ML17244A765

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Monthly Operating Rept for Jul 1979
ML17244A765
Person / Time
Site: Ginna Constellation icon.png
Issue date: 08/09/1979
From: Mcnamara A
ROCHESTER GAS & ELECTRIC CORP.
To:
Shared Package
ML17244A764 List:
References
NUDOCS 7908210370
Download: ML17244A765 (10)


Text

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~ OPERATING STATUS OPERATING DATA REPORT DOCKET NO.

50 244 DATE Au us 197 COMPLETED BY Andrew E. McNamara TELFPHONE 1-716-546-2700

. Ext. 291-205, at Ginna

1. Unit Name:

GINNA STATION N

2. Reporting Period:

Jul 1979

3. Licensed Thermal Power (MWt):
4. Namcplatc Rating (Gross MWe):
5. Design Electrical Rating (Net MWe):
6. Maximum Dependable Capacity (Gross MWe):

490

7. Maximum Dependable Capacity (Net MWe):

otcs The Unit operated at 100% Reactor Power Level until Shutdown on 7/6; to comply with Inspection Requirements of NRC I6E Bulletin 79-13.

8. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Rcport, Give Reasons:
9. Power Level to Which Restricted, If Any (Net MWe)t
10. Reasons For Restrictions, If Any:

This Month Yr.-to-Date Cumulative

11. Hours In Reporting Period
12. Number of Hours Reactor Was Critical
13. Reactor Reserve Shutdown Hours
14. Hours Generator On-Line
15. Unit Reserve Shutdown Hours
16. Gross Thermal Energy Generated (MWH)
17. Gross Electrical Energy Generated (MWH)
18. Nct Electrical Energy Gcncrated (MWH)
19. Unit Service Factor
20. Unit AvailabilityFactor
21. Unit Capacity Factor (Using MDC Net)
22. Unit Capacity Factor (Using,DhR Net)
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Over Next 6 Months (Type, 744 142.75 5 087 3 288.

2 142.75 3 224**

19.19%

19. 45%

19.45%

0/

63.38%

62.53%

62.53%

Date and Duration of Each):

212 952 4 672 752 71 474 1 572 045 68 047 1 495 124 19.19%

63.38%

8489 6441 4

62 802.63 8.5 83 602 666 27 145 285 25 696 162 74.03%

74.04%

66.97%

66.97%

25. IfShut Down At End Of Report. Period, Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation):

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INITIALCRITICALITY INITIALELECTRICITY COMMERCIALOPERATION Forecast Achieved V 908210 +~~

  • Cumulative Data Commencing January 1,

1975 49 ed lRcve 1/78)

Corrects error in May and June Operating Summaries which were reported one hour short.

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e AVERAGE DAILYUNIT POWER UNIT DOCKET NO.

50.244 UNIT, Nl @irma Statio DATF Au ust 9.

1979 COMPLETED BY Andrew E. McNamara TELFPHON E 1-716-546-2700 xt.,at nna MONTH DAY AVERAGE DAILYPOWER LEVEL (MWe-N et) 485 485 482 483 484 437 10 12 13 15 16 DAY,AVERAGE DAILYPOWER LEVEL (MWe-Net) lj 18 20 21 22 23 24 25 26 27 28 29 30 31 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month.

Compute to the nearest whole megawatt.

49 ~ 87

'tREV, 1/78)

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DOCKET NO.

I UNII'AME ill Ginna Station UNIT SHUTDOWN AND POWER REDUCTIONS DATE~

(:OMPLETED BY ~ntlrew c amara TELEPHONE 1-716-546-2700 Ext. 291-205, at Ginna Date 40 L

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0 0 ~

40 40 e+0 c 440

> IY Dc@ 4 0

CL Licensee Event Report 0

Em-0 Vl 40 lA 4o u7 C04 40 lJ Cause L Corrective Action to Prevent Recurrence 790706 S

601.25 H

LER 879-13 ZZ To comply with Inspection Require-ments of NRC I&E Bulletin 79-,.13 (F.V. Steam Generator Nozzle Veld Inspection)..':

Forced S:

Scheduled 49 89 (Ruvo t/78)

Reason:

A-Equipmcnt Failure (Explain) 8-hlaintcnance or Test C-Refueling D-Regulatory Restriction E-Operator Training 8r License Examination F-Administrative G-Operational Error (Explain)

H-Other (Explain) hlethod:

I-hfanual 2-hla nual Scram.

3-Automatic Scram.

4-Other (Explain)

Exhibit G - Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG-0161)

Exhibit 1 - Same Source Unit remained shutdown at end of Report Month.

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-4 NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE DOCKET NO.

Ginna Station, Unit //1 Au ust 9

1979 COMPLETED BY Andrew E. McNamara MONTH TELEPHONE 1-716-546-2700 Ext. 291-205, at Ginna TheeUnit operated at 100% Reactor Power Level until it was shutdown on 7/6 to comply with Inspection Requirements of NRC l&E Bulletin 79-13 (F.W. Steam Generator Nozzle Weld Inspection).

The Unit remained shutdown at the end of the Report Period.

49 123 u/78)

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GINNA STATION MAINTENANCE REPORT FOR JULY 1979 During July, normal inspection and minor maintenance was performed.

Major safety related maintenance included:

1.

Replacement of the feedwater elbows adjacent to the steam generator nozzles per IE Bulletin 79-013.

2.

Installation of new internals on the pressurizer power operated relief

valves, to meet the necessary CV flow as reported per LER-79-011.

3.

Inspection and overhaul of the 1A Station Service Water Pump.

4.

Replaced diodes and capacitors for two rods on the rod position indicating system.

5.

Replaced a faulty bistable on one of the pressure signals for the RCS overpressure protection system.

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