

concluded

the

new motor was acceptable

for use, it

was installed

on the

D-SW pump.

Some modifications were

made to the power

cables

and the bearing temperature

instrument wiring.

Complex test

instrumentation

was installed

on the motor to obtain performance

data

and to

permit detailed engineering

analysis of the test results.

Preliminary motor

testing

was performed with the motor uncoupled

from the

D-SW pump in order to

obtain accurate inertial

and torque reaction data,

and to validate the

licensee's

motor performance

model.

The motor was then coupled to the

pump

and tested

under normal operating conditions for an extended

period.

The test

results indicated that the motor performed

more efficiently, drew less

current,

and operated

at

a lower temperature

than the old motor.

The

hydraulic characteristics

of the

D-SW pump were unchanged with the

new motor.

The inspector concluded that the licensee

made

a sound decision to replace the

D-SW pump motor and restore

the

pump to operability in a timely manner through

dedication testing.

The new motor's performance

was thoroughly modeled

and

reviewed, with conservative

engineering

assumptions

and ample consideration

for the existing plant design

and safety evaluations.

3.2

Steam Generator

Replacement

Project

The licensee

is planning to replace

both steam generators

(SGs) during the

next refueling outage,

currently scheduled

to begin in March 1996.

A special

Cl

10

crane will be used to move the

SGs into and out of containment

through two

openings that will be made in the containment

dome.

The dome will then

be

restored

and

a full-strength pressure

test of the containment building will be

performed.

The old SGs will be stored

on site in a newly constructed

temporary storage facility.

The inspectors

are monitoring the licensee's

preparations

for SG replacement

and are reviewing the effectiveness

of RG&E's project management

controls,

the

safety evaluations

prepared for the project,

and the engineering

specifications

associated

with the

new SGs.

Hajor construction activities for

the project to date

have included:

~

Installation of the two concrete

foundations for the

SG lift crane

(a

Lampson Transi-Lift crane).

Fabrication of a full-thickness containment

dome mockup.

This structure

is sufficiently large to accommodate

the actual

size

and geometry of one

opening

as it will be made in the containment

dome.

The construction

details of this mockup (steel-reenforced

concrete with a steel liner)

closely simulate the actual

containment

dome.

The mockup will be used

for testing, refining,

and proving excavation

and reconstruction

techniques,

and will also

be used for personnel

training.

Construction of the Old

SG Storage Facility (OSGSF).

Rerouting of various site services

and construction of several

onsite

support facilities.

The

NRR and Region I-based Project Hanagers visited the site to obtain

an

overview of the

SG replacement

project

(SGRP)

and to coordinate

inspection

plans with the

NRC Senior Resident

Inspector.

Discussions

were held with RG&E

and Bechtel

managers,

supervisors,

craftworkers

and quality assurance

personnel

on the project team.

Procedures

and specifications

related to the

project were sampled for review.

Work in progress

and sites of planned work

were observed.

From these discussions,

reviews

and observations, it was found

that the

SGRP is being conducted

by a team of utility and contractor

personnel,

using the experiences

gained through completion of similar

projects,

in preparation of detailed plans

and procedures

to accomplish the

SG

replacement.

The work in progress

showed careful attention to detail; for

example,

the manufacturing of the

new

SGs

was being covered

by a full time

licensee quality inspector in residence

at the fabrication plant.

Aspects of the project that were reviewed or observed

included

an overview of

the project, the lifting equipment

(Lampson

and tower cranes),

the containment

dome mockup,

dome cutting plans,

welding training/qualification plans,

the

Lampson crane foundations,

a video/computer-photographic

tour of containment

in the project affected areas,

the measurement

method, controls

on

SG

fabrication,

the

OSGSF,

SG transportation

to the site,

secondary

side water

chemistry, Quality Assurance/Quality

Control involvement, the project library,

and overall project control.

11

The

NRR Project

Manager obtained

and reviewed several

licensee

safety

evaluations

and design criteria, including:

SEV 1019

SEV 1024

SEV 1021

SEV 1025

SEV 1018

BWNT 77-

1235965-01

DC 10034A

Containment Structural Modifications

DRAFT SG Rigging and Handling,

SG Vessel,

Piping,

and Insulation

Temporary Utilities, Services

and Shielding

Facilities Outside Containment

Replacement

Steam Generator

Safety Evaluation

Replacement

Steam Generator

Design Criteria-

Containment Structural Modifications

The licensee

is required to submit to the

NRC, for review and approval,

any

change that constitutes

an unreviewed safety question or requires

a change

in

technical specifications

(TSs).

During this inspection visit, no unreviewed

safety questions

or required

changes

to TSs were identified. If the

containment

access

is enlarged,

design reviews should

be coordinated with

NRR/ECGB, via the Project Manager,

to confirm the restored

design margin.

If

necessary,

this will be performed

by NRR in the future during the licensee's

structural integrity test

(SIT) and integrated

leak rate test

(ILRT) on the

reconstructed

containment.

No areas of concern

were identified during review of the

SGRP.

The licensee

was well prepared to address

questions

posed during the discussions.

4.0

PLANT SUPPORT

(71750)

4.1

Radiological

Work Controls

and External

Exposure Monitoring in

Radiologically Controlled Areas

During recent

months,

several

incidents

have occurred

where personnel

entering

a radiologically controlled area

(RCA) in the plant did not log into the

licensee's

radiation work permit

(RWP) access

control system,

and/or did not

have the secondary

alarming dosimetry required for entry.

None of the

incidents involved entry without the primary personnel

exposure monitoring

devices

(thermoluminescent

dosimeters);

however, all represented

a failure of

qualified radiation workers to adhere to the procedure

requirements

pertaining

to

RCA access,

RWP work controls,

and possession

of alarming dosimetry.

Three

of the documented

incidents

are described

as follows.

On April 21,

1995, during the last refueling outage,

a qualified radiation

worker entered

the containment

enclosure

(a posted

high radiation area) to

inspect work on reactor coolant system piping.

Upon exiting the containment

approximately

one hour later,

he realized that

he entered

the containme'nt

without the required

secondary

dosimetry

(ALNOR) and without signing in on the

b0

12

applicable

RWP.

The radiation protection

(RP) technician

on duty subsequently

initiated an action report

(AR 95-082) to investigate

the cause of this

incident and to initiate the appropriate corrective actions.

The worker's

exposure

during the containment entry was temporarily estimated

from the

ALNOR

dosimeter reading

(4 mR) of a coworker who accompanied

him during his entire

stay inside containment.

Subsequent

analysis of the worker's

TLD confirmed

the

4

mR exposure.

RG&E's immediate actions to address

this incident included

temporarily restricting the individual's access

to restricted

areas,

conducting interviews with other individuals in the

same work group, reviewing

the incident with all

RP personnel,

and posting signs at the

RCP access

point

to remind workers of the

RWP and dosimetry requirements for RCA entries.

RGEE's

RP department

reviewed this incident

and concluded that the Technical

Specification

(TS) requirements

(Section 6.13) were satisfied

since the TSs

allow for a group of individuals to use

a single alarming dosimeter inside

a

high radiation area.

Also, no work had apparently

been

performed outside .the

restrictions of the applicable

RWP.

However, several

plant procedures

require

that all individuals entering restricted

areas (i.e.,

RCAs) shall log into the

RWP access

control system

and obtain secondary

alarming dosimetry.

Procedure

A-l, "Radiation Control Manual," stipulates

that workers must acknowledge all

RWP requirements

by logging into the access

system

and obtaining

a secondary

dosimeter that must

be worn continuously

by each individual while inside

a

restricted

area.

Also, procedures

A-1.3, "Restricted Area Entry and Exit,"

and A-l.8, "Radiation Work Permits,"

both require worker acknowledgement

of

the radiological controls associated

with their job by logging into the

RWP

system

and obtaining alarming dosimetry prior to

RCA entry.

AR 95-082 was

closed in August 1995,

and

recommended

a longer term corrective action to

investigate

a possible link between

the

RWP and security access

systems to

prevent unauthorized

access

to the

RCA.

This was later investigated

by the

licensee,

but was not implemented

because

the two systems

are not physically

compatible.

On June

27,

1995,

an

RP technician discovered that

a qualified radiation

worker had entered

the

RCA to work in the Intermediate Building without his

required dosimetry

(RADOS).

The worker had signed into the

RWP access

system,

indicating he had read,

understood,

and would comply with the

RWP requirements

applicable to his work assignment.

However,

he subsequently

entered

the

RCA

without taking the

RADOS dosimeter with him.

After approximately five

minutes,

the

RP technician

on duty noticed his dosimeter still at the access

control desk

and paged the worker to return to the entry point.

The

RP

technician

allowed the worker to return to the

RCA after giving him the

dosimeter,

and counselling

him on the

RWP and procedure

requirements for

possessing

a

RADOS when entering the

RCA.

The

RP technician then initiated an

action report

(AR 95-166) to investigate

the incident

and to pursue corrective

actions.

As of this inspection,

the final disposition of this

AR was not

complete.

On August 3,

1995,

a qualified radiation worker self-identified that

he had

entered

and worked in a high radiation area inside the Auxiliary Building.

After receiving

a pre-job briefing from an

RP technician,

the individual

entered

the high radiation area without his required

RADOS dosimeter.

Prior

to entering the

RCA, the individual had donned anti-contamination clothing,

13

but did not register into the

RWP electronic

access

system.

Upon exiting the

RCA, the individual discovered

his missing dosimeter

and immediately discussed

the situation with RP personnel

and his supervisor.

The worker subsequently

initiated an action report

(AR 95-0240) to investigate

the causes for this

incident and to pursue corrective actions.

RP personnel

were able to estimate

the worker's dose

from the job duration

and the radiation levels in his work

area.

His actual

exposure

was later confirmed by reading his TLD.

As of this

inspection,

the final disposition of AR 95-0240

was not complete.

On August 3,

1995,

RG&E initiated

a Human Performance

Evaluation System

(HPES)

report

(HPES 95-0240) to perform an in-depth root cause

analysis of these

three incidents

and to determine

the necessary

corrective actions to prevent

recurrences.

HPES 95-0240

was not complete

as of this inspection;

however,

the licensee's

detailed

comparison

between the security

and

RWP access

logs

indicated that twenty instances

of per'sonnel

entry into the

RCA actually

occurred without the required

secondary

dosimeter

between

January

1,

1995,

and

August 6,

1995.

Most of these

instances

also involved

a failure to log into

the

RWP system prior to

RCA entry.

The draft HPES indicated that

a turnstile

barrier could be installed to prevent

RCA access

without the necessary

entries

into the

RWP and

RADOS systems.

This initiative is considered

to be

a

positive measure

by the licensee.

However, the final root cause

evaluation

and disposition of ARs95-166

and 95-0240,

and the

HPES are still ongoing.

Although of minor radiological

consequence,

these

incidents represent

a

relatively high occurrence

over

a seven

month period of a lack of adherence

to

procedure

requirements for radiological work controls

and access

to radiation

and high radiation areas.

This item is unresolved

pending

NRC review of the

completed

HPES95-240 report

and the licensee's

implementation of permanent

corrective actions.

(URI 50-244/95-15-02)

5. 0

SAFETY ASSESSMENT/EQUALITY VERIFICATION (71707)

5. 1

Periodic Reports

Periodic reports

submitted

by the licensee

pursuant to Technical Specification 6.9.1 were reviewed.

The inspectors verified that the reports contained

information required

by the

NRC, that test results

and/or supporting

information were consistent

with design predictions

and performance

specifications,

and that reported

information was accurate.

The following

reports

were reviewed:

~

Monthly Operating

Reports for July and August

1995

No unacceptable

conditions were identified.

5.2

Licensee

Event Reports

Two Licensee

Event Reports

(LERs) submitted to the

NRC were reviewed

and the

inspector determined that the details

were clearly reported,

the causes

were

properly identified,

and the corrective actions

were appropriate.

The

inspectors

also determined that the potential safety consequences

were

properly evaluated,

the generic implications were indicated,

events that

14

warranted additional follow-up were identified,

and the licensee

met the

applicable

requirements

of 10 CFR 50.73.

The following LERs were reviewed

(Note: date indicated is event date):

~

95-006,

Loss of 34.5

KV Offsite Power Circuit 751,

Due to Offsite

Lightning Strike, Results

in Automatic Start of "A" Emergency Diesel

Generator

(June

30,

1995)

~

95-007,

Loss of 34.5

KV Offsite. Power Circuit 751,

Due to Offsite

Electrical Storm, Results

in Automatic Start of "B" Emergency Diesel

Generator

(August 3,

1995)

The inspector concluded

the

LERs met regulatory requirements

and appropriately

evaluated

the safety significance of the events.

LERs95-006

and 95-007 are

closed.

6.0

ADMINISTRATIVE

6.1

Senior

NRC Management Site Visits

During this inspection period, three senior

NRC managers visited Ginna

Station.

On August 16-17,

1995, Hr. James

C. Linville, Chief of Reactor

Projects

Branch 3, toured the site

and met with senior licensee

management.

On August 22,

1995, Hr. Thomas T. Hartin, Regional Administrator for NRC

Region

1, toured the site

and met with senior licensee

management.

On August

23-24,

1995, Hr. William J.

Lazarus,

Chief of Reactor Projects

Section

3B,

t'oured the site

and met with senior licensee

management.

6.2

Exit Meetings

At periodic intervals

and at the conclusion of the inspection,

meetings

were

held with senior station

management

to discuss

the scope

and findings of

inspections.

The exit meeting for the current resident

inspection report 50-

244/95-15

was held

on September

11,

1995.