ML17194A543

From kanterella
Jump to navigation Jump to search
IE Insp Repts 50-010/81-21,50-237/81-38 & 50-249/81-31 on 811231-820129.Noncompliance Noted:Several safety-related Equipment Areas Had Significant Quantities of Combustible Matls Present
ML17194A543
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 03/09/1982
From: Jordan M, Reimann F, Tongue T, Walker R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17194A541 List:
References
50-010-81-21, 50-10-81-21, 50-237-81-38, 50-249-81-31, IEB-80-11, NUDOCS 8203250577
Download: ML17194A543 (9)


See also: IR 05000010/1981021

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Reports No. 50-010/81-21; 50-237/81-38; 50-249/81-3l(DPRP)

Docket Nos.50-010, 50-237, 50-249

Licensee:

Commonwealth Edison Company

P. O.Box 767

Chicago, IL

60690

Licenses No. DPR-02, DPR-19, DPR-25

Facility Name:

Dresden Nuclear Power Station, Units 1, 2, and 3

Inspection At:

Dresden Site, Morris, IL

Inspection Conducted:

December 31, 1981 through January 29, 1982

Inspectors:

T. M. Tongue

M. J. Jordan

~µ:.~~~~~-

F W. Reimann*

Approved By:

R. D. Walker

Inspection Summary

Inspection from December 31, 1981 through January 29, 1982 (Reports

No. 50-010/81-21, 50-237/81-38, 50-249/81-31(DPRP))

Areas Inspected:

Routine *unannounced resident inspection of Followup on

Previous Inspection Findings, Operational Safety Verification, Monthly

Maintenance Observation, Monthly Surveillance Observation, Unusual Events,

Plant Training, Plant Trips, Refueling Activities, Refueling Surveillance,

Refueling Maintenance, Inspection During Long Term Shutdown, Regional

Requests, Licensee Identified Items, and Bulletin Review.

The inspection

involved 202 inspector-hours onsite by three NRC inspectors, including 42

inspector-hours during offshift.

Results:

Of the 14 areas inspected, no items of noncompliance were

identified in 13 areas; one item of noncompliance was identified in one

area(inadequate housekeeping - Paragraph 3).

8203250577 820309

PDR ADOCK 05000010

Q

PDR

'*

DETAILS

SECTION 1

1.

Persons Contacted

  • D. Scott, Station Superintendent
  • R. Ragan, Operations Assistant Superintendent

J. Eenigenburg, Maintenance Assistant Superintendent

  • D. Farrar, Administrative Services and Support Assistant Superintendent

J. Brunner, Technical Staff Supervisor

J. Wujciga, Unit 1 Operating Engineer

J. Almer, Unit 2 Operating Engineer

M. Wright, Unit 3 Operating Engineer

T. Ciesla, Assistant Technical Staff Supervisor

D. Adam, Waste Systems Engineer

D. Sharper, Radiliogical Waste Foreman

  • G. Myrick, Rad-Chem Supervisor

B. Saunders, Station Security Administrator

  • B.Zank, Training Supervisor
  • E. Wilmer, QA Coordinator
  • R. Stobert, QA Engineer

The inspector also talked with and interviewed several other licensee

employees, including members of the technical and engineering staffs,

reactor and auxiliary operators, shift engineers and foremen, electrical,

mechanical and instrument personnel, *and contract security personnel.

  • Denotes those attending one or both exit interviews conducted on

January 22 and 29, 1982.

2.

Followup on Previous Inspection Findings

3.

(Closed) Inspection Item 50-249/81-14-02.

The inspector found that the

licensee had completed the necessary repairs to the 150 ton overhead

reactor building crane.

The repairs included using the services of a

private engineering firm for evaluation and consultation.

The licensee

did not write a licensee evaluation report on this problem because the

crane was not used in the Restricted Mode condition identified in

Technical Specifications.

Operational Safety Verification

The inspector observed control room operations, reviewed applicable

logs and conducted discussions with control room operators during

the period of December 31 through January 29, 1982.

The inspector

verified the operability of selected emergency systems, reviewed

tagout records and verified proper return to service of affected

components.

Tours of Unit 2 reactor buildings and turbine buildings

were conducted to observe plant equipment conditions, including

2

potential fire hazards, fluid leaks, and excessive vibrations and to

verify that maintenance requests had been initiated for equipment in

need of maintenance.

The inspector by observation and direct inter-

view verified that the physical security plan was being implemented

in accordance with the station security plan.

The inspector observed plant housekeeping/cleanliness conditions and

verified implementation of radiation protection controls.

During the

period of December 31, 1981 through January 29, 1982, the inspector

walked down the accessible portions of the Unit 2 Core Spray, Standby

Liquid Control, 2A LPCI, 2/3 Diesel Generator, and Unit 2 Diesel

Generator systems to verify operability.

The inspector also witnessed

portions of the radioactive waste system controls associated with

radwaste shipments and barreling.

,.

While conducting routine plant tours during this inspection period,

the inspectors noted several locations with significant quantities

of combustible materials accumulated. in safety related equipment

areas.

Examples are:

(1) On January 26, 1982, in the Unit 2 Emergency

Diesel Gene.rator room, loose papers, wood, and oil scattered around

the room and engine foundation, plus a GI can without a lid, con-

tained used oil filters, oil rags, papers, and plastic, (2) On January 27,

1982, in the Unit 2/3 Emergency Diesel Generator room, about 12 open

oi.l drums with as much as several gallons of 'oil remaining in each

barrel, an open refuse barrel overflowing with oily rags, papers, wipes,

etc., plus considerable rags, wipes and oil were on the floor and work

bench.

In addition, there was evidence that individuals had been smoking

in the area by the presence of numerous cigarette butts, burned matches

and an empty match book on the floor.

It was found that the combus-

tibles in the Unit 2/3 Diesel Generator room were apparently left

from maintenance work that had been conducted during the previous

week.'

This is contrary to ANSI 18.7-1976, Section 5.2.10 which the

licensee is committed to under their Quality Assurance Program.

This

is an item of noncompliance (50-237/81-38-01 and 50-249/81-31-01).

A

similar noncompliance (10/80-19-01; 237 /80-21-01; and 249 /80-25-01)

brought about licensee corrective action in the form of a new adminis-

trative procedure DAP 3-11 which identified responsibilities for plant

cleanliness.

This is a significant breakdown in that corrective action.

Along with the combustibles left from maintenance and/or surveillance

work, the inspectors noted access covers missing or out of place as

follows on the Unit 2 Emergency Diesel Generator: *.access cover over

the engine fly wheel unlatched and hanging open; a cover over a micro-

switch on the engine governor open and hanging by one screw; and

the cover missing from an electrical junction box for engine exhaust

RTDs.

Each of these items by themselves may appear insignificant;

however, they show evidence of carelessness in completion of work

assignments and could lead to eventual personnel injury or degradation

of exposed equipment.

This concern of the inspectors was relayed to

station management.

The inspectors will follow licensee corrective

actions.

The station superintendent pointed out that this had been

3

previously identified independently by non NRC personnel.

This is

open inspection item (50-237/81-38-02) and (50-249/81-37-02).

One item of noncompliance was identified.

These reviews and observations were conducted to verify that facility

operations were in conformance with the requirements established under

technical specifications, 10 CFR, and administrative procedures.

4.

Monthly Maintenance Observation

. 5.

Station maintenance activities of safety related systems and com-

ponents listed below were observed/reviewed to ascertain that tµey

were conducted in accordance with approved procedures, regulatory

guides and industry codes or standards and in conformance with

  • technical.specifications.

The following items were considered during this review:

the limiting

conditions for operation were met while components _or systems were

removed from service; approvals were obtained prior to initiating the

work; activities were accomplished using approved procedures and were

inspected as applicable; functional testing and/or calibrations were

performed prior to returning components or systems to service; quality

control records were maintained; activities were accomplished by

qualified personnel; parts and materials used were properly certified;

radiological controls were implemented; and, fire prevention controls

were implemented.

Work requests were reviewed to determine status of outstanding' jobs

and.to assure that priority is assigned to safety related equipment

maintenance which may affect system performance.

The following maintenance activities were observed/reviewed:

ii

Unit 2

2/3 Emergency Diesel Generator

Following completion of maintenance on the 2/3 Emergency Diesel

Generator, the inspector verified that this system had been returned

to service properly.

No items of noncompliance were identified .

Monthly Surveillance Observation

The inspectors observed technical specifications required surveillance

testing on portions of the Unit 2 RBCCW Service Water Radiation Monitor

and the High Steam Flow Isolation Surveillance and verified that testing

was performed in accordance with adequate procedures, that test instru-

mentation was calibrated, that limiting conditions for operation were

met, that removal and restoration of the affected components were

4

accomplished, that test results conformed with technical specifications

and procedure requirements and were reviewed by personnel other than

the individual directing the test, and that any deficiencies identified

during the testing were properly reviewed and resolved by appropriate

management personnel.

No items of noncompliance were identified.

6.

Unusual Event

The licensee declared an unusual event on January 19, 1982, upon

detection of a release of airborne radioactive material on the

refuel floor in the Reactor Building.

The release occurred as a

result of polishing the Unit 3 reactor vessel feed nozzles for

  • feed sparger replacement.

Initial indications showed release levels

about three times the Technical Specification limit of 0.12 µC/sec.

The licensee evacuated the Reactor Building, secured Reactor Building

Ventilation, and started the Standby Gas Treatment system.

The licensee

also made the required notifications to the NRC and State of Illinois.

Upon being informed by Region III management personnel, the SRI reported

to the site and remained until the event was cleared.

Later licensee

actions were to verify that the Reactor Building air activity had re-

turned to normal, and then to return the ventilation systems to normal.

Licensee personnel then commenced decontamination of affected areas.

Samples of snow, dirt, and air outside the site fence showed no

indication of an offsite release.

Later reevaluation by the licensee

and consultation with Region III health physics personnel showed that

the air activity did not exceed the allowable limits.

No items of noncompliance were identified.

7.

Review of Plant Operations

During the period of December 31, 1981 through January 29, 1982, the

inspector reviewed the following activities:

Training

The inspector attended one of the licensee's operator requalification

lecture series and verified that lesson plan objectives were met and

that training was in accordance with the approved operator requalifi-

cation program schedule and objectives.

No items of noncompliance were identified.

8.

Plant Trips

Following the plant trips of Unit 2 on January 26, 1982 the inspector

ascertained the status of the reactor and safety systems by observa-

tion of control room indicators and discussions with licensee personnel

concerning plant parameters, emergency system status and reactor coolant

5

chemistry.

The inspector verified the establishmerit of proper communi-

cations and reviewed the corrective actions taken by the licensee.

All

systems responded as expected, and the plant was returned to operation

on January 27, 1982.

No items of noncompliance were identified.

9.

Refueling Activities

The inspector verified that prior to the handling of fuel in the

core, all surveillance testing required by the technical specifica-

tions and licensee's procedures had been completed; verified that

during the outage the periodic testing of refueling related equipment

was performed as required by technical specifications; observed six

shifts of the fuel handling operations and verified the activities

were performed in accordance with the technical specifications and

approved procedures; verified that containment integrity was main-

tained as required by technical specifications; verified that good

housekeeping was maintained on the refueling area; and, verified that

staffing during refueling was .in accordance with technical specifi-

cations and approved procedures.

The inspectors also walked down accessable portions of the following

ECCS systems to verify operability.

Unit 3

Standby Liquid Control Syst~m

LPCI

Core Spray

No items of noncompliance were identified.

10.

Surveillance - Refueling

The inspector observed the calibration of ARM surveillance testing on

Unit 3 to verify that the tests were covered by properly approved pro-

cedures; that the procedures used were consistant with regulatory

requirements, licensee commitments, and administrative controls; that

minimum crew requirements were met, test prerequisites were completed,

special test equipment was calibrated and in service, and required data

was recorded for final review and analysis; that the qualifications of

personnel conducting the test were adequate; and that the*test results

were adequate.

No items of noncompliance were identified.

11.

Maintenance - Refueling

The inspector verified maintenance procedures include administrative

approvals; provisions for special authorization and fire watch respon-

sibilities for activities involving welding, open flame, *and other

6

ignition sources; reviews of material certifications; provisions for

assuring LCO requirements were met during repair; and responsibilities

for reporting defects to management.

The inspector observed the maintenance activities listed below and

verified work was accomplished in accordance with approved procedures

and by qualified personnel.

Unit 3

Core spray spargers inspection

Fuel sipping

Fuel channeling

Calibration of water level indicators in the Control Room for feedwater

sparger removal.

Steam separator removal

No items of noncompliance were identified.

12.

Inspection During Long Term Shutdown

The inspector observed control room operations, reviewed applicable

logs and conducted discussions with control room operators during the

period of December 31, 1981 through January 29, 1982.

The inspector

verified surveillance tests required during the shutdown were accom-

plished, reviewed tagout records, and verified applicability of

containment integrety.

Tours of Units 1 and 3 accessible areas,

including exterior areas were made to make independent assessments

of equipment conditions, plant conditions, radiological controls,

safety, and adherence to regulatory requirements and to verify that

maintenance requests had been initiated for equipment in need of

maintenance.

The inspector observed plant housekeeping/cleanliness

conditions, including potential fire hazards, and verified

implementation of radiation protection controls.

The inspector by

observation and direct interview verified that the physical security

plan was being implemented in accordance with the station security

plan.

No items *of noncompliance were identified.

13.

Regional Requests

The resident inspector prepared and forwarded a Significant Occurence

Report to Region III on the simultaneous inoperability of the High

Pressure Coolant Injection system and one of the Electromatic Automatic

Depressurization System valves.

This event occurred on December 23,

1981, and was documented in a previous inspection report (50-237/81-37

and 50-249/81-29).

The resident inspector followed up on a Region III request to conduct a

special inspection on the licensee's Prompt Public Notification/Warning

System.

The inspectors personally sited over 20% of the installed sirens.

The inspectors also contacted CECo corporate personnel regarding the

7

--

capability and availability of this system.

The results of the inspec-

tion were forwarded. to Region III and will be issued in a special report

by the Division of Emergency Preparedness or Operational Support.

During the inspection period, the Senior Resident Inspector and a

Region III inspector conducted the Dresden portion of a lengthy

investigation following up on allegations.

The allegations pertained

to operator training on Vice Presidents Instruction 1-0-17, offsite

review of DVRs, scrams of unknown cause or numerous scrams from

similar causes and approvals for restart; and LER corrective actions,

steps to prevent recurrence and trending.

Since the allegations were

related to all CECo plants, a similar review was conducted at Quad Cities

and Zion Stations.

A final summary report will be forthcoming with

the findings.

Region III requested followup by the resident inspectors to review

fire doors installed at Dresden.

This came about as a result of a

recent situation where certification was unavailable for fire doors

at the Kewaunee Nuclear Station.

CECo personnel stated that fire

protection doors at Dresden were manufactured by the James Walker

Company, a subsidiary of Allied Fire Equipment Company of Chicago,

which is not the manufacturer of the doors at Kewaunee, and that

certification is available upon request.

14.

Licensee Identified Items

The licensee reported finding a discrepancy in the timeliness of the

installation of the Unit 2 Drywell continuous pressure recorder to

meet TM! Task Action plan T.A.P. II-F-1.4.

The pressure recorder was

scheduled to be installed by January 1, 1982.

However, it was combined

in a modification package with the torus wide range level recorder

whpse delayed installation was reported to NRR by CECo letter dated

December 15, 1981, to be completed by February 1, 1982.

Immediately

upon discovery of the discrepancy, the licensee took steps to complete

the installation and report the item to the NRC.

The licensee reported identifying that the submission of the updated

curvers (Technical Specification Figure 3.6.1) had not been submitted

to the NRC prior to six effective full power years as required by

Technical Specification 3.6.B.1.

(The licensee did conduct a study

with a consultant in 1979, and concluded that the curvers should remain

the same for the next 10 to 16 years.)

The apparent cause was delay in

offsite review.

Upon discovery, the licensee immediately submitted the

updated information (TS Figure 3.c.1) to NRR.

The inspector was also

informed by* CECo offsite review personnel that they were taking steps

to prioritize and track items submitted for offsite review to prevent

future occurence.

This matter is similar to one of the allegations

reviewed and addressed in P~ragraph 13 of this report.

Final resolution

will be reviewed by the Region III team conducting the investigation of

the allegations.

8

These are licensee identified items of noncompliance.

In accordance

with the Interim Enforcement Policy, 45 FR 66754 (October 7, 1980),

Section IV.A, a Notice of Violation will not be issued for these

licensee identified items of noncompliance which are of Severity

Level V or VI.

Corporate corrective action followup is being conducted

by Region III personnel and conclusions will be presented in a separate

report.

No other items of noncompliance were identified.

15.

Bulletin Review

Based on the licensee's 180 day response dated November 30, 1981, to

IE Bulletin No. 80-11, the inspector reviewed many of the walls not

meeting the licensee's acceptance criteria.

The licensee failed to

determine if the failure of the walls not meeting the acceptance

criteria joepardized the operability of any safety related system.

The licensee is conducting a review to determine if the failure during

a seismic event of these walls not meeting the acceptance criteria

would affect the operability of systems or components.

Based on a

telecon between Region III DRPR personnel and CECo licensing per-

sonnel, the results of that review will be submitted to Region III

within one month.

This bulletin remains open.

No items of noncompliance were identified.

16.

Exit Interview

The inspectors met with licensee representatives (denoted in Paragraph 1)

throughout the month and at the conclusion of the inspection on January 22

and 29, 1982, and summarized the scope and findings of the inspection

activities.

The licensee acknowledged the findings of the inspection.

9