ML17262A486
| ML17262A486 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 04/29/1991 |
| From: | Mccabe E NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17262A484 | List: |
| References | |
| 50-244-91-07, NUDOCS 9105220120 | |
| Download: ML17262A486 (19) | |
See also: IR 05000244/1991007
Text
U. S. NUCLEARREGULATORY COMMISSION
REGION I
Inspection Report 50-244/91-07
License: DPR-18
Licensee:
Facility:
Inspection:
Inspectors:
Approved by:
Rochester Gas and Electric Corporation (RG&E)
R. E. Ginna Nuclear Power Plant
March 12 through April 15, 1991
T. A. Moslak, Senior Resident Inspector, Ginna
N. S. Perry, Resident Inspector, Ginna
P. P. Sena, Reactor Engineer, PB3, DRP
E. C. McCabe, Chief, Reac'tor Projects Section 3B
INSPECTION SCOPE
wjell>
Date
Plant operations, radiological controls, maintenance/surveillance,
security, engineering/technical
support, and safety assessment/quality
verification.
OVERVIEW
Rf llg y* 'gyH
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from a leaking secondary neutron source.
Mid-loop operations were rigidly controlled.
R~dil
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outage activities to minimize personnel exposures
and contaminations.
Maintenance/Surveillance:
Improper coordination between the operations and maintenance
departments
resulted in the temporary loss of the Component Cooling Water System.
Emer enc
Pre aredness:
Guidance has been issued on the classification and notification
actions for already terminated events.
~ec i~rit: No discrepancies
were identified during routine security checks.
En ineerin /Technical u:
Relevant engineering procedures
have been revised to assure
timely updating of as-built drawings.
9105220120
Wi0509
ADOCy, 05000244
Q
TABLEOF CONTENTS
OVERVIEW
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TABLE OF CONTENTS......................;.................
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1.0
PLANT OPERATIONS
1.1
Operational Experiences.........
1.2
Control of Operations ......'....
1.3
Fire Protection
1.4
Valve Found Out of Required Position
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2.0
RADIOLOGICALCONTROLS
2.1
Routine Observations
2.2
ALARA(As Low As Reasonably Achievable) Program ..
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3,0
MAINTENANCE/SURVEILLANCE
3.1
Corrective Maintenance...... ~..............
3.1.1
Service Water Pump Expansion Joint Replacement
3.1.2
Valve Repacking...... -...............
3.2
Surveillance Observations............ ~.......
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4.0
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4.1
(Closed) Unresolved Item (50-244/90-31-02) EPIP Classification for SI
D1sabled
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5.0
SECURITY
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5.1
Routine Observations
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6.0
ENGINEERING/TECHNICALSUPPORT ..;..........
6.1
(Closed) Violation (50-244/90-80-02) Failure to Maintain
Drawings As Required
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7.0
SAFETY ASSESSMENT/QUALITY VERIFICATION
7.1
Periodic Reports
7.2
Written Reports of Nonroutine Events
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8.0
ADMINISTRATIVE.............
8.1
Inspection Hours ...........
8.2
ExitMeetings.....;.......
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DETAILS
1,0
PLANT OPERATIONS
1.1
Operational Experiences
At the start of the inspection, the plant was at approximately 91% power and coasting down
for the annual refueling outage.
The start of the outage was postponed from March 15 to
March 22, 1991 to allow outage support personnel, who worked long hours responding to the
March 3-4 ice storm, to prepare and train for the outage.
Operators began shutting down the
plant early on March 22, and the plant was shut down later that day.
3
After reaching cold shutdown, operations personnel conducted a hydrogen peroxide flush
(superflush) of the Reactor Coolant System (RCS) to aid in crud removal.
Following the
superflush, elevated concentrations of Antimony (Sb) 122 and 124 occurred in the RCS.
The
origin was determined to be one or more leaking Antimony-Beryllium (SbBe) secondary
neutron source assemblies
in the reactor core.
To minimize the spread of contamination and
lower personnel radiation exposures, RG&E management
decided to delay refueling until the
Chemical and Volume Control System (CVCS) could reduce these contaminants.
Allfour
secondary source assemblies were subsequently
removed 'during refueling operations and
placed in storage.
On April 3, 1991, an Unusual Event was conservatively declared when operators terminated
refueling operations and removed the Residual Heat Removal (RHR) System and the
Component Cooling Water (CCW) System from service,
This was done to stop a CCW
valve packing leak which developed during valve maintenance.
When the CCW system was
unavailable, the RHR system was started every five minutes and run for two minutes to
recirculate the coolant and trend any temperature increase.
The leak was stopped by
manually backseating
the leaking valve.
The CCW and" RHR systems were restarted
approximately 24 minutes after being removed from service, and the Unusual Event was
terminated about one hour and nineteen minutes after declaration; all required notifications
were made.
1.2
Control of Operations
Overall, the inspectors found the R. E. Ginna Nuclear Power Plant to be operated safely.
Control room staffing was as required.
Operators exercised control over access to the control
room.
Shift supervisors consistently maintained authority over activities and provided
detailed turnover briefings to relief crews.
Operators adhered to approved procedures
and
understood the reasons for lighted annunciators.
The inspectors reviewed control room log
books for activities and trends, observed recorder traces for abnormalities,
assessed
compliance with Technical Specifications, and audited selected safety-related
tagouts.
During
normal work hours and on backshifts, accessible
areas of the plant were toured.
No
inadequacies
were identified.
Cl
The inspectors monitored the plant's entry into a reduced inventory (mid-loop) condition and
subsequent
operation in this mode in preparation for removing the reactor vessel head.
The
licensee's controlling document for this condition is Operating Procedure (O)-2.3.1, Draining
and Operation at Reduced Inventory of the Reactor. Coolant System, Revision 39.
Prior to
entry into mid-loop conditions, the inspectors verified the licensee's controls assuring
containment closure capability.
Licensee 24-hour quality control coverage of plant operations
was provided while in a reduced inventory condition.
The inspector determined that the
licensee demonstrated
a conservative approach to the drain-down evolution and resulting
reduced inventory operation.
This was evident when operations personnel secured the
draining of the Reactor Coolant System (RCS) due to a discrepancy between Loop A and
Loop B hot leg level indicators LT-432A and LT-432B. Instrumentation and 'Control (1&C)
personnel vented and restored the detectors to resolve the differences.
In addition, operations
personnel manually started the "B" Emergency Diesel Generator when high wind conditions
'osed a threat to the offsite power supply during mid-loop operation.
Although no loss of
offsite power occurred, this was assessed
as a prudent licensee-initiated action to assure
continuity of power.
The licensee is issuing a voluntary LER describing these actions.
A questioning attitude was demonstrated
by licensee personnel while lowering the RCS water
level.
Errors in the draining procedure were identified by operators and resolved prior to
proceeding.
For example, Step 5.6.2 required Residual Heat Removal (RHR) Pressure
Transmitter PT-682B to be placed in service by opening Valve V-'712E.
The operator
performing the line-up noted this was a drain valve and that it should be closed.
Additionally, Step 5.11.1 required remote loop level indication to be available in the Control
Room via LT-432A and LT-432B. However, the valve lineup to place LT-432A in service
was omitted from the procedure.
Both of these discrepancies
were properly resolved with the
draining secured and RCS level available on the loop level indicators.
The inspectors determined that licensee personnel were aware of on-going plant activities and
avoided operations that could lead to perturbations to the RCS or to systems necessary
to
maintain the RCS in a stable mode during mid-loop conditions.
The Outage Coordinator
briefed site personnel during daily task planning meetings on NRC Information Notice 91-22
to sensitize them to recent industry events during mid-loop conditions.
Additionally, the
Outage Coordinator specified what tasks were stopped or rescheduled
to reduce the possibility
that on-going jobs could impact safety equipment operation.
For example, in light of recent
industry events, the access road to the 13B offsite plant switchyard was closed and the gate
locked while the plant was in a reduced inventory condition.
In addition, all maintenance
within the switchyard was prohibited by the Plant Manager to avoid any disturbances
to the
site's electrical power supplies.
The inspectors concluded that the licensee was appropriately
aware of the risks associated with the RCS being partially drained and performed the draining
evolution in a safe and conservative manner.
1.3
Fire Protection
On March 14, 1991, a continuous fire watch with backup suppression
was not established
when an auxiliary building sprinkler system was removed from service.
Prior to initiating
work, maintenance personnel notified Fire and Safety Department personnel and control room
operators as required.
Control room personnel erroneously believed that maintenance
personnel had arranged for the required fire watch.
No fire watch was established
since Fire
and Safety Department personnel were waiting for formal'notification from control room
personnel.
Operators declared the fire system inoperable, initiated the appropriate paperwork
for tracking, and disabled the system by closing and tagging an isolation valve. -After
maintenance completed work, an auxiliary operator was notified by radio to restore the
system to service.
Fire and Safety Department personnel heard the radio transmission and
contacted the shift supervisor, informing him that the required fire watch had not been
established.
A fire watch was then established,
the tags were removed and the system was
restored.
Control room personnel made the appropriate notifications and initiated a Ginna
Station Event Report.
The inspectors reviewed the circumstances
leading to this incident and determined that,
normally, after maintenance personnel request that operators hold the system, control room
personnel contact Fire and Safety personnel to arrange for the appropriate compensatory
actions.
In this instance, that did not occur.
Plant management
determined that the controlling procedures were vague concerning how the
appropriate compensatory
actions were to be arranged.
The governing Administrative
Procedure [(A)-52.4.1, Control of Limiting Conditions for Operation of Fire Spray/Sprinkler,
Fire Detection Equipment and Fire Barriers, Revision 27, effective February 13, 1991], states
that Site Contingency Procedure (SC)-3.15.17 provides instructions for posting fire watches.
SC-3.15.17 does not clearly define who is responsible, for notifying Fire and Safety personnel
to establish the required fire watch.
In this instance, the procedure used by the maintenance
personnel did have a step addressing
the establishing of a fire watch.
This maintenance
procedure [(M)-67.3, Flood Valve System Maintenance SO4 V-9242D WO9024072, Revision
11, effective January 26, 1991], requires in step 5.2 that personnel ensure that there is fire
watch coverage of the affected area in place.
Maintenance personnel signed this step,
signifying that a fire watch would be posted.
For the incident on March 14, plant management
determined that Technical Specification 3.14.3.1 was violated due to inadequate adherence
to procedures
and erroneous assumptions
made by personnel involved.
Corrective'actions included making personnel involved aware
of management
expectations,
and the appropriate procedures were changed to require formal
notifications and the posting of a fire watch prior to the removal of the system from service.
Additionally, Licensee Event Report (LER)91-003 was submitted for this event at the end of
the inspection period.
The LER willbe reviewed in a future inspection report.
The inspectors determined that formal communications between maintenance and control
room personnel on March 14 resulted in a continuous fire watch with backup fire suppression
equipment not being established within one hour as required by Technical Specification 3.14.3.1.
The violation was identified by plant personnel.,
Immediate correction was
achieved by establishing the fire watch and restoring system operability.
To prevent
recurrence,
the appropriate procedures were changed.
There is minor safety significance to
this event since the fire detection system, which alarms in the main control room, was
operable, the spray system was inoperable for a short duration, and there were personnel in
the area while the system was inoperable.
Under Section V.G.1 of 10 CFR 2, Appendix C,
no violation was cited since this event was licensee identified, of minor safety significance,
properly reported, immediate corrective measures
and actions to prevent recurrence were
appropriate, and the event was not identified as willfulor as preventable through corrective
action on a prior violation (50-244/91-.07-01).
1.4
Valve Found Out of Required Position
On March 21, 1991, Residual Heat Removal (RHR) Heat Exchanger Bypass Valve V-712A
was found out of its required (closed) position by operators during monthly surveillance (S)-
30.2, RHR System Valve and Breaker Position Verification. Subsequently,
operators closed
the valve and completed S-30.2 with no further discrepancies
noted.
As required, operators
verified that all other safeguards
systems were properly aligned by completing each system's
appropriate position verification procedure..
Plant management
determined that there was minor safety significance to this particular valve
being out of position since the valve was a manual valve in series with two other closed
valves.
Plant personnel determined that, when the system was aligned by operators after
V-712A maintenance,
V-712A was inadvertently omitted from the alignment sheet developed
from the tagging order and was therefore not checked for proper positioning.
As a corrective action, plant management
directed Operations to verify the position of all
'alves,
whether manipulated or not, within the boundaries of a tagout when restoring system
operability.
Additionally, Administrative Procedure (A)-1408, Independent Verification, was
revised to require two independent signoffs on the alignment worksheet for all valves inside
the tagging boundary.
The inspectors concluded that the alignment error was identified in a timely manner and that
the corrective actions taken were comprehensive.
Plant management
became involved shortly
after discovery and exhibited an appropriate level of concern.
Administrative procedure (A)-1408, Independent Verification, Revision 5, effective October
11, 1990, requires an independent verification whenever valves in safety-related
systems are
manipulated for maintenance.
On March 20, 1991, V-712A was not independently verified
to be in the required position after maintenance.
The out-of-position condition was identified
by plant personnel,
and immediate corrective actions were taken by properly positioning the
valve.
To prevent recurrence,
a procedure change was made requiring independent signoffs
on the alignment worksheet for all valves inside the tagging hold boundary.
There is minor
safety significance to this valve being out of position, since the valve was in series with two
other closed valves.
Under 10 CFR 2, Appendix C, Article V.G.1, a violation was not cited
since this event was licensee-identified, of minor'safety significance, properly reported,
immediate corrective measures
and action to prevent recurrence were appropriate,
and the
occurrence was not identified as willfulor as preventable through corrective action on a prior
violation (50-244/91-07-02).
2.0
RADIOLOGICALCONTROLS
2.1
Routine Observations
The resident inspectors periodically confirmed that radiation work permits were effectively
implemented, dosimetry was correctly worn in controlled areas and dosimeter readings were
accurately-recorded,
access to high radiation areas was adequately controlled, and postings
and labeling were in compliance with procedures
and regulations.
Through observations of
ongoing activities and discussions with plant personnel,
the inspectors concluded that
radiological controls were conscientiously implemented.
2.2
ALARA(As Low As Reasonably Achievable) Program
As described in Paragraph
1.2, following plant shutdown, plant management
anticipated
potential contamination and personnel exposure control problems arising from elevated
concentrations of Sb 122/124 in the RCS.
The RG&E staff consulted with another utility that
has experienced similar conditions and determined that it was prudent to delay head removal
until the Sb was substantially reduced.
Through use of CVCS ion exchangers,
the total RCS
activity was reduced from about 0.5 uC/ml to less'han 0.05 uC/ml in about 3 days.
From these actions, the inspectors concluded that licensee management
demonstrated
a strong
commitment to the ALARAprinciple.
This commitment was further demonstrated
by the
high frequency of ALARAcommittee meetings designed to review forthcoming tasks from an
ALARAperspective and to critique mock-up training to better assess radiological controls.
Additionally, Health Physics personnel actively participated in daily task planning meetings to
direct attention to contamination control concerns.
3.0
MAINTENANCE/SURVEILLANCE
3.1
Corrective Maintenance
3.1.1
Service Water Pump Expansion Joint Replacement
On March 20, 1991, the discharge expansion joint on the "D" Service Water Pump was
replaced.
Operators had noticed a deformation in the joint and requested
the replacement.
The spare expansion joint in stock appeared old, so maintenance personnel ordered new joints
and had a hydrostatic test performed prior to installation.
Maintenance management
stated
that the old expansion joint would be removed from stock.
The inspectors observed portions of the expansion joint 'replacement
and the post-maintenance
test including the leak inspection.
A quality control inspector performed a thorough leak
examination, and there appeared to be good coordination between the working groups
involved. No inadequacies
were identified.
3.1.2
Valve Repacking
On April 2, 1991, maintenance personnel began repacking Component Cooling Water (CCW)
Motor-Operated Inlet Valve V-738B to the "B" Residual Heat Removal (RHR) heat
exchanger.
Maintenance planners had prepared
a package for the activity, and operators had
held the system for the maintenance.
The valve was to be repacked with the valve backseated
since V-738B could not be completely isolated due to the CCW system configuration.
While
the old packing was being removed, a leak. developed through the remaining packing.
The
activity was immediately stopped and the control room was notified. The valve was in
mid-position.
Operators attempted to stop the leak by electrically opening {backseating) the
valve.
However, the leak rate did not decrease
since opening V-738B electrically willnot
fully backseat it.
Operators decided that they would have to stop the running CCW pump in order to access
the
valve to manually backseat it. Reactor refueling was in progress,
so that activity was
terminated first, and the running RHR pump was stopped prior to stopping the running CCW
pump.
Operators conservatively declared an Unusual Event due to the loss of CCW cooling
to the RHR system.
The leaking valve was manually placed on its backseat and the leak was
stopped.
During the loss of CCW, the RHR pump was run for two of every five minutes in
order to recirculate the coolant and trend any temperature increase.
When the plant was
returned to pre-event conditions after one hour and nineteen minutes, the Unusual Event was
terminated.
Plant management
had a Human Performance Enhancement
System (HPES) evaluation
performed to identify the root causes
and recommend corrective actions,
As corrective
action, plant management
distributed inter-office correspondence
re-emphasizing
the
requirements for checks and verifications to ensure personnel and equipment safety during
work.
Repacking valves on the backseat was highlighted, and appiopriate procedure
revisions were made or initiated.
Other corrective actions willbe tracked by the corrective
action report system.
Additionally, the Operations Manager distributed inter-office
correspondence
to operations personnel, providing information and guidance concerning valve
backseating.
Copies were also distributed to maintenance and training management for
incorporation'nto their programs.
Through interviews and document review, the inspectors determined that the hold request did:
not specify that the valve should be backseated,
the Holding Authority (Shift Supervisor) did
not properly verify the adequacy of the isolated work area as required by Administrative
Procedure (A)-1401, Station Hold Rules, Revision 25, and the Authorized Person (Hold
Requester) for the hold did not properly assure that the equipmen< was properly isolated and
it was safe to proceed with the work as required by A-1401.
Communications between
maintenance personnel and control room personnel were informal and inadequate,
in that
control room personnel did not understand
that the valve needed to be manually backseated
in
order to perform the activity, and the personnel performing the maintenance did not
understand
the condition of the equipment prior to the start of their work.
Additionally, the inspectors determined that the analogous valve in the other train of CCW
had been successfully repacked earlier on March 31, 1991, without the same problems.
In
that case, the system was also inade'quately held, but the maintenance person performing the
w'ork backseated
the valve prior to repacking it. This individual did not point out the
inadequate hold to management,
and this problem was not corrected prior to April 2.
The
inspectors noted that the lack of feedback on the first inadequate hold contributed to the
April2 event.
Technical Specification 6.8.1 requires establishment of the applicable procedures
recommended in Appendix A of Regulatory Guide 1.33, November 1972 (Safety Guide 33).
Regulatory Guide 1.33, November 1972, Appendix A,Section I, specifies that maintenance
which can affect the performance of safety-related equipment should be properly preplanned
and performed in accordance with written procedures,
documented instructions, or drawings
appropriate to the circumstances.
Administrative Procedure (A)-1401, Station Hold Rules,
Revision 25, effective March 25, 1991, requires that the Holding Authority properly verify
the adequacy of the isolated work area and that the Authorized Person for the hold properly.
assure that the equipment is properly isolated and that it is safe to proceed with the work.
Contrary to the above, on April 2, 1991, CCW valve V-738B was not properly isolated,
leading to the shutdown of the CCW and RHR systems and to the declaration of an Unusual
Event.
The maintenance activity was not properly preplanned in that the Hold Request did
not specify that the operators manually backseat the valve.
Additionally, Maintenance
Procedure (M)-37.116.3, Valve Packing, Revision 0, effective March 9, 1991, for repacking
the valve did not require maintenance personnel to verify that the valve was properly
backseated prior to the repacking.
The inadequate hold was identified by plant personnel,
and immediate corrective actions were
t'aken by manually backseating
the valve prior to,resumption of maintenance.
To prevent
recurrence, procedure changes were being reviewed and plant personnel were notified of
management
expectations concerning the establishment of a safe, isolated work area.
There
was minor safety significance to this event since the work was planned for a time during
which the reactor was in a safe condition with more than 23 feet of water above the core.
3.2
Surveillance Observations
Inspectors observed parts of surveillances to verify proper calibration of test instrumentation,
use of approved procedures,
performance of work by qualified personnel,
conformance to
Limiting Conditions for Operation (LCOs), and correct system restoration following testing.
The following surveillances were observed:
Periodic Test (PT)-2.7, Service Water System, Revision 54, effective August 24,
1990, observed March 21, 1991.
Although there were no safety significant discrepancies
noted, the inspectors observed minor
discrepancies.
Procedure direction from the person controlling the procedure and the-
sequencing through the procedure were weak.
The inspectors pointed out these observations
to Results and Test supervision and were informed that the personnel were counselled about
how they are expected to perform during surveillances.
The inspectors had no further
questions.
PT-22.10, Mechanical Manifold 'C'eakrate Test, Revision 12, effective March 30,
1990.
Activities in the control room during the surveillance were professional, with good
communications between workers.
The containment penetration leak detection test was
conducted per Technical Specification 4.4.2, which ensures
the total leakage from.all
and isolation valves does not exceed 0.60La.
La is the maximum allowable
containment leakage rate vessel test atmosphere
at design pressure (Pa).
The surveillance was
conducted by qualified and knowledgeable personnel.
The inspector noted that the procedure
was properly performed at the containment integrated leak rate test pressure of 61 (+1, -0)
psig.
Additionally, the leak test procedure properly conformed to an approved testing method
An independent calculation of the leakage by the inspector
verified that the administrative leakage limitof 50cc/min was not exceeded.
No deficiencies
were identified.
Refueling Shutdown Surveillance Procedure (RSSP)-2.3B, 'B'mergency Diesel
Generator Trip Testing, Revision 3, effective March 23, 1991, observed April 10,
1991.
S
PT-12.2, Emergency Diesel Generator
1B, Revision 63, effective April 5, 1991,
observed April 11, 1991.
The surveillances on the diesel generator were performed well by plant personnel.
During
the testing the inspectors noted good management oversight of activities at the diesel
generator.
No unacceptable conditions were identified.
4.0
EMERGENCY PREPAID)NESS
4.1
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(Closed) Unresolved Item (50-244/90-31-02) EPIP Classification for SI Disabled
This item concerned the adequacy of EPIP (Emergency Plan Implementing. Procedure)
1-0,
Ginna Station Event Evaluation and Classification, for classification of past events.
RG&E
management clarified their policy to all control room personnel and all plant personnel
qualified to serve as Emergency Coordinators.
The policy states that the NRC willbe
notified by means of the Emergency Notification System (ENS) phone any time conditions
are identified that would have warranted an Emergency Classification, but are no longer in
effect at the time of identification.
Appropriate EPIPs willbe changed
as necessary
to state
this policy.. The inspectors had no further questions.
5.0
SECURITY
5.1
Routine Observations
The resident inspectors verified that x-ray machines and metal and explosive detectors were
operable, protected area and vital area barriers were well maintained, personnel were
properly badged for unescorted or escorted
access,
and compensatory
measures
were
implemented when necessary.
No unacceptable
conditions were identified.
6.0
ENGINEERING/TECHNICALSUPPORT
6.1
(Closed) Violation (50-244/90-80-02) Failure to Maintain As-built Drawings As
Required
Following identification that procedural direction for processing vendor drawings received as
part of site-originated procurement did not exist, a Nuclear Engineering/Records
Management
Ad Hoc Group was formed to analyze this issue.
As a result, revisions were made to the
Engineering Procedures,
QE-324, Preparation,
Review & Disposition of Drawing Change
Requests,
and QE-704, Review and Approval of Vendor Design and Manufacturing Technical
'ocuments.
Inspector review found that appropriate technical direction is given in the
revised procedures to adequately control vendor drawings.
10
7.0
SAFETY ASSESSMENT/QUALITYVERIFICATION
7.1
Periodic Reports
The Monthly Operating Report for February 1991, submitted by the licensee pursuant to
Technical Specifications 6.9.1 and 6.9.3, was reviewed.
Inspectors verified that the report
contained information required by the NRC and that selected reported information was
accurate.
No unacceptable conditions were identified.
7.2
Written Reports of Nonroutine Events
Written reports submitted to the NRC were reviewed to determine whether details were
clearly reported, causes were properly identified, and corrective actions were appropriate.
The inspectors also assessed
whether potential safety consequences
had been properly
evaluated, generic implications were indicated, events warranted on-site follow-up, reporting
requirements of 10 CFR 72 were applicable and requirements of 10 CFR 73 had been met.
The following Licensee Event Reports (LERs) were reviewed (Note:
date indicated is event
date):
90-010 (Revision 1), Inadvertent Closure of "A" Steam Generator Main Feedwater
Regulating Valve Due to Controller Malfunction Causes
a Reactor Trip on Low Steam
Generator Water Level, June 9, 1990.91-001, Loss of Safeguards
Bus During Emergency D/G Monthly Load Test Due to Supply
Breakers Tripping, February 2, 1991.91-002, Loss of Offsite Power Circuit 751, Due to Ice Storm, Causes Automatic Actuation of
the ESF and RPS, March 4, 1991.
The event associated with 90-010 was reviewed in NRC Inspection Report 50-244/90-09.
Revision
1 was necessary
to update the root cause identification. The events associated with
91-001 and 91-002 were reviewed in NRC Inspection Report 50-244/91-05.
The inspectors concluded that the LERs were accurate and met regulatory requirements.
No
unacceptable conditions were identified.
8.0
. ADMINISTRATIVE
8.1
Inspection Hours
This inspection included 6 backshift and 16 deep backshift hours.
Cll
11
8.2
Exit Meetings
At periodic intervals and at the conclusion of the inspection, meetings were held with senior
station management
to discuss the scope and findings of this inspection.
In addition, NRC
exit meetings were held for the following inspections during this inspection period: 50-
244/91-03 on March 14, 1991, 50-244/91-08 on April5, 1991, and 50-244/91-09 on April
12, 1991.
The exit meeting for this inspection report (50-244/91-07) was held on April 17, 1991 with
the following individuals attending:
~me
~Titl
Harry Aurand
John Fischer
Alan Jones
Michael Lilley
Thomas Marlow
Thomas Moslak
Stanley Spector
Joseph friday
Corrective Action Assistant
Manager, Maintenance Planning & Scheduling
Corrective Action Coordinator
Manager, Nuclear Assurance
Superintendent,
Support Services
Senior Resident Inspector - NRC
Resident Inspector - NRC
Plant Manager
Superintendent,
Ginna Production