ML17262A199
| ML17262A199 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 09/30/1990 |
| From: | Dodge R, Mecredy R ROCHESTER GAS & ELECTRIC CORP. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9010250327 | |
| Download: ML17262A199 (9) | |
Text
ACCELERATED DISTIUBUTION DEMONST$&TION SYSTEM REGULATO INFORMATION DISTRIBUTIONSTEM (RIDE) r ACCESSION NBR:9010250327 DOC.DATE: 90/09/30 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G
05000244 AUTH.NAME AUTHOR AFFILIATION DODGE,R.E.
Rochester Gas 6 Electric Corp.
MECREDY,R.C.
Rochester Gas 6 Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION RECIPIENT ID CODE/NAME PDl-3 LA JOHNSONFA COPIES LTTR ENCL 3
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SUBJECT:
Monthly operating rept for Sept 1990 for License DPR-18.W/
901012 ltr.
DISTRIBUTION CODE:
IE24D COPIES RECEIVED:LTR i
ENCL SIZE:
TITLE: Monthly Operating Report (per Tech Specs)
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
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J izzard ROCHESTER GAS AND ELECTRIC CORPORATION ROBERT C MECREDY Vice Prestdent Cinne Nudeer Production e
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4 89 EAST AVENUE, ROCHESTER N.K 14649.0001 TELEPHONE Atty,cooers e 546-2700 GINNA STATION October 12, 1990 US Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
Monthly Report for September, 1990 Operating Status Information R.
E. Ginna Nuclear Power Plant Docket No. 50-244
Dear Sir:
Pursuant to our Technical Specification 6.9.1, attached herewith is the monthly operating status report for Ginna Station for the month of September, 1990.
Ver truly yours, Robert C. Mecred RCM/eeh At:tachments cc:
Mr. Thomas T. Martin NRC (1)
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PDR ADOCK 900930 05000244 PNV g(
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OPERATING DATA REPORT DOCKET NO.
DATE COMPLETED BY 50-244 Octo r 12 1990 Robert E. Dodge OPERATING STATUS TELEPHONE 315 524.4446 ext. 396 2.
3.
4, 5.
6.
70 8.
Unit Name:
R.E.
GINNA NUCLEAR POWER PLANT Reporting Period:
Se terber 1990 Licensed Thermal Power (MWt):
Nameplate Rating (Gross MWe):
Design Electrical Rating (Net MWe):
Maximsn Dependable Capacity (Gross MWe):
Maximus Dependable Capacity (Het MWe):
If Changes Occur in Capacity Ratings (Items 1520 490 470 490 470 Notes:
The unit operated at approximately 100/ reactor power level for the majority of the report period, except for the event detailed on page 4 of this report.
Hunber 3 Through 7) Since Last Report, Give Reasons:
9.
Power Level to Which Restricted, If Any (Net MWe):
10.
Reasons For Restrictions, If Any:
This Month Yr.-to.Date Cmaiative 11
'2.
13 ~
14.
15.
16.
17.
18.
19.
20.
21.
22.
23.
Hours In Report Period Nunber of Hours Reactor Was Critical Reactor Reserve Shutdown Hours Hours Generator On-Line Unit Reserve Shutdown Hours Gross Thermal Energy Generated (MWH)
Gross Electrical Energy Generated (MWH)
Net Electrical Energy Generated (MWH)
Unit Service Factor Unit Availability Factor Unit Capacity Factor (Using MDC Net)
Unit Capacity Factor (Using DER Het)
Unit Forced Outage Rate 720 662.97 657.25 959 083 322 536 306 541 91.28 91.28 90.59 90.59 6 551 5 400.81 5 361.75 7 863 948 2 651 566 2 521 534 81.85 81.85 81.90 81.90 1.98 182 735 143 746.95 1 687.55 141 203.13 8.5 199 486 398 65 684 911 62 339 447 77.27 77.28 6.20 24.
Shutdowns Scheduled Over Next 6 Months (Type, Date and Duration of Each):
Annual Refuelin and Maintenance Shutdown:
March 1991 25'fShut Down At End Of Report Period, Estimated Date of Startup:
May 7, 1990 26.
Units In Test Status (Prior to Coemerciai Operation):
Forecast Achieved INITIALCRITICALITY INITIALELECTRICITY COMMERCIAL OPERATION
- CUMULATIVETOTAL COMMENCING JANUARY 1, 1975
ll
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0 0
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-244 UNIT R.E.
Ginna Nuclear Power Plant DATE Octobe 12 990 COMPLETED BY Robert E.
Dod TELEPHONE 1
315 524-4446 ext.
396 MONTH Se tember 1990 DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
DAY AVERAGE DAILY POWER LEVEL (MWe-Net) 466 17.
470 2 ~
465 18'70 3 ~
466 19.
469 4 ~
467 20.
469 5 ~
467 21.
468 6 ~
467 2 2 ~
468 7 ~
466 23'69 8.
467 24.
470 9.
474 25 ~
471 10'73 26.
210 474 27
'2
'75 28'12 13'72 29'73 14.
472 30.
469 15'70 31 ~
16.
470 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month.
Compute to the nearest whole megawatt.
DOCKI(1 NO.
SO 244 UNI1'NAhll'. R E. GINNA NUCLEAR POWER PLANT UNIT SHUTDOWN AND POWER REDUCTIONS COhlPLI'.1'l:D HY ge t
REPORT hfONTH 1.1: LI(PHONI: 315-524-4446 x-396 No.
Date 0
4t 0
CV 40 tO4 IX ot o-0 ocv40 tt.'IA4 0
Cl Licensee Event Report 0
Em 0
0 Vl 0 IA 40th 40 40 O
Cause & Corrective Action to Prevent Recurrence 186 9/26 cI/,29 F
62.75 H
LZR 90-012 INSTRU A reactor trip occurred from the in-advertent opening of the "A" reactor trip breaker caused by a technician accidentally dropping a flashlight on 2 of 3 turbine auto-stop trip relays.
1 F: Forced S:
Scheduled REV. 4/85 4949 Reason:
A-Equipment Failure (Explain)
B-Maintenance or Test C-Refueling D-Regulatory Restriction E-Operator Training gc License Examination F-Administrative G-Operational Error (Explain)
H-Other (Explain) 3 hlethod:
1-Manual 2-Manual Scram.
3-Automatic Scram.
4-Other (Explain) 4 Exhibit G - Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161)
Exhibit 1 - Same Source
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NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE DOCKET NO.
50-244 UNIT R.E.
Ginna Nuclear Power Plant DATE Octobe 12 990 COMPLETED BY bert E.
Dodg TELEPHONE 1
315 524-4446 ext.
396 MONTH Se tember 1990 The unit operated at approximately 974 reactor power level for the majority of the report period, except for the following event:
On September 26, 1990 at 1100
- EDT, a reactor trip occurred from the inadvertent opening of the "A" reactor trip breaker caused by a technician accidentally dropping a flashlight on 2 of 3
turbine autostop trip relays.