ML17219A592
| ML17219A592 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 05/14/1987 |
| From: | Stohr J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | Woody C FLORIDA POWER & LIGHT CO. |
| References | |
| NUDOCS 8705280478 | |
| Download: ML17219A592 (4) | |
See also: IR 05000335/1987004
Text
Fgorida
Power and Light Company
~ATTN:
Mr. C. 0.
Woody
Group Vice President
Nuclear Energy Department
P. 0.
Box 14000
Juno
Beach,
FL
.33408
Gentlemen:
SUBJECT:
REPORT
NOS. 50-335/87-04
AND 50-389/87-04
Thank you for your response
of April 27,
1987, to our Notice of Violation,
issued
on March 27,
1987,
concerning activities
conducted
at your St. Lucie
facility.
We
have
evaluated
your
response
and
found that it meets
the
requirements
of
We will examine
implementation
of your
corrective actions during future inspections.
We appreciate
your cooperation in this matter.
Sincerely,
C I/5sL SlGNFD
FY
D-."'. L~.S V.. C:@Litic
g'.
Philip Stohr, Director
Division of Radiation Safety
and Safeguards
cc:
.
N. Harris, Vice President
/St. Lucie Nuclear Plant
A. Sager,
Plant Manager
B. Harper, Site
gA
Superintendent
87052
DOCH 05PP0335
80478 870514
G
bcc:
NRC Resident
Inspector
Document Control
Desk
State of Florida
RII
RII
RI
5Q /87
5/ 7/87
5/ p /87
RII
~i/amgs
[~ tR3
8Wil Son
/I/8~//z
5/tI'5/87
g(iyP)
In your response
to Violation A(1), you stated that you did not agree that the
requirement for minimum volume of liquid in waste
was not met
and that tests
conducted
Department of Health
and
Environmental
Control,
FPL and
Chem Nuclear indicated that the criteria for minimum volume of liquid
(O.M) had
been
met.
The regulations
specify that in no case
shall liquid
exceed
0.5% of the volume of the waste for waste
processed
to
a stable
form.
Liquid is not defined by the regulations
as water but may be any physical state
characterized
by the free
movement of material.
As verified by your
own
guality Assurance
audit,
one liner in the
shipment
in question failed to
solidify, as
evidenced
by
a paste-like
material
flowing from the liner when
punctured,
while the
second
contained
a
mass
equal
to approximately
85K
solidification.
It is the
NRC position that the requirement for 0.5% minimum
volume of liquid means that 99.5X of the volume of the waste will be solid.
In
the
case of your liners,
one was free flowing when punctured
and the other was
only 85% solidified.
Therefore,
the criteria for minimum volume of liquid in
your shipment
was not met and the violation is considered
correct
as stated.
REGULATORY INFORMATION DISTRIBUTION SYSTEN
(R IDS)
ACCESSION
NBR: 8705280478
DOC. DATa: 87/05/14
NOTARI2 ED:
NO
FACIL:50'335 St.
Lucie Planti
Unit iz Florida Power 5 Light
CD.
.50-389 St.
Lucie Plant>
Unit 2i Florida Power
5 Light Co.
AUTH. NAME
AUTHOR AFFILIATION
STOHRi P. J
Region
2i Office of Director
RECIP. NANE
RECIPIENT AFFILIATION
WOODY'. O.
Florida Power
8< Light Co.
DOCKET
05000335
05000389
SUBJECT:
Ack receipt of 870427 res'ponse
to violations noted
in Insp
Repts
50-335/87-04
Sc 50-389/87-04. Violation Ai concerning
failure tD satisfy criteria re min vol of liquid in radwaste
shipmenti considered
correct
as
s+ated.
DISTRIBUTION CODE:
IEOID
COPIES
RECEIVED: LTR J
ENCL Q SIZE:
TITLE: Qeneral
(50 Dkt)-Insp Rept/Notice of Violation Response
NOTES:
RECIPIENT
ID CODE/MANE
PD2-2 LA
TOURIQNY> E
INTERNAL: AEOD
ENF LIEBERNAN
NRR/DOEA DIR
NRR/DREP/RPB
NRR,
8/ ILRB
RQN2
FILE
01
EXTERNAL:
LPDR
COPIES
LTTR ENCL
1
1
1
T
1
1
1
RECIPIENT
ID CODE/NANE
PD2-2
DEDRO
ROEi N. L
NRR/DREP/EPB
NRR/DR IS DIR
OGC/HDS2
DEPY QI
NRC
COP IES
LTTR ENCL
TOTAL NUMBER OF COPIES
REQUIRED:
LTTR
21
ENCL
tQI5 I
F~rida
Power and Light Company
~ATTN:
Mr. C. 0.
Woody
~
~
~
~
~
Group Vice President
Nuclear Energy Department
P. 0.
Box 14000
Juno Beach,
FL
33408
Gentlemen:
SUBJECT:
REPORT
NOS. 50-335/87-04
AND 50-389/87-04
Thank you for your response
of April 27,
1987, to our Notice of Violation,
issued
on March 27,
1987;
concerning activities
conducted
at your St.
Lucie
facility.
We
have
evaluated
your
response
and
found that it meets
the
requirements
of
We will examine
implementation
of your
corrective actions during future inspect;ions.
We appreciate
your cooperation
in this matter.
Sincerely,
C"'='I/I.l. SIGNF.D 8Y
D O'P.S
M. COLL(tiS Q
J. Philip Stohr, Director
Division of Radiation Safety
and Safeguards
cc:
.
N. Harris, Vice President
JSt.
Lucie Nuclear Plant
~
~
A. Sager,
Plant Manager
B. Harper, Site
gA
Superintendent
8705
DOC~ 05ppp>35
804.78
S705> +
ADO
6
bcc:
NRC Resident
Inspector
Document Control
Desk
State of Florida
RII
RII
RI
RII
5Q /87
5/ 7/87
5/ I /87
5/['7/87
NVP/among
II/S~//<
In your response
to Violation A(1), you stated that you did not agree that the
requirement for minimum volume of liquid in waste
was not met and that tests
conducted
by South
Carolina
Department of Health
and
Environmental
Control,
FPL and
Chem Nuclear indicated that the criteria for minimum volume of liquid
(0.5%)
had
been
met.
The regulations
specify that in
no case
shall liquid
exceed
0.5X of the volume of the waste for waste
processed
to
a stable
form.
Liquid is not defined
by the regulations
as water but may be any physical state
characterized
by the free
movement of material.
As verified by your
own
quality Assurance
audit,
one liner in the
shipment
in question
failed to
solidify, as
evidenced
by
a paste-like
material
flowing from the liner when
punctured,
while the
second
contained
a
mass
equal
to approximately
85Ã
solidification.
It is the
NRC position that the requirement for 0.5% minimum
volume of liquid means that 99.5% of the volume of the waste will be solid.
In
the case of your liners,
one was free flowing when punctured
and the other was
only 85K solidified.
Therefore,
the criteria for minimum volume of liquid in
your shipment
was not met and the violation is considered
correct
as stated.
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION
NBR: 8705280478
DOC. DATE.: 87/05/14
NOTARIZED:
NO
FACIL:50"335 St.
Lucie Plant>
Unit
1> Florida Power 5 Light Co.
.50-389't.
Lucie Plant>
Unit 2> Florida Power
8< Light Co.
AUTH. NAME
AUTHOR AFFILIATION
STOHR> P. J.
Region
2> Office of Director
RE CIP. NAME
RECIPIENT AFFILIATION
WOODY> C. O.
Florida Power
Zc Light Co.
DOCKET
N
05000335
05000389
SUB JECT:
Ack receipt of 870427 response
to violations noted
in Insp
Repts
50-335/87-04
8c 50-389/87-04. Violation A> concerning
failure to satisfy criteria re min vol of liquid in radwaste
shipment> considered
correct
as stated.
DISTRIBUTION CODE:
IEOID
COPIES
RECEIVED: LTR J
ENCL + SIZE:
TITLE: General
(50 Dkt)-Insp Rept/Notice of Violation Response
NOTES:
RECIPIENT
ID CODE/NAME
PD2-2 LA
TOURIGNY> E
COPIES
LTTR ENCL
RECIPIENT
ID CODE/NAME
PD2-2
COPIES
LTTR ENCL
INTERNAL: AEOD
ENF LIEBERMAN
NRR/DOEA DIR
NRR/DREP/RPB
AIR~8A
.ffEG FIL
RCA2
FILE
01
EXTERNAL: LPDR
1
1
1
2
1
DEDRO
ROE> M. L
NRR/DREP/EPB
ttRR/DRIS DIR
OGC/HDS2
DEPY GI
t!RC
TOTAL NUMBER OF COPIES
REQUIRED:
LTTR
21
ENCL