LER-1975-039, A-00 for Dresden Unit 2, Supplemental Report on Unit 2 Diesel Generator Starting Failures |
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| 2371975039R00 - NRC Website |
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Commonwealth.9son Dresden Nuclear Power Station R.R. #1 Morris, Illinois 60450 Telephone 815/942-2920 BBS Ltr. # 310-76 April Mr. James G. Keppler, Regional Director Directorate of Regulatory Operations - Region III U. S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137
SUBJECT:
SUPPLEMENTAL REPORT ON UNIT-2 DIESEL GENERATOR
References:
- 1)
Letters from B. B. Stephenson to J. G. Keppler, Report Nos. 50-237/1975-16, 26, 37, and 39
- 2)
Drawing Number:
M-173 Report Number:
50-237/1975-39A Report Date:
April 13, 1976 Occurrence Date:
June 12, 1975 Facility:
Dresden Nucle~r Power Station, Morris, Illinois
INTRODUCTION
The Unit-2 diesel generator experienced a number of starting failures in 1975.
Related starting failures occurred on March 17, April 15, June 4, and June 12, 1975.
On March 1.7, the diesel generator failed to start on the first attempt and was taken out.of service.
During subsequent testing, the diesel genei;-ator again failed to start. It was discovered that the pinion geara of the air start motors were not properly engaging the main ring gear.
The air start motors were replaced and sent to the man~!acturer (Ingersoll-Rand).
. for detailed examination.
Ingersoll-Rand personnel were. unable to find any defect in either air start motor.
On April 15, as the diesel: generator was being returned to service following repair~,.the pinion gears and ring gear jammed again.
Although an Ingersoll-Rand representative could not pinpoint the cause of the failures; he suggested that the pilot air pressure used to engage the piniofis was too high, causing the teeth to jam rather than engage.
A modification which would lower the pilot air pressure was briefly under consideration; however, this was eventually discarded as an improbable solution.
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The* diesel generator failed to start again on June 4, following a monthly inspection.
The diesel was then started a number of times in an attempt to isolate the cause of failure.
The diesel generator had started 12 times without incident when*, on June 12, it failed to start twice in four
.attempts.
The same day, with a factory representative present, the diesel started six consecutive times.
A surveillance program was initiated that placed an operator at the diesel each time it was started.
CORRECTIVE ACTION
As a result of the many air start failures experienced on the diesel generator, vendor representatives were summoned to the plant on November 14,.1975, to. exhaustively investigate the air starting system.
The ring gear was examined in detail and found to have two small, slightly gouged and burred areas.
A series of 22 tests was performed, consisting of rotating the ring gear manually and engaging the pinion gears from the
- control switch with the main air valved out, simulating an actual start.
At the two gouged and burred areas, the pinion gears failed to engage three out of six times, while at all other points on.the ring gear. the tests were satisfactory.
The ring gear was dressed up in these 'areas with a stone and file according to the vendor's recomm~.ndations.
No diesel generator starting failures have o*ccurred since the burrs were removed from the ring gea*r; accordingly, the air starting system difficult*ies are.considered to be resolved.
~
Station Superintendent
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- on 750428,during Routine Insp,Two Hydraulic Piping Restraints Inoperable.Cause Unknown.Inoperable Snubbers Will Be Replaced Before End of Outage
| | | 05000249/LER-1975-026, AO 50-249/75-26:on 780509,during Discharge test,24/48 Volt Dc Batteries Failed to Deliver Rated ampere-hour Capacity. Caused by Six Bad Cells in One Battery & Four Bad Cells in Other.Deteriorated Cells Will Be Replaced | AO 50-249/75-26:on 780509,during Discharge test,24/48 Volt Dc Batteries Failed to Deliver Rated ampere-hour Capacity. Caused by Six Bad Cells in One Battery & Four Bad Cells in Other.Deteriorated Cells Will Be Replaced | | | 05000249/LER-1975-027, :on 750515,cracks Observed on Five of Eight Header Pipe & One of Four Thermal Sleeve to Junction Box Welds.Caused by Design of Spargers Susceptible to Flow Induced Vibration.Spargers Will Be Replaced |
- on 750515,cracks Observed on Five of Eight Header Pipe & One of Four Thermal Sleeve to Junction Box Welds.Caused by Design of Spargers Susceptible to Flow Induced Vibration.Spargers Will Be Replaced
| | | 05000249/LER-1975-028, AO 50-249/75-28:on 750522,main Steam Line Area Temp Sensors 261-16B,261-17 A-D & 261-18D Found W/Setpoints Above Tech Spec Limit.Caused by Misapplied Switches.Switches Reset within Tech Spec Limit | AO 50-249/75-28:on 750522,main Steam Line Area Temp Sensors 261-16B,261-17 A-D & 261-18D Found W/Setpoints Above Tech Spec Limit.Caused by Misapplied Switches.Switches Reset within Tech Spec Limit | | | 05000249/LER-1975-035, Regarding Failure of Circuit Breaker 152-3403 to Open During a Breaker Trip Event | Regarding Failure of Circuit Breaker 152-3403 to Open During a Breaker Trip Event | | | 05000237/LER-1975-038, A-00 for Dresden Unit 2 Supplemental Report to Letter Dated June 25, 1975, Entitled Failure of Valve MO-2-1301-2 to Operate | A-00 for Dresden Unit 2 Supplemental Report to Letter Dated June 25, 1975, Entitled Failure of Valve MO-2-1301-2 to Operate | | | 05000237/LER-1975-039, A-00 for Dresden Unit 2, Supplemental Report on Unit 2 Diesel Generator Starting Failures | A-00 for Dresden Unit 2, Supplemental Report on Unit 2 Diesel Generator Starting Failures | | | 05000249/LER-1975-042, Regarding Failure of LPCI Valve 3-1501-5D Motor Trip | Regarding Failure of LPCI Valve 3-1501-5D Motor Trip | | | 05000237/LER-1975-044, A-00 for Dresden Unit 2 Supplemental Report to Letter Dated October 2, 1975, Entitled Unit-2 Diesel Generator Failure to Start | A-00 for Dresden Unit 2 Supplemental Report to Letter Dated October 2, 1975, Entitled Unit-2 Diesel Generator Failure to Start | | | 05000249/LER-1975-044, Letter Submitting Correction to Abnormal Occurrence Report Entitled, Off-Gas Increase on Unit 3 (Report 50-249/75/44) | Letter Submitting Correction to Abnormal Occurrence Report Entitled, Off-Gas Increase on Unit 3 (Report 50-249/75/44) | | | 05000249/LER-1975-045, :on 751203,during Weekly Surveillance,Irm 12 Tripped Above Tech Spec Limit.Probably Caused by Instrument Setpoint Drift |
- on 751203,during Weekly Surveillance,Irm 12 Tripped Above Tech Spec Limit.Probably Caused by Instrument Setpoint Drift
| | | 05000237/LER-1975-046, Regarding Inoperability of Snubber 25 | Regarding Inoperability of Snubber 25 | | | 05000249/LER-1975-046, :on 751207,during Reactor Shutdown for Maint, Snubber 25 Found Inoperable Due to Insufficient Amount of Hydraulic Fluid.Caused by Deteriorated Seals.Snubber Zirc Fitting Replaced |
- on 751207,during Reactor Shutdown for Maint, Snubber 25 Found Inoperable Due to Insufficient Amount of Hydraulic Fluid.Caused by Deteriorated Seals.Snubber Zirc Fitting Replaced
| | | 05000249/LER-1975-047, :on 751211,during Surveillance Testing,Unit 3 Diesel Generator Would Not Accept Load Above 100 Kw.Caused by Loose Locknut on Shutdown Solenoid.Locknut Tightened. Diesel 6 Month Insp Procedure Revised |
- on 751211,during Surveillance Testing,Unit 3 Diesel Generator Would Not Accept Load Above 100 Kw.Caused by Loose Locknut on Shutdown Solenoid.Locknut Tightened. Diesel 6 Month Insp Procedure Revised
| | | 05000249/LER-1975-048, :on 751222,during Instrument Surveillance,Hpci Flow Switch DPIS 3-2353 Tripped Above Tech Spec Limit.Caused by Misapplication of Switch.Program to Modify Instruments in Progress |
- on 751222,during Instrument Surveillance,Hpci Flow Switch DPIS 3-2353 Tripped Above Tech Spec Limit.Caused by Misapplication of Switch.Program to Modify Instruments in Progress
| | | 05000237/LER-1975-048-01, Letter Enclosing LER 75-048-01 Regarding Current Status of a Long-Term Corrective Action to Prevent Reoccurrence of a Through-Wall Crack in the Drywell-Torus Nitrogen Purge Line 1604-18 | Letter Enclosing LER 75-048-01 Regarding Current Status of a Long-Term Corrective Action to Prevent Reoccurrence of a Through-Wall Crack in the Drywell-Torus Nitrogen Purge Line 1604-18 | | | 05000237/LER-1975-049, Regarding Failure of Channel a Floor Radiation Monitor Downscale | Regarding Failure of Channel a Floor Radiation Monitor Downscale | | | 05000249/LER-1975-049, :on 751223,during steady-state Operation,Channel a Refueling Floor Radiation Monitor Failed Downscale.Caused by Cable Connector Failure.Connector Replaced |
- on 751223,during steady-state Operation,Channel a Refueling Floor Radiation Monitor Failed Downscale.Caused by Cable Connector Failure.Connector Replaced
| | | 05000237/LER-1975-051, For Dresden Unit 2 Regarding Report of Unit-2 High Torus Water Level Exceeding the Technical Specifications Limit | For Dresden Unit 2 Regarding Report of Unit-2 High Torus Water Level Exceeding the Technical Specifications Limit | | | 05000237/LER-1975-052, For Dresden Unit 2 Regarding a Report of Rapid Closure of Unit-2 Main Steam Isolation Valve 203-1C | For Dresden Unit 2 Regarding a Report of Rapid Closure of Unit-2 Main Steam Isolation Valve 203-1C | |
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