ML17221A515

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Insp Repts 50-335/87-21 & 50-389/87-20 on 870906-1031. Violations Noted.Major Areas Inspected:Tech Spec Compliance, Operator Performance,Overall Plant Operations,Qa Practices, Site Security Procedures & Radiation Control Activities
ML17221A515
Person / Time
Site: Saint Lucie  
Issue date: 11/17/1987
From: Bibb H, Crlenjak R, Wilson B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17221A513 List:
References
50-335-87-21, 50-389-87-20, NUDOCS 8711230162
Download: ML17221A515 (17)


See also: IR 05000335/1987021

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-335/87-21

and 50-389/87-20

Licensee:

Florida Power and Light Company

9250 West Flagler Street

Miami,

FL

33102

Docket Nos.:

50-335

and 50-389

Facility Name:

St.

Lucie 1 and

2

License Nos.:

DPR-67 and

NPF-16

Inspection

Conducted:

September

6 - October 31,

1987

Inspectors:

r en

a

,

en>or

es

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nspector

esi

ent

nspecto

Approved by:

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Division of Reactor Projects

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SUMMARY

Scope:

This inspection

involved

on site activities in the area of Technical

Specification

compliance,

operator

performance,

overall

plant operations,

quality

assurance

practices,

station

and

corporate

management

practices,

corrective

and

preventive

maintenance

activities, site security procedures,

radiation control activities, surveillance activities, refueling outage

review,

and plant events

review.

Results:

Of the

area

inspected,

two violations,

one with two examples,

were

identified (paragraphs

3 and 12).

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REPORT DETAILS

Persons

Contacted

Licensee

Employees

K. Harris, St.

Lucie Vice President

G. J.

Boissy, Plant Manager

"R. Sipos,

Services

Manager

~"J ~

H. Barrow, Operations

Superintendent

T.

A. Diliard, Maintenance

Superintendent

J.

B. Harper,

gA Superintendent

"L.

W. Pearce,

Operations

Supervisor

"R. J. Frechette,

Chemistry Supervisor

"C.

F. Leppla,

I8C Supervisor

C.

A. Pell, Technical Staff Supervisor

E. J. Wunderlich, Reactor Engineering

Super v'isor

H.

F.

Buchanan,

Health Physics

Supervisor

W. White, Security Supervisor

~CD

L. Burton, Reliability and Support Supervisor

J.

Barrow, Fire Prevention Coordinator

R.

E.

Dawson, Assistant Plant Superintendent

-, Electrical

C. Wilson, Assistant Plant Superintendent

- Mechanical

"N.

G.

Roos, guality Control Supervisor

Other

licensee

employees

contacted

included

technicians,

operators,

mechanics,

security force members,

and office personnel.

"Attended exit interview.

Exit Interview

The

inspection

scope

and findings were

summarized

on

November 3,

1987,

with those

persons

indicated in paragraph

1 above.

The licensee

did not identify as proprietary any of the materials

provided

to or reviewed by the inspectors

during this inspection.

Licensee Action on Previous

Enforcement Matters

Withdrawn (Unit 1)

VIO 50-335/85-36-01:

Failure to Have

Two Shutdown

Cooling

Loops Operable

While In Mode With Reactor Coolant

Loops Drained.

A Notice of Violation was

issued

on February

10,

1985, for violating

Unit 1 technical specification (TS) 3.4. 1.4.2,

which requires

that

two

independent

trains of shutdown cooling

be operable

when in mode

5 with

reactor coolant loops not filled.

Specifically, the violation was written

because

the licensee

had taken

one train of component cooling water

(CCW),

which supports

shutdown cooling,

out of service for maintenance.

By a

letter dated July 22,

1986,

the

licensee

stated

that its maintenance

of

the

CCW system

in mode

5 with reactor

coolant

loops not filled did not

violate

Unit 1

TS 3.4. 1.4.2.

By

memorandum

dated .November 7,

1986,

Region II asked

the Office of Nuclear Reactor Regulation

(NRR) to review

the licensee's

arguments

and confirm or provide

a regulatory position.

The inspection

report (50-335/85-36)

documented

that one of two required

shutdown cooling loops

were

inoperable

because

the heat exchanger of its

respective

CCW,

CCW train

B

was

out of service

for repairs.

The

licensee's

position was that:

1) two shutdown cooling loops were operable

because

a fully operable

CCW

system,

with

emergency

diesel

power

available,

was supplying both

shutdown cooling loops with cooling water,

2) because

CCW heat exchangers

are passive

rather than active fluid system

components,

they

do not fall under the single failure criterion for fluid

systems,

and

3)

TS

Amendment

56 incorporated

NRR's

long-term

shutdown

redundancy

requirements

expressed

in the letter dated

June ll, 1980,

from

the Director of the Division of Licensing to the licensee.

In

summary,

NRR

acknowledged

in

a

memorandum

to

Region II, dated

September

17,

1987,

that

the definition of "operability" in the

TS is

subject to a wide range of potential interpretations.

For plant operation

in

mode

5, Unit 1

TS 3.4. 1.4. 2 clearly requires

two redundant

shutdown

cooling loops;

however,

no Unit 1

TS clearly required

two redundant

CCW

cooling

loops.

Accordingly,

the

licensee

s

actions

in performing

maintenance

work

on

the

CCW system

heat

exchanger

in mode

5 does

not

constitute

a violation of Unit 1 TS.

This violation is withdrawn.

Closed

(Unit 2)

P2187-Ol:

Sorento

Electronics,

a subsidiary

of

GA

Technologies,

reported

in

a letter dated

February 23,

1987,

a possible

defective

co-axial

cable

used

in conjunction with the Regulatory

Guide

1.97,

Post-LOCA High Range Radiation Monitor.

This cable

was found to be

in

use

on St.

Lucie Unit 2.

The Licensee

conducted

a safety analysis.

(JPE-LR-018)

which concluded that the existing radiation monitors with

their

associated

coaxial

cables

are

acceptable

as

installed.

Addi-

tionally,

the radiation

monitors

have

been

shown to

meet the design

criteria for St.

Lucie Unit 2 and are not an unreviewed safety question.

Closed

(Unit 2)

UNR 50-389/87-17-01:

Containment

Penetration

Not In

Accordance

With Regulatory

Guide

1.63.

A recent

inspection (ref.

IE

Report 50-389/87-17

of Unit 2 identified

a

concern

with respect

to

conformance

with Regulatory

Guide 1.63,

Rev.

2, for the Maintenance

Hatch

Hoist Motor.

In resolving this concern,

the licensee

conducted

a review

of all electrical

circuits

routed

through containment

penetrations

to

ensure

proper

disposition

in

accordance

with the

Regulatory

Guide.

Additionally, the

scope of the review was

expanded;

by the licensee,

to

include all associated

circuits powered

from safety related

power sources

to verify conformance

with Regulatory

Guide

1 ~ 75,

Rev.

2.

The following

Unit 2

energized

non-essential

circuits penetrating

containment

were

identified by the licensee

as not meeting their commitments to Regulatory

Guides

1.63 or 1.75:

a.

Maintenance

Hatch Monorail Hoist (BKR-41381),

b.

Reactor Building Jib Crane Receptacle

(BKR-42151),

c.

Power Receptacle

257,

261,

265 and 271 (BKR-41278),

d.

Power Receptacle

227,

232,

258,

262 and 266 (BKR-42044),

e.

Power Receptacle

259,

263,

267 and 270 (BKR-41379) and

f.

Power Receptacle

260,

264,

268 and 269 (BKR-42148)

g.

Reactor Building Telescoping

Crane

(BKR - 42152),

and

h.

Reactor Building Elevator Starter

(BKR - 42149)

il

Additionally, the

above

listed

energized

circuits

do not comply with

license conditions

2.C. 10 and 2.C. 11, which state:

Non-Safet

Loads

on Emer enc

Power Sources

Section 8.4.2

SER

Prior to startup

following the first refueling outage,

the licensees

shall

implement the design modification to disconnect four-kilovolt

loads

on detection

of

a safety injection signal

and provide

two

isolation

devices

in series

for those

non-safety electrical

loads

that are

not disconnected

by

a safety injection signal

or loss of

offsite power.

Containment Electrical Penetration

(Section 8.4.3

SSER

3

Prior to startup

following the first refueling outage,

the licensees

shall

complete

the

design

modifications

to provide

independent

primary

and

backup fault protection for each electrical

conductor

penetrating

containment.

The failure to meet the license

conditions

2. C. 10

and

2. C. 11, for the

above

non-essential

circuits

penetrating

containment

is

a violation

(50-389/87-20-02).

The licensee

has

completed

a safety evaluation for the non-conformances

discovered

during their reviews.

The safety evaluation

concluded that the

non-conformances

are

not

a substantial

safety hazard,

and as

such are not

reportable

under

10 CFR 21.

Included

in the

licensee's

report,

are

recommended

actions for final disposition of these

non-conformances,

as

well

as

a safety evaluation

substantiating

these

recommendations.

The

recommended

actions

are to open the circuit breakers

during modes

1-4 for

those circuits identified in the safety evaluation.

Plant Engineering

(Juno) will provide

an engineering

package to modify the

sump

pump circuit

to conform to the

Reg.

Guide 1.75,

Rev.

2.

4.

Plant Tours (Units

1 and 2)

The inspectors

conducted

plant tours periodically during the inspection

interval to verify that monitoring equipment

was recording

as required,

equipment

was properly tagged,

operations

personnel

were

aware of plant

conditions,

and plant housekeeping

efforts were adequate.

The inspectors

also

determined

that

appropriate

radiation

controls

were

properly

established,

critical clean

areas

were being controlled in accordance

with

procedures,

excess

equipment

or material

was

stored

and

combustible

materials

and debris

were

disposed

of expeditiously.

During tours,

the

inspectors

looked

for the

existence

of unusual

fluid leaks,

piping

vibrations,

pipe

hanger

and seismic restraint settings,

various valve and

, breaker positions,

equipment caution

and danger tags,

component positions,

adequacy

of fire fighting equipment,

and instrument calibration dates.

Some tours were conducted

on backshifts.

The

inspectors

routinely conducted

partial

walkdowns of

ECCS

systems.

Valve,

breaker/switch

lineups

and

equipment

conditions

were

randomly

verified both locally

and in the control

room.

During the inspection

period

the

inspectors

conducted

a complete

walkdown in the accessible

areas

of the Units

1 and

2 component cooling water

(CCW), emergency diesel

generators

and

AC/DC electrical distribution systems

to verify that the

lineups

were in accordance

with licensee

requirements

for operability and

equipment material

conditions

were satisfactory.

Additionally, flow path

verifications

were

performed

on the following systems;

Units

1 and

2

chemical

volume control

and auxiliary feedwater

(AFW).

The

NRR Project

Manager

(PM) for the St.

Lucie Plant visited the site

September

15-18,

1987.

Me reviewed

a reactor trip (subject of LER 335/

87-13),

external

missile protection,

several

plant change/ modification

packages,

mangrove restoration efforts and conducted

various plant tours.

The

PM reviewed

the circumstances

associated

with the Unit 1 reactor trip

of June

14,

1987.

The

1B main feedwater

pump tripped

and the reactor

subsequently

tripped

on

a high pressurizer

pressure.

The review included

the

licensee

event

report

(LER), 335/87-13,

submitted to the staff by

letter dated July 10,

1987;

the monthly report submitted to the staff by

letter

dated July 15,

1987;

and the post-trip review report

(completed

Operating

Procedure

No.

0030119,

Revision 4,

dated

June

14,

1986).

Additionally, the

event

was

discussed

with the licensee.

An in-depth

review of the event

was

performed to evaluate

the possibility that. the

reactor

tripped

on

low steam

generator

water level,

versus

high pres-

surizer pressure,

and the discrepancy of whether the power-operated relief

valves

(PORV's)

opened

during the event.

The sequence

of events

recorder

indicated that the reactor tripped

on high pressurizer

pressure

followed

five seconds

later by a low steam generator

water level trip.

Apparently,

the pressurizer

pressure

increase

was

dominant over the loss of steam

generator

level.

As

a result of discussions

with the licensee

personnel,

it was

determined

that the time difference

between

the signal

to

open

the

PORV's

and the signal

to close the

PORV's

was less

than two seconds.

Therefore, it would be difficult to determine if they opened

under these

conditions.

However,

the post-trip report stated

that the

PORVs opened

but the

LER stated that they did not.

The licensee

agreed

to resolve the

discrepancy

by either revising the

LER or correcting the monthly report.

The

PM observed

that

some safety-related

equipment,

located outside,

are

not fully protected

from postulated

tornado/hurricane

generated

external

missiles.

The postulated

scenario

involves

a severe

weather condition

at the site,

a missile

being generated

and propelled toward the safety-

related

equipment,

the missile breaking

the

boundary of the equipment,

and the

subsequent

inability of the plant to achieve

cold shutdown, if

required.

Additional assumptions

include

no on-site electrical

power and

multiple missiles.

Equipment

observed

to have

a potential for being not

fully protected,

under certain

conditions,

are

the Unit 1 condensate

storage

tank,

two Unit 1 diesel

fuel oil storage

tanks,

two Unit, 1

component

cooling water

system

heat

exchangers,

and the refueling water

taken for each unit.

After detailed discussion with the licensee,

the

PM

was satisfied with the licensee's

response

and prior actions.

l

The technical

specifications

for both units require that the licensee

conduct

a

beach

survey and mangrove photographic

survey at least

once per

year.

These

surveys

are associated

with flood protection

measures

for the

site.

The results

of the

beach

survey

were submitted to the staff by a

letter dated July 7,

1987.

The results

indicated that the present

dune

condition

is

acceptable.

The

results

of the

mangrove

survey

were

submitted to the staff by letters

dated

March

2 and July 1,

1987.

The

results indicated that there

has

been

some deterioration of the mangroves.

As

a result,

the

licensee

performed

an

engineering

evaluation.

The

licensee

concluded that the mangroves

are not required to maintain design

basis

of the

St.

Lucie site

to protect safety-related

structures

and

equipment

from probable

maximum hurricane

surge

and erosion

damage.

Thus,

the licensee

determined

that the deterioration did not create

a condition

of any safety significance.

The licensee

has

embarked

on

a program to

rejuvenate

the

50

acre

mangrove

tract.

The licensee

has installed

a

piping system

to water the tract.

The piping system

draws water from the

intake

canal

and

pumps it through

PVC pipe to the northern

edge of the

50 acre tract,

where the water is released

along the edge of the tract.

Pooled water in the tract is eventually released

back to the intake canal.

The licensee

believes that much of the 50 acre tract will be restored

in a

few years.

The

PM believes that, although under

no requirement to do so,

the licensee is acting in a responsible

manner to restore

the tract.

A number of Unit 1 plant change/modification

packages

were

reviewed

by

the

PM.

Emphasis

was placed

on the safety evaluation

conducted

by the

licensee.

These

were St.

Lucie Unit 1/Unit 2 security systems

(141-81);

electrical

penetration

E-4 nozzle (003-184);

steam line radiation monitor

weather

enclosure

(024-184);

and

environmental

qual ification

update

(077-186).

Unit 2 plant change/modification

packages

were reviewed during

a prior 1987 site visit.

All safety evaluations

were adequate.

It should

be

noted

that

the security

system

plant change/modification

package

containing

safeguards

information was stored in a locked file cabinet,

as

required.

Additionally, the

environmental

qualification

update

plant

-change/modification

package

is

a

good

example of a

change

made

under

10 CFR 50.59 that is not hardware-orientated.

It demonstrates

that the

licensee

envelopes

all

changes

described

in the

FSAR into their change

program,

not just hardware

changes.

The

PM conducted

various tours.

Particular

emphasis

was

placed

on the

reactor auxiliary building (RAB) for each unit.

The

PM toured all levels

inside the

RAB's and the ground level outside the

RAB's and fuel handling

buildings.

All outside

doors

to the RAB's were closed

as required.

All

outside

doors

to the fuel handling buildings were closed

as required,

except for one

door

on the Unit 2 fuel'andling building, which was

open

because

new fuel

was just received on-site

and

was just

moved into the

building.

A guard

was posted

because

the door was

open

and personnel

were

working in the

immediate area.

The licensee

has

had

some problem, in the

past,

keeping

some exterior

RAB doors closed.

The reason for keeping the

doors

closed is if an airborne radiological release

occurred in the

RAB,

an open door would represent

an unmonitored

and unfiltered

escape

pathway,

partially bypassing

the

RAB ventilation cleanup

and filtration system,

Significant improvement

has

been

noted

and housekeeping

was excellent in

both RAB's.

The

PM noted

a possible

discrepancy

in the shield building wall penetra-

tion (no. 57)

associated

with the

containment

mini-purge

system line

(Unit 2).

Apparently,

the piping run went through the penetration,

but

the areas

between

the outside of the line and the inside of the penetra-

tion was

not sealed.

This discrepancy

was discussed

with the licensee.

The licensee

demonstrated,

by utilizing drawings,

that the

seal

between

the outside of the pipe and the inside of the penetration

was

made at the

inside of the shield building wall. 'dditionally, the licensee

stated

that leak tightness

of the annulus

area is periodically checked to ensure

that

there

is

no

unacceptable

leakage.

The

licensee's

explanation

resolved the

PM's concern.

Plant Operations

Review (Units 1 and 2)

The inspectors,

periodically during the

inspection

interval,

reviewed

shift logs

and

operations

records,

including data

sheets,

instrument

traces,

and records'f

equipment

malfunctions.

This

review included

control

room logs

and auxiliary logs, operating orders,

standing orders,

jumper

logs

and

equipment

tagout

records.

The

inspectors

routinely

observed

operator

alertness

and

demeanor

during plant tours.

During

routine

operations,

operator

performance

and

response

actions

were

observed

and

evaluated.

The

inspectors

conducted

random off-hours

inspections

during the reporting interval to assure

that operations

and

security

remained

at

an acceptable

level.

Shift turnovers

were observed

to verify that they were

conducted

in accordance

with approved licensee

procedures.

The inspectors

performed

an in-depth review of the following

safety-related

tagouts

(clearances):

Unit 1

1-9-64

1-9-94

1-10-7

1-10-8

Unit 2

PM On Reactor Trip Circuit Breakers

Pressure

Test - lA Charging

Pump

Pressure

Test -

1C Charging

Pump

Pressure

Test - 1B Charging

Pump

Tag Open Breakers

To Comply With

RG 1.63 and 1. 75

Repair

LCV-2110P

2C Charging

Pump - Adjust Accumulator Pressure

for Mode Change

Technical Specification

Compliance (Units 1 and 2)

During this reporting interval,

the inspectors

verified compliance with

limiting conditions

for operations

(LCO's)

and results

of selected

surveillance

tests.

These

verifications

were

accomplished

by direct

observation

of monitoring

instrumentation,

valve positions,

switch

positions,

and

review of completed

logs

and records.

The licensee's

compliance

with

LCO

action

statements

were

reviewed

on

selected

occurrences

as they happened.

Maintenance

Observation

Station

maintenance

activities of selected

safety-related

system

and

components

were observed/reviewed

to ascertain that they were conducted

in

accordance

with requirements.

The following items were considered

during

this review; limiting conditions for operations

were met, activities were

accomplished

using

approved

procedures,

functional tests

and/or calibra-

tions were performed prior to returning components

or systems

to service;

quality control

records

were maintained;

activities were -accomplished

by

qualified personnel;

parts

and materials

used

were properly certified;

and radiological

controls

were

implemented

as

required.

Work requests

were

reviewed

to determine

status

of outstanding

jobs

and to assure

the priority was

assigned

to safety-related

equipment.

The inspectors

observed portions of the following maintenance activities;

Unit 1

PWO 7608

Pre/Post

Test Calibration of IST Test Gages

Unit 2

PWO 5885

Auto Load Sequence

Test

Review of Nonroutine Events

Reported

by the Licensee

(Units

1 and 2)

The following Licensee

Event Reported

(LER's) were reviewed for potential

generic

impact,

to detect

trends,

and to determine

whether corrective

actions

appeared

appropriate.

Events which were reported

immediately were

also

reviewed

as

they occurred to determine that technical specifications

were

being

met

and that

the public health

and safety

were of upmost

consideration.

The following LER's are considered

closed:

Unit 1

87-13

87-14

Unit 2

Reactor

Trip on High Pressure,

Loss of

1B S/G

Feedpump

(ref.

paragraph

4, this report

and

IE Report

No. 335/87-14,

dated

July 28,

1987)

Unidentified

RCS

Leakage

Greater

Than

TS Limits (ref. paragraph

l2, this report).

87-06

2A and

2B Diesel Generator

Automatic Load Sequence

Relays Missed

Surveillance

On September

17,

1987,

the licensee's

gA organization

discovered that the

surveillance

for the

2A and

2B Emergency

Diesel

Generator

(DG) 12 month

test of the automatic

load sequence

relays

had not been properly completed

when

last

performed

(May 4,

1987).

The

review of the

surveillance

procedure

indicated that only the components

on the 4160 volt 2A3 and

2B3

switchgear

were tested.

The test did not include the components

on the

4160 volt

2AB switchgear

and

the

480 volt load centers/motor

control

centers.

Apparently,

the

May 1987

reviews

by individual(s) implementing

the

maintenance

surveillance

procedure

as

well

as

quality control

personnel

given charge of reviewing the plant work order and the surveil-

lance

maintenance

procedure

for'ompleteness

and

compliance

to the

surveillance

requirements

did not identify the incomplete surveillance

procedure.

The

immediate

and corrective actions

implemented

by the

licensee

were;

(1) electrical

maintenance

personnel

satisfactorily performed the required

surveillance

in accordance

with the approved procedure,

(2) plant manage-

ment

have

reemphasized

the

importance of adequate

review of plant work

orders

and surveillance

procedures,

and (3) the surveillance

procedure

was

revised for clarity.

Unit 2 technical specification (TS) 4.8. 1. 1.2.d

requires

that while

operating

in modes

1,

2,

3,

and

4 each diesel

generator

shall

be demon-

strate

operable

by verifying at least

once

per

12

months

that

the

automatic

load

sequence

times

are

operable.

The last

12

month

DG

surveillance

of the

automatic

load

sequence

relays

was satisfactorily

performed in May 1986.

As an .immediate action the surveillance

procedure

was performed satisfactorily

on September

18,

1987.

This is approximately

18 days

past

the

TS allowable

25K extension of the testing interval.

The

surveillance

was

completed,

with all

components

testing satisfactorily,

approximately

22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br /> after discovery of the

incomplete

status

of the

previous surveillance of May 4,

1987.

In summary,

the failure to properly complete

the scheduled

surveillance

of the diesel

generator

on .May 4,

1987

and the subsequent

exceeding

the

allowed

25K extension

is

a violation of Unit 2

TS.

However,

since it

was identified by the licensee,

considered

to be severity level IV or V,

reported,

corrected

within a reasonable

length of time,

and

was not

a

violation which could be expected

to have

been prevented

by the licensee's

previous

corrective

actions,

in accordance

with 10 CFR 2,

Appendix

C,

V.A., a Notice of Violation will not be issued.

Physical

Protection (Units 1 and 2)

The inspectors verified by observation

and interviews during the reporting

interval

that

measures

taken to assure

the physical

protection of the

facility met current requirements.

Areas inspected

included the organiza-

tion of the security force,

the establishment

and maintenance

of gates,

doors

and isolation

zones

in the proper conditions,

that access

control

and badging

was proper,

and procedures

were followed.

Surveillance

Observations

During the

inspection period,

the inspectors

verified plant operations

in compliance with selected

technical

specifications

(TS) requirements.

Typical of these

were confirmation of compliance with the

TS for reactor

coolant

chemistry,

refueling water, tank,

containment

pressure,

control

room ventilation

and

AC

and

DC electrical

sources.

The

inspectors

verified that

testing

was

performed

in

accordance

with

adequate

procedures,

test instrumentation

was calibrated,

limiting conditions for

operations

were

met,

removal

and restoration

of the affected

components

were

accomplished,

test

results

met requirements

and

were

reviewed

by

personnel

other

than

the individual directing the test,

and that

any

deficiencies

identified during the testing

were properly reviewed

and

resolved

by appropriate

management

personnel.

The inspectors

observed

portions of the following surveillance(s):

10

Unit 1

1-0110050 Control Element Assembly Periodic Exercise

1-0010125

Check Sheets

1, 2, 3, 4, 6,

and 10;

and Data Sheets

1, 3,

4,'nd

9

HP-4

Attachment B-Daily Area Surveys

Unit 2

HP-4.2

Health Physics

Weekly Checks

Boric Acid/Safety Injection Tanks - Activity/Concentration

Refueling Outage

Review

During the inspection period,

the inspector

observed

certain

aspects

of

the licensee's

preparations

for refueling of Unit 2 (scheduled,

October

3

thru November 1).

The following objectives

were addressed:

b.

Ascertain

the

adequacy

of licensee

procedures

for the conduct of

refueling operations,

Ascertain

the

adequacy

of the licensee's

administrative

requirements

for control of:

(1)

Refueling operations,

and

(2)

Plant conditions during refueling,

and

c.

Ascertain

the

adequacy

of the licensee's

implementation of controls

for items 2a.

and b.,

above,

The

inspector

reviewed

the following refueling related

procedures

to

ensure

that

the

licensee

had

implemented

controls for the

conduct of

refueling operations

and for establishing

and maintaining control of plant

conditions in accordance

with technical specifications:

~0eratione

2-0030127

2-0030128

2-011022

2-0120021

2-1600022

2-1600023

2-1610020

2-1630021

2-1630022

2-1630023

2-1630024

2-1630025

2-1630028

Reactor Plant Cooldown - Hot Standby to Cold Shutdown

Reactor

Shutdown

Coupling and Uncoupling of Control Element Assembly

(CEA)

Extension Shafts

Draining the Rector Coolant System

Unit 2 'efueling Operation

Refueling Sequencing

Guidelines

Receipt

and Handling of New Fuel

New Fuel Elevator Operation

.

Spent

Fuel Handling Machine Operation

Fuel Transfer System Operation

Refueling Machine Operation

CEA Change Fixture Operation

New Fuel Handling Crane Operation

11

Administration

0005746

Outage

Management

0010438

Control of Heavy

Load Lifts

Maintenance

2-M-0036

Reactor

Vessel

Maintenance - Sequence

of Operations

Instrument'and

Control

2-120054

Low Temperature

Overpressure

Protection Setpoint Verification

~ll

1th Ph

HP-23

Health

Physics Activities in the Reactor

Containment

Building

During Shutdown

HP-40A

Receipt of Radioactive Material

Review of Plant Events

On October 8,

1987, with Unit 1 in mode

1 at

100K power, during

a leak

rate

calculation,

the

licensee

discovered

that unidentified

reactor

coolant

leakage

was

1.08 gpm, greater

than the

TS limit of 1 gpm.

An

unusual

event

was declared

at 5:29 a.m.

and

the

NRC notified (ref.

PN).

Operations

personnel

entered

containment

at 5:30 a.m. to investigate

and

possibly identify the

source

of the leakage.

The containment entry team

reported

leaks in, several

reactor

coolant

pump

(RCP) areas.

At 6: 12 a.m.,

a reactor

shutdown

was

commenced

so that detailed

investigations

could be

conducted

in containment.

At 9: 13

a.m.

the turbine was

removed from the

grl d.

At. 9: 30 a. m.,

another

containment

entry

was

conducted

by

a

team of

operators

and

maintenance

personnel

to reassess

the leaks.

From this

investigation it was discovered that the

1A1

RCP vapor seal

was slinging a

mist of water.

Additionally, the

1A2

RCP vapor seal

was showing signs of

leakage

along with the 1Bl charging

header

to the

1B1 loop

and safety

injection line to the 182 loop.

Because

the exact sources

of the leakage

could not

be identified the licensee

decided

to remain in an

unusual

event.

The licensee

assigned

a

team to evaluate

the event

and prepare

a plan to

positively identify the leak sources

and plan for necessary

repairs.

At

12:05 p. m.,

the unit was

shut

down and in mode 3.

The unusual

event

was

terminated

at 2:05 p.m.

because

the

RCS

leaks

were

now identified with

total identified leakage

less than the

TS limit of 10 gpm.

12

The following sources

of leakage

were identified and repaired:

a+

b.

C.

d.

e.

lAl RCP seal

leak from a cracked weld joint on a seal

nozzle flange,

1B1 loop 2-inch charging line check valve cover plate gasket

leak,

1B2 loop 12-inch safety injection line check valve hinge pin gasket

leak,

2-inch pressurizer auxiliary spray line check valve gasket

leak,

1B1 loop 3-inch pressurizer

main spray line check valve gasket

leak,

and

a minor

PORV discharge

flange gasket

leak.

Maximum unidentified

leakage

recorded

during the event

based

on letdown

system mismatch

was 4.9

gpm.

The failure of the lA1 RCP seal

cracked weld

was probably responsible

for the leak rate going from less

than to greater

than

1

gpm unidentified over

a short period of time (between

normal leak

rate calculations).

All leaks

were repaired

and the unit returned

to

service

on October 18,

1987.

On

October 25,

1987,

while

reassembling

the

Unit 2

reactor

vessel

internals

and performing

a liftof the in-core instrument (ICI) plate onto

the work platform,

the plate

was

deformed

due to excessive

force being

applied

using the polar crane.

The procedure,

2-M-0036,

Reactor

Vessel

Maintenance - Sequence

of Operations,

paragraph

9. 10.36,

requires that the

load cell readout

be continuously

observed

during the lift and that the

free

hanging weight not

be

exceeded

by more than

600 lbs.

Oue to the

confusion caused

by the shift change

and the use of the crane, without the

load cell, for other lifts in containment

immediately following the shift

change,

the

load cell

was

not reinstalled prior to continuing procedure

2-M-0036.

The failure to continuously observe

the load cell readout

when

proceeding

to step

37 of the procedure

resulted in the deformation of the

instrument

plate.

This is

a violation of Unit 2

TS 6. 8. 1, failure to

establish/implement

procedures, first example

(50-389/87-20-01).

As of the

end of the reporting period, the licensee

had completed taking

measurements

to determine

the extent of the ICI plate deformation

and

inspections

of the plate welds.

The plate

was

found to have

a maximum

deformation

on the outer edge or rim of 1 7/8 inches.

The manufacturer's

specification

is

a

maximum

1/2

inch deformation.

Additionally, the

licensee

was in the process

of fabrication the tools, in accordance

with

Combustion

Engineering

recommendations,

necessary

for straightening

the

plate.

The licensee

has

completed

a review of other lifts which had been

performed

previously during the

outage

to ensure'hat

all lifts were

conducted

properly.

No further problems

were identified.

The outage

was

expected to be delayed approximately

seven

days.

On October 28,

1987, the licensee

had removed the Unit 1 turbine generator

from the grid to balance

the generator exciter.

The exciter

had developed

a vibration

problem earlier in the

month.

On October 29,

1987, after

13

successfully

completing balancing of the exciter and returning the turbine

generator

to service,

the turbine operator inadvertently stopped

the only

operating

condensate

pump,

the

1A pump.

Subsequently,

a trip of the main

feed

pump occurred

and at 3:35 a.m., at 20K power,

and the reactor tripped

on low steam generator

water level.

All system functioned

as designed.

The

1A condensate

pump was stopped while electric realigning the operating

condensate

pumps

(from lA and

1B to

1A and

1C operating).

After

completing

the

pump electrical

realignment,

using procedure

1-0700020,

Condensate

and

Feedwater,

the operator

encountered

problems

removing one

(of three)

of the interlock keys required for changing

the disconnect

lineup.

The control

room

was

informed of the

problems

and sent

an

electrical

supervisor

to the disconnect

area to provide assistance

to the

operator.

At this point, for reasons

undetermined,

the operator inserted

one of the three

keys into the

1A pump electrical

disconnect

l.ock.

The

interlock was

then activated

which tripped the remaining,

lA condensate

pump.

The interlock prevents

either

opening

an energized

disconnect

or

aligning the

1C

condensate

pump to two independent

power sources.

In

summary,

the

procedure,

1-070020,

was

inadequate

because it does

not

specify

how

or. under what conditions

the interlock keys

may

be removed

after

the

disconnect

lineup is

completed.

Additionally, the operator

failed to follow procedures,

~ in that,

upon

encountering

problems

in

removing

the last

remaining

key,

he inserted

another

key without the

utilization of the

procedure.

This is

a violation of Unit 1

TS 6.8. 1,

failure to establish/implement

procedures,

second

example,

(50-335/87-

21-01).

While recovering

from the event described

above,

on October 29,

1987, with

statup

operations

in progress,

shutdown

rods withdrawn

and Unit 1 not

critical at

5:42 a.m.,

the unit tripped

on

a spurious

channel

B high

startup

rate

(SUR).

All equipment functioned

as designed.

Channel

C

SUR

was tripped

because

of previous

problems with the instrument.

When the

spurious

channel

B

SUR occurred the required

2 out of 4 logic was

made

up,

initiating the

reactor trip.

The licensee

repaired

channel

C, placed

channel

B in bypass

and

commenced

a reactor startup.

The reactor

was

critical at 11: 10 a.m.

and the unit placed on-line at 1: 10 p.m. the

same

day.

No further problems

were experienced.