ML17252A863
ML17252A863 | |
Person / Time | |
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Site: | Indian Point |
Issue date: | 05/21/1973 |
From: | Caldwell W Con Edison, Consolidated Edison Co of New York |
To: | O'Reilly J US Atomic Energy Commission (AEC) |
References | |
Download: ML17252A863 (1) | |
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Category:Letter
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Limit - Indian Point Unit 2 ML17252A8791973-12-0303 December 1973 Letter Regarding a 11/18/1973 Occurrence Relating to the Discovery of the Erroneous Setting for 1 of the Bistables Associated with Low Pressurizer Safety Injection Required by the Technical Specifications - Indian Point Unit No. 2 ML17252A8781973-11-30030 November 1973 Letter Providing Supplemental Information Concerning the 11/13/1973 Incident at Indian Point Unit No. 2 ML17252A8821973-11-19019 November 1973 Letter Concerning a 11/16/1973 Occurrence Regarding Periodic Tests and Calibration Checks Indicating the Setting for 1 of the Bistable Device Was Below the Technical Specification Requirements - Indian Point Unit 2 2018-05-21 |
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PMS JAMES P OREILLY DIRECTOR R£:JULATORY OPERATIONS REGION I US ATOMIC ElllERGY COMM 970 BORAD ST NE WARK NJ 0710 2
~;*, ,, DEAR fllR ORE IllY-I"! ACCORDANCE WI TH THE REQUIREMENTS OF TECHNl:CAL SPEC!tICATION i ; ',
6 .6.18 FOR FACILITY OPERATING LICENSE NO
~,. " DPR--26* WE WISH TO I"'lFORM YOU OF AN ABNORMAL OCCURRENCE WHICH WAS
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IDENTIFIED ON MAY 18, 1973 AT 0552 HOURS-IN THE" COURSE or HEATING UP THE REACTOR COOLANT SYSTEM *~._ .
PREPARATORY' TO THE CONDUCT. or A HYDROSTATIC t
TEST,. A PRESSURE TRANSIENT: TO ABOUT 575 PSIG
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WAS: EXPERIENCED OU TO CLOSURE OF CERTAir~ AIR OPERATED VALVES ASSOCIATED WITH THE CHARGING ANO LETDOWN SYSTEM UPON LOSS or:- .
CONTROL AIR*
OUR. PREl:.IMlNARY INVESTIGATION INDICATES THT THE LOSS or* CON TROL. AIR. WAS THE RESULT OF A FREEZE UP OF THE A:IR. SUPPLY -
LINF Ar T.HE REFRIGERANT OYRER. AT THE TIME OF THE TRANSIENT, THE REACTOR COOLANT SYSTEM WAS A APPROXIMATELY 440 PSIG *
. MIO: 1~0 DEGREES F WITH FOUR REACTOR COOLANT PUMPS IN SERVICE:.. ANO.**.*
ALL CONTROL ROOS rnLLY INSERTED.
- THERE. WAS NO DAMAGE TO Am SYSTEM: OR COMl?Ol\ENT NOR WAS . _; .. . .L . I r .. .
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.. .. ..--:., .. ~--- 1 THERE: ANY. REASON TO EXPECT ANY AS A RESULT Of THE'. PRESSURE ... * :* :-, -* .* /.:. :!
. TRANSIENT.MR. A. FASANO OF' YOUR. OffICE WAS INFORMED OF' THE OCCURRENCE~:* :
B.Y MR_ JOHN MAKEPEACE av* l'E:LEPHONE' ONMAY18 1973.
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[N ACCORDANCE WITH THE REQUIREMENTS OF TECHNlCAL SPEClrICATlON o*2: NO'.fIF.TCATlON OF THE VICE. CHAIRMAN OF THE NUCLEAR F'ACIUTIES SAFETY. COMMITTEE HAS BEEN MADE.*....
WF ARE CURRElllrl'LY Ir.JVES'TIGATING THE CAUSE Of THE: .'/* * <. '* * . . . -:-', ~- .. .**-:-**
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-o:ccuRRENCE AND VI LL ADVISE YOU or* QlJR_ F'lNDlNGS .
- AND. CORRECTIVE ACTION TAKEN IN. A WRITTTEN. REPORT *r -...,.,_
- . IC' WlilCH . VlLLBE SU Bf'II.TTEO VlTHlN THE:* REUIRED TEN. ( 10.) -DAYS YOURS' TRULY .
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