ML17202U794
| ML17202U794 | |
| Person / Time | |
|---|---|
| Site: | Dresden |
| Issue date: | 08/16/1990 |
| From: | Miller H NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | |
| Shared Package | |
| ML17202U793 | List: |
| References | |
| 50-237-90-20, 50-249-90-20, NUDOCS 9008270036 | |
| Download: ML17202U794 (2) | |
Text
NOTICE OF VIOLATION Cummonwealth Edison Compariy Dresden Nuclear Power Station Units 2 and 3 Docket Nos. 50-237.; 50-249 Licenses. No. DPR-19; No. DPR-25 As a result *of the inspt:ction conducted on Ma.y 21 through June 21, 1990, and in accordance with the "General Statcrr:ent*of Policy and Procedure for NRC Enforcement Actions," 10 *CFR Part 2, Appcridix C, (1990) (Enforcernent Policy) the following violaticins were identified:
- 1.
10 CFR S0.49, Paragraph (f): r_equfres that each item of electrical equipment important to safety be qualified by testing and/or analysis of an'identical item of equipment under identic~l conditions,* or a similar ite~ or under similar conditions with a. supporting analysis to show that the equipment to b~ qu~lified is acceptable.
Contrary to the above, the. following examples of electrical equipment impot~tant to safety were not propc:rly c;ualified by EQ tests and/or analysis:.
('a)
. ( b)
( C).
(d)
Six splices made of cloth tape.wrapped over plastic in_sulation tape were found inst~lled in th~ powe~ and coritrol ~i~cuits fot the HPCI U~i*t 2 Turbine St~im Supply'I~olat~on Valve.
Two stub splices with wire nuts were-installed on ~he Reactor *Coolant.
~ost~Accident Sample Valve in Unit 3.
Two Voltrex heat shrink splices were install~d in the *heat trace
- circuit for the Hydrogen Analyzer in Unit 2.
Four Amphenol corinectors encapsulated in Voltrex heat shrink tubing were installed in the instrur;;t:r:t. circuits to the* Unit 3 containment High Range Radiation Monitors.
This is a Severity Level IV violation (Supplement I.D).
2~
10 CFR 50.49, Paragraph (j), requires_ a record of qullificati.on be
~aintained in ari auditable forffi for the entire period in whic~ the covered
- item is installed in the plarit.
'"~'.'i*:}:*.* :'
-::.... ~*.
Contrary to the above, as of A;:Jrii 1989,--the licensee's EQ files did not contain EQ tests and/or analysis which demonstrated qualification.6f.
- forty-three (43) General Electric (GE) CR 151 terminal blocks* four (4)
GE 2960 terminal blocks, one:,:) Cir.ch.terminal block, one (i) Marathon 6000 terminal block, and eleve~ *~1; elettrical enclosures jnstalled without the requ.ired weepholes in ~i~h Energy Line Break (HELB)/radiation areas. In addition, the licensee's C file for Marathon terminal blocks failed to identify 64 Marathon 1500 !600 EQ terminal blocks which were found installed in EQ circuits in H LB and/or radiation environments.
. ~-. --.
I l
2 This is a Severity Level IV violation (Supplement I.D).
Pursuant to th~ provisions of 10 CFR 2.201, you are required to submit to this office within thirty days of the date of this Nbtice a written statement or explanation in repiy, including for each violation:
(1) thE: corrective steps that have been taken and the results achieved; (2) the corrective steps that will be taken to avoid further violations~ and (3) the date when full complia~ce will be achieved.
Consideration may be given to extendin~ your _response time for good cause show11.
Dated H. J. Mier, Di rector :.
Division of Reactor Safety*
- ,*