ML17261A767

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Insp Rept 50-244/87-27 on 871026-30.Violations Noted. Major Areas Inspected:Licensee Actions on NRC Concerns & Drawing Control Program
ML17261A767
Person / Time
Site: Ginna Constellation icon.png
Issue date: 12/24/1987
From: Blumberg N, Dudley N, Oliveira W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17261A765 List:
References
50-244-87-27, NUDOCS 8801200382
Download: ML17261A767 (16)


See also: IR 05000244/1987027

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION I

Report

No.

50-244/87-27

Oocket No.

50-244

License

No.

OPR-18

Licensee:

Rochester

Gas

and Electric Corporation

49 East Avenue

Rochester,

New York

Facility Name:

R.

E. Ginna Nuclear

Power Plant

Inspection at:

Ontario,

New York

Inspection

Dates:

October

26-30,

1987

Inspectors:

W. Oliveira, Reactor

Engineer

rz -P

-Z'ate

N. Oudley,

Sen or Operations

Engineer

//~3

g 7

date

Approved by:

N. Blumberg,

C ief, Operational

Programs

Section,

Operations

Branch,

ORS,

RI

date

Ins ection

Summar

Routine

unannounced

inspection

on October 26-30,

1987

(Report

No. 50-244/87-27)

Areas Ins ected:

Licensee's

actions

on previous

NRC concerns

and the drawing

control

program.

Results:

One violation (paragraph

3.5) was identified for licensee's

failure

to identify and correct the cause of errors

on Piping and Instrumentation

Drawings.

sso>20ossa

ssoios

PDR

ADOCK 05000244"-

8

PDR

DETAILS

1.0

Persons

Contacted

"C. Anderson,

Quality Assurance

Manager

"J. Bodine,

Manager,

Nuclear Assurance

"D. Bryant, Quality Assurance

Engineer - Operations

"B. Carroll, Training Coordinator,

Licensing

"R. Davis, Quality Assurance

Engineer

"W. Faustuferri,

Technical Staff Engineer

  • A. Jones,

Staff Assistant to Superintendent

  • G. Link, Manager, Electrical Engineering

Design

"R. Mecredy, Director, Engineering Services

"J. St. Martin, Station Engineer

  • K. Nassauer,

Quality Control Supervisor

"J. Neis, Technical

Section

Engineer

  • T~ Schuler,

Operations

Manager

"R. Smith, Chief Engineer

"S. Spector,

Superintendent,

Ginna Production

E. Voci, Mechanical

Engineer

  • J. Widay, Technical

Manager

United States

Nuclear

Re viator

Commission

"T. Polich, Senior Resident

Inspector

"N. Perry,

Resident

Inspector

  • Denotes

those attending

the exit meeting.

The inspector also contacted

other administrative

and technical

personnel

during the inspection.

2.0

Licensee's

Actions on Previous

NRC Concerns

2. 1

(Closed)

Inspector Follow Item (244/83-19-02):

Drawing Control

Due to the untimely issuance

of drawing revisions,

a large backlog

of Engineering

Work Requests

(EWR) existed which resulted

in a

cumbersome

system for print usage,

since operators

were required to

review all outstanding

EWRs applicable to a print prior to using the

print.

The inspector

reviewed the number of outstanding

EWRs and the

recommendations

made

by the licensee's

Drawing Update

Task Force.

As

a result of the recommendations,

requirements

were established

for

the timely incorporation of drawing changes.

There

has

been

a reduc-

tion in the number of outstanding

EWRs.

This item is closed.

2.2

(Closed)

Inspector

Follow Item (244/85-06-04):

Drawing Control

The Station

Document Control

Room did not track outstanding

EWR

modifications

on "non-controlled" drawings.

As

a result, station

personnel

might not have

had drawings which accurately reflected

as-built conditions for up to 30 days after

a modification was

completed, if the drawing was not a controlled document.

2.3

The inspector

reviewed the recommendations

made by the licensee's

Drawing Update Task Force.

As a result of the recommendations

additional drawings,

which were previously "non-controlled," were

included in the controlled drawing system.

The inclusion of the

drawings into the control

system appears

to provide

a means of

ensuring timely incorporation of EWRs and the availability, of

as-built drawings.

This item is closed.

(Open) Inspector Follow Item (244/83-23-02):

Modification Process

Weaknesses

existed in the station modification process

which

included unsigned

procedural

steps,

incomplete review signatures,

and untimely supervisory

reviews.

The functional test of the

pH

meter

had been accepted

even

though the accuracy specified in the

Design Criteria had not been satisfied

when

a

pH of 10 was used

as

the standard.

2.4

The inspector

reviewed

a sample of the Station Modification (SM)

procedures

that were not previously reviewed.

The facility's reviews

were completed

and the procedures

have

been

submitted to Central

Records.

The inspector

sampled

and reviewed

1987

SMs relative to

improving the timely sign off, turnover

and supervisory

review.

The

sign off, turnover and supervisory

reviews averaged

one month as

opposed

to one year for 1983

SMs.

The licensee,

however,

has not

resolved the specific issue of the acceptability

of the results of

the

pH meter functional test.

This item remains

open.

(Closed)

Inspector

Follow Item (244/83-26-01):

Training Program

Timely rev'iew of on-shift work assignments

had not been conducted

and

a program did not exist for evaluation of instructors.

The inspector

reviewed Operator Training Guideline

No.

OTG-4,

Individualized Instruction, which was issued

on October 20,

1987.

The procedure

requires that

a cover sheet

be completed for each

student

when

a training assignment

is issued.

The cover sheet

shows

the date the assignment

is due

and the date the assignment

is reviewed

in the classroom.

The inspector

conducted

a review of selected

individuals'raining records to evaluate

proper completion of the

assignment

cover sheets.

In most cases,

the facility review signa-

tures

were

made

soon after the completion 'of the classroom

reviews.

The inspector

reviewed Training Administrative Procedure

T.R.5.3,

Rev. 3, Instructor Observation,

issued

February

19,

1987.

The

procedure

provides

a program for student

feedback

and evaluation

of instructors.

All instructors

are required to be evaluated

by

their supervisors

annually

and have

been evaluated at least

once in

1987.

Steps

are being taken

by the training supervisors

to establish

a long range

schedule for instructor evaluations.

Student

feedback

forms are collected,

and reviewed

by the corporate training depart-

ment and

a report is i ssued

which may recommend further evaluation of

an instructor.

A formal program for evaluation of instructors is in.

place

and effectively monitors the quality of the training being

provided.

This item is closed.

2.5

(Open) Inspector Follow Item (244/84-06-01):

Effectiveness of the

Quality Control

(QC) Organization

The licensee

had committed to improve the Plant

QC Department's

effectiveness

in the followup of plant activities.

The licensee

does not expect to have its improvement

program fully

implemented until mid 1988.

The inspector

reviewed the following

actions which have

been

taken or are planned:

QC staff was reduced

from twelve to six personnel

in June

1987.

The reduction of the

QC staff is also discussed

in

NRC

Inspection

Report 50-244/87-26

Project (modification)

QC and plant

QC have

been

merged together

and

now report to the

QC supervisor

Operations

QC position

has

been

approved

and will be

established

QC inspectors

are receiving Auxiliary Operator training to

understand

the plant systems,

the training will be completed

by

the

end of December

1987

QC is developing

a

QC inspector training program using

INPO

guidelines

QC is having interface meetings with plant sections,

e.g.,

Maintenance,

Operations

and Health Physics,

to prepare for the

Outage

scheduled

in February

1988.

This item remains

open pending full implementation of the program,

and

a review by NRC as to its effectiveness.

2.6

(Closed)

Inspector

Follow Item (244/86-16-02):

Drawing Control

Inconsistencies

existed in the labeling of locked valves

on Piping

and Instrumentation

Drawings (P&IOs), and were identified to the

licensee

in Inspection

Report 50-244/86-16

issued

on November 3,'986.

These identified inconsistencies

on the

P&IDs had not been corrected

by April 1987.

The failure to correct the inconsistencies

and ad-

ditional discrepancies

were identified to the licensee

in Inspection

Report 50-244/87-08

issued

on Nay 26,

1987.

The inspector

reviewed the accuracy of the

P&IDs as detailed in

Paragraph

3.0.

Numerous

new discrepancies

on the

P&IDs were

identified and as

a result

a violation was issued.

Since the

concerns

of inconsistencies

on the P&IDs will be followed as part

of the violation, this item is closed for administrative

purposes.

3.0

Controlled ~Drawin

a

3.1

References/Re

uirements

The following references

and requirements

were

used

by the inspector

to evaluate

the adequacy of the controlled drawing program in general

and the accuracy of the

P&IDs in particular.

10 CFR 50 Appendix B, Criteria III, Design Control

10 CFR 50 Appendix B, Criteria VI, Document Control

10 CFR 50 Appendix B, Criteria XVI, Corrective Action

Safety Guide 33,

1972, Quality Assurance

Program

Requirements

Regulatory

Guide 1.64, Quality Assurance

Requirements

for the

Design of Nuclear

Power Plants

ANSI N45.2-1971,

Section

17, Quality Assurance

Program Requirements

for Nuclear

Power Plants,

Corrective Action

ANSI N45.2. 11-1974,

Paragraph

9, Quality Assurance

Requirements

for

the Design of Nuclear Power Plants,

Corrective

Action

Technical Specifications, Section 6.8,

Procedures

3.2

Documents

Reviewed

The following procedures

were reviewed

by the inspector.

QE-303, Preparation,

Review and Approval of Engineering

Drawings issued

07/01/86.

gE-323, Preparation,

Review,

and Approval of Computer 'Assisted

Drawing Program

(CAOP) Piping and Instrument

Drawings,

issued

11/18/85.

gE-324, Preparation,

Review and Approval of Drawing Change

Requests,

issued

11/18/86.

gE-316, Preparation,

Review and Approval of Field Change

Requests,

issued 01/23/87.

A-603,

Control of As-Built Drawings and Design Documents,

issued Ol/29/87.

A-606,

Drawing Change

Requests,

issued 02/21/87.

3.3

Details of the Review

In order to assess

corrective actions for problems which had been

identified in previous inspection reports,

the inspector

conducted

a

review of selected

PKIDs to ensure as-built conditions were documented

and that locked valve positions

were properly annotated.

The review

was limited to the

PKIDs and not other drawings since

an upgrade

program

had been

completed for the

PKIDs in January

1987.

3.4

~Fkndfn

s

The licensee's

Drawing Upgrade Task Force,

which had been established

by the licensee

to study the problems concerning control drawings,

presented

recommendations

to the Chief Engineer

in an inter-office

correspondence

dated October 31,

1986.

As a result of the recom-

mendations priority was assigned

by the licensee

to upgrade

the

P@IDs by establishing

target dates for completing three

phases

of a

P8 ID upgrade

program.

The last phase of the

P&ID upgrade

program was

completed

by January

7,

1987.

Revised

procedures

for controlling

changes

to the P&IDs were completed

and issued

by January

23,

1987.

The inspector

conducted

a partial walkdown of two systems

to verify

that selected

PAID drawings represented

as-built conditions.

The

walkdown inspection guidelines,

provided in the Task Management

Manual

Fluid System Diagram Upgrade

document

were used

as guidance.

The

following discrepancies

were noted:

PAID 33013-1248, Auxiliary Cooling Spent

Fuel

Pool Cooling, did

not include the flange for the discharge

connection to the

temporary

gas stripper feed

pump even though the flange for the

suction connection to the

pump was included

on the drawing.

PAID 33013-1262,

Safety Injection and Accumulators (SI), did not

show the heat tracing

on the

RWST supply line.

Ill

P&ID 33013-1262,

Safety Injection and Accumulators (SI), did not

include the test connection

on the SI

pump suction line from the

Boric Acid Storage

Tanks.

The inspector

compared

the drawings for six systems

against

procedure

number A-52.2, Control of Locked Valve and Breaker Operation.

Both

the drawings

and the procedure

are controlled documents.

The follow-

ing discrepancies

were identified.

The throttle position for V-769 was not the

same

on the drawing

and in the procedure.

The representation

for throttled valves

V-769 and

V-7640&C was

inconsi stent

on two different drawings.

Valve V-804 is shown

as throttled in the procedure

and the

drawing does not contain

a note

on throttle position

as it

does for other throttled valves

on the drawing.

Valve V-547 is listed as closed in the procedure

and

open

on the

drawing.

Valve V-1826 is included in the procedure

as locked and is not

indicated

as locked

on the drawing.

The inspector

noted additional

cases

of a lack of drawing control

during the review of the P&IDs.

In one case,

the inspector

was

unable to determine

which Drawing Change

Requests

(DCRs) were still

outstanding.

The Main Control

Room

DCR log and the Operations

Department

DCR log indicated over

a dozen outstanding

DCRs associated

with the

P&IDs.

The inspector

was able to determine that three of

these outstanding

OCRs

had been incorporated

onto the P&IDs.

The

Central

Record

DCR log indicated four outstanding

OCRs associated

with the P&IDs. It was impossible to determine

from the Engineering

Department

DCR log which DCRs were associated

with the P&IDs, however

the Engineering

Department

stated that there

was only one outstanding

DCR associated

with the P&IDs.

In a second

case,

an error was identified by Central

Records

in the

incorporation of a

DCR onto

a print.

The error was addressed

in a

letter from the Engineering

Department to Central

Records

on August

12,

1987,

and involved adding the letter "A" to a valve number.

However,

no change

has

been generated

for over 60 days.

In contrast,

the facility was able to incorporate errors identified by the

inspector in two days.

Central

Records is following the guidance

provided in A-606 and the Engineering

Department is following the

guidance in gE-324.

As

a result,

no change

has

been

made to correct

the error.

J

In a third case,

a drawing was found that contained

a sticker

which

required the user to reference

an

EMR prior to use.

The

EWR which

was referenced

had

been closed out.

There does

not appear to be

a

control

system to assure all drawings initially affected

by an

EMR

are either replaced or reviewed

once

an

EWR is closed out.

The Chief Engineer stated that

no guality Assurance

audit has

been

conducted

by the facility to evaluate

the effectiveness

of the

P&ID

upgrade

program.

3.5

Conclusion

The licensee

has

completed

a major upgrade

program for the

P&IOs and

judged the

P&IDs ready for review.

A small

sample of P&IDs were

reviewed for accuracy.

The inspector identified numerous errors

and

inconsistencies

in all areas

that were reviewed.

Similar errors

had

been identified by the

NRC in Inspection

Reports

50-244/87-08,

50-244/86-18,

and 50-255/86-16.

The licensee

has failed to effectively implement

a program to ensure

P&ID drawings reflect as-built conditions,

to ensure

P&IOs drawings

are in agreement with controlled procedures

and to ensure

drawing

changes

are adequately

controlled.

The type and

number of errors

found on the

P&IDs represent

recurring deficiencies for which inade-

quate corrective action

has

been taken to determine

the cause

or to

correct

the problem.

The above findings are contrary to the correc-

tive actions requi red by 10 CFR 50 Appendix B, guality Assurance

Criteria for Nuclear

Power Plants, Criteria XVI; ANSI N45.2. 11-

1974Property "ANSI code" (as page type) with input value "ANSI N45.2. 11-</br></br>1974" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., guality Assurance

Requirements

for the Design of Nuclear

Power

Plants,

Section

9;

and Ginna guality Assurance

Manual Section

16.

This is

a violation (50-244/87-27-01).

4.0

Mana ement Meetin

s

Licensee

management

was informed of the scope

and purpose of the inspec-

tion at the entrance

interview on October 26,

1987.

The findings of the

inspection

were discussed

with licensee

representatives

during the course

of the inspection

and presented

to licensee

management

at the exit inter-

view (see

Paragraph

1 for attendees).

At no time during the inspection

was written material

provided to the

licensee

by the inspector.

The licensee did not indicate that proprietary

information was involved within the scope of this inspection.

CS