ML17180B154

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Enforcement Conference Repts 50-237/95-07 & 50-249/95-07 on 950309.Major Areas Discussed:Violations Identified During Special Safety Insp,Along W/Corrective Actions Taken or Planned by Licensee
ML17180B154
Person / Time
Site: Dresden  
Issue date: 03/14/1995
From: Hiland P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17180B153 List:
References
50-237-95-07-EC, 50-237-95-7-EC, 50-249-95-07, 50-249-95-7, EA-95-030, EA-95-30, NUDOCS 9504070190
Download: ML17180B154 (25)


See also: IR 05000237/1995007

Text

.

.

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Report No. 50-237/249-95007{DRP)

Docket Nos. 50-237; 50-249

Licensee:

Commonwealth Edison Company

Opus West I II

1400 Opus*Place

Downers Grove, IL 60515

License Nos. DPR-19; DPR-25

Facility Name:

Dresden Nuclear Power Station, Units 2 and 3

Meeting Conducted:

March 9, 1995

Meeting Location:

NRC Region III Office

801 Warrenville Road

Lisle, Illinois

Type of Meeting:

Enforcement Conference

Inspection Conducted:

Dresden Site

Morris, Illinois

January 25 to February 10, 1995

Inspectors:

C. J. Phillips.

Approved By:

A. M. Stone

~2//Lf

Patrick L. Hiland, Chief

Reactor Projects Section lB

Meeting Summary

Enforcement Conference on March 9, 1995 {Report No. 50-237/249-95007(DRP))

Areas Discussed:

Three apparent violations identified during a special safety

inspection were discussed, along with the corrective actions taken or planned

by the licensee.

The enforcement options pertaining to the apparent

violations were also discussed with the licensee. The apparent violations

concerned: (1) improper control of primary containment integrity, (2)

recirculation pump restart in violation of technical specification

requirements, and (3) inadequate instructions and/or failure to follow

procedures associated with the above evolutions .

9504070190 950315

PDR

ADOCK 05000237

G

PDR

DETAILS

1.

Persons Present at Conference

Commonwealth Edison Company

T Joyce, Site Vice President, Dresden

E. Eenigenburg, Unit 3 Station Manager, Dresden

J. Kotowski, Unit 2 Operations Manager

G. Tietz, Unit 3 Operations Manager

W. Sheldon, Unit 2 Maintenance Superintendent

S. Barrett, Radiation Protection Manager

U. S. Nuclear Regulatory Commission

H. Miller, Deputy Regional Administrator, Region III

T. Martin, Deputy Director, Reactor Projects, Region III

B. Clayton, Acting Deputy Director, Reactor Projects, Region III

P. Hiland, Chief, Reactor Projects, Section 18, Region III

M. Jordan, Chief, Operator Licensing, Section 1, Region III

R. DeFayette, Director, Enforcement and Investigation Coordination

Staff, Region III

M. Leach, Senior Resident Inspector, Dresden, Region III

C. Phillips, Resident Inspector, Dresden, Region III

R. Capra, Director, Project Directorate III-2, NRR

J. Stang, Project Manager, Project Directorate III-2, NRR

M. Satorius, Enforcement Specialist, OE

2.

Enforcement Conference

An Enforcement Conference was held in the Region III office on March 9,

1995.

The conference was conducted to address three apparent

violations:

(1) improper control of primary containment integrity,

(2) recirculation pump restart in violation of technical specification

requirements, and (3) inadequate instructions and/or failure to follow

procedures associated with the above evolutions.

The inspection

findings were documented in Inspection Report 50-237/249-95004(DRP)

which was transmitted to the licensee by letter dated February 17, 1995.

The purpose of the conference was to: (1) discuss the apparent

violations, causes, and the licensee's corrective actions; (2) determine

if there were any escalating or mitigating factors; (3) obtain

information which would help determine the appropriate enforcement

action; and (4) provide any additional information developed subsequent

to the inspection noted above.

Regional representatives presented a brief description of the pertinent

facts that led to the apparent violations, the regulatory requirements,

and potential safety significance of the event.

Licensee

representatives provided a description of the sequence of events, the

apparent violations, the safety significance, root cause analysis, and

corrective actions .

2

At the conclusion of the conference, the licensee representatives were

informed that they *would be notified in the near future of final

enforcement actions.

Attachments:

1.

NRC Presentation

2.

ComEd Presentation

3

.-*

. .. . :. '

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c.*

U.S. NUCLEAR REGULATORY

COMMISSION

REGION III

ENFORCEMENT CONFERENCE

COMMONWEALTH EDISON

DRESDEN STATION *

  • MARCH 9, 1995

10:00 .A.M. (CST)

REPORT NUMBER 50~237 /249-95004

. *EA NUMBER 95~030

NRCREGIONID

801 WARRENVILLE ROAD

LISLE, ILLINOIS

+..i:@ U!S i _Q.UZQ(i_

& J t . ! UWA&i&lt ii

ME

-*

DRESDEN STATION

ENFORCEMENT CONFERENCE AGENDA

MARCH 9, 1995

INTRODUCTION AND MEETING PURPOSE -

H. Clayton, Acting Deputy Director, DRP

. ENFORCEMENT PROCESS

R. DeFayette, Director EICS

APPARENT VIOLATIONS SUMMARY

M. Leach, Senior Resident Inspector

LICENSEE PRESENTATION AND DISCUSSION

. CLOSING REMARKS

H. Miller, Deputy Regional Administrator

. * ....

' ** .. **

\\: ...

' .

I '. .

I

.

i

. *

.

~ .. :,

" ..


THREE APPARENT VIOLATIONS

1. T.S. 3m 7 .A.2,

Primary Containment Integrity

-

  • January

6

primary

co*nt.aiiFHmierart::

boundaries were broken iin err-arr* fair

testing

Required LLRT was not performed .

Identified *through site engineering

.

review

February 3 LLRT result could not b*e

quantified

I*.

I

  • .
  • .-

'*

. -*~ :* .. , ...

..

2. T.S. 3/4.6.H.5,

. . :

~

Recirculation Pump Restart Limitations

28 recirculation pump tripped due to

maintenance error

Temperature differential between

reactor vessel stea*m space coolant

and* the bottom head drain coolant

was great~r than 145 ° F

. Operator workarounds - The bottom

heaq drain was plugged for years

.Engineering and management were

not consulted

Non-conservative decision making

by operating crew

. .. :*. '.

.*

.

.--~------ .*............

.

aas

3. 1 OCFR 50, Appendix B, Criterion V,

Instructions, Procedures and Drawings

  • Instructions

not*

ade*quate

for

locating .and. removing access plate

outside the primary containment

boundary

Procedure inadequate and/or lack of

adherence to isolate seal purge flow

to the idle recirculatio.n loop *

Recirculation

pymp. restart

procedure.* did

~,not .. match

the

.,_

requirement of *pl~'nt r.s .

,*:

.

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.

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tXSSUSM&J&Q_

_ t4UZM.a;awmws:.a. a a z

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  • -

DRESDEN UNITS 2 & 3

INSPECTION REPORT 50-237/249-95004

ENFORCEMENT BOARD

FEBRUARY 16, 1995

ITEM 1 - CONTAINMENT BREECH

ITEM 2 - RECIRC PUMP START

1.

ITEM 1 -

CONTAINMENT INTEGRITY BREECH*

Facility:

Unit(s):

Docket No(s):

License No(s):

Insp. Dates:

Lead Inspector:

ESCALATED ENFORCEMENT

BOARD PACKAGE

DRESDEN

Unit 3

50-249

DPR 25

February 6 - 10, 1995

Charles Philli:gs

BRIEF SUMMARY OF EVENT(S)

January . 6,

1995, an operator performed Dresden Operating

surveillance (DOS) 1600-13 on Unit 3. The surveillance was an

operational verification of a

check valve in the reactor

building to torus vacuum breaker. line.

  • *

The surveillance was performed incorrectly.

The operator

opened an access plate to the check valve hinge pin and broke

the pr1mary containment boundary.

The correct method was to

open

a

different access plate outside the

containment

boundary.

The valve was returned to service without a type B

LLRT.

Engineering had been performing this surveillance for the last

two years.

When it was reviewed by the IST coordinator, on

February 3, 1995, Operations was questioned as to how the

surveillance was performed.

When it was determined. on Feb. 3 ,fi' *that the procedure was

performed incorrectly a LLRT was performed on both the 31A and

31B valves.

Both valves failed with indeterminately high

leakage rates~ Sixty percent of La is 488 SCFH.

l ):. fvJI fr-./._ .,() 'f'GScrl!

There was an air operated valve upstream of both these valves.

  • The leakage past the AOV was about 2-5 SCFH.

However, this

valve fails open on a loss of instrument air.

Instrument air

at Dresden would be lost within minutes of a loss of offsite

power .

2

DRESDEN CONTAINMENT BREECH

Discussion:

The licensee failed to implement corrective actions to prevent

recurrence of a

problem that resulted in exceeding the

technical specification limits for type

B

& C primary

containment leakage.

On January 6, 1995, operations performed Dresden Operating

Surveillance (DOS) 1600-13, "Suppressi_on Chamber to.Reactor

building Vacuum Breaker Full Stroke Exercise Test" on both 3-

1601-3 lA & B valves.

The operator improperly performed the

surveillance. The operator was required to open an inspection

hatch upstream of the check valve and check it's operation

with a broom handle.

Instead, *the operator performed the

surveillance the way it used to be performed which was to

remove an .access plate for the check valve hinge pin and use

a socket tool to open the valve.

The access plate he opened

was part of the primary containment boundary.

When the

operator reinstalled the.plate, a type B local leak rate test

(LLRT) was not perfor.med on either 31A or 31B.

This was discovered on February 3, 1995, by site engineering.

Engineering had performed this test for Operations for about

two years.

Engineering was aware that the test was due but

had

not

been

contacted.

Engin~ering asked

about the

performance of the test and was told when and how it was

performed.

Engineering performed LLRTs on February 3 whicn

failed.

The

leak rates at both of the flanges were

indeterminately high.

This problem was identified by the licensee in the past.

The

resident inspectors became aware of the problem through a

review of corrective actions in an LER.

The licensee was

previously cited in Inspection Report 94014 for the failure to

conduct Type-B LLRTs.

The past violation required no response

because the licensee had already changed the surveillance

procedure so as not to operate the valve by removing the

access plate that was part of the primary containment

boundary.

History:

Unit, 3

had technically "inoperable" primary containment

isolation boundaries for the majority of the time between 1987

and 1994.

The Unit 3 reactor building to torus

valves (3-1601-31A&B) have flanges that

pins.

These

flanges

are

primary

penetrations.

3

vacuum breaker check

cover the valves hinge

containment

boundary

DRESDEN CONTAINMENT BREECH

2.

From

1987 to 1992,

a

surveillance verified the vaives

operability by removing the flange and cycling the valve

quarterly. The flanges were then reinstalled. However, local

leak rate tests were not performed to check the penetrations

as required by 10 CFR 50, Appendix J.

A 1987, on-site review

determined that the flanges were not part of the primary

containment and the surveillance procedure was changed to

remove the_ requirement to perform a LLRT.

A 1989, LLRT of the

3-1601-JlB valve was 159 SCFH.

An investigation revealed that

the 1987 on-site review decision was incorrect.

A corrective

action from that investigation was to evaluate using a

downstream access port to cycle the valve.

The surveillance procedure was not changed to use the

downstream access port until October 1992 and, no change was

made to the existing procedure to perf arm LLRTs after the

flange was removed and replaced.

However, even after the

procedure was changed, no effort was made to LLRT the flanges

until the as-found tests were performed for 3DR13 in March

1994.

The as-found for the March 1994, LLRT on 3-1601-31B was

257 SCFH.

This in combination with other type B and C leakage

exceeded the technical specification limit of 488 SCFH (0.6

La) .

[x]

A Notice of Violation (without "boilerplate"), including

recommended severity levels, is attached.

[ x J

Thi.s

NOV has been reviewed by the Branch Chief or

Di vision Director and each violation includes appropriate

specificity including how and when the requirement was

violated.

3.

[x]

Copies of the appropriate technical specifications or

license conditions are attached.

4.

Identify the enforcement policy supplement(s) that best fits

the violation(s):

Supplement 1.C.1. (b)

&

Supplement 1.C.2. (a)

ITEM 1 & ITEM 2 =Supplement 1.C.7

4

DRESDEN CONTAINMENT BREECH

5.

What is the apparent root cause of the problem?

(NOTE:

If

the root cause is programmatic maintenance deficiencies,

escalation of any civil penalty will be considered.)

Poor corrective actions requiring procedural changes.

6.

What actions have been taken by the licensee to correct the

specific violation(s)?

When the problem was found, the licensee entered Technical

Specification 3.0.A, which required the unit to be in hot shut

down in 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

When the flanges failed, the unit began a

shutdown.

When the flanges were repaired and LLRT's were

passed, the shutdown ceased.

7.

Briefly state the message that should be given to the licensee

through this enforcement action.

corrective actions at the station are poor.

between departments are poor *

5

communications

    • -

DRESDEN CONTAINMENT BREECH

8.

Factual information related to civil penalty ESCALATION or

MITIGATION factors:

a.

IDENTIFICATION AND REPORTING:

Violations were identified by licensee; an SEC engineer

identified the problem during an engineering review of

the surveillance.

Reported? Yes

(If so, LER #)

ENS Call

Report required?

Yes*

b.

CORRECTIVE ACTION TO PREVENT RECURRENCE;

UNKNOWN

c.

PAST PERFORMANCE:

(For

two

years or covering last two

inspections,

whichever is greater.)

Violation 50-249/94014-0S(DRP)

10 CFR so, Appendix J,Section III, D.2.

Pertinent SALP category and rating for last two SALP

periods.

Operations 3,3

Engineering 3,3.

d.

PRIOR NOTICE OF SIMILAR EVENTS:

Did the licensee have prior knowledge of this problem as

result

of

review

of

specific

NRC

or

industry

notification,

and fail to take effective preventive

steps?

Yes

Between 1987 and 1994 the lisensee was unable to

take effective corrective action.

6

DRESDEN CONTAINMENT BREECH

e.

MULTIPLE OCCURRENCES:

Were

multiple

examples

of

a

particular violation

identified during this inspection?

Yes

If yes, identify the violation and number of examples:

Both the 31A and 31B valves were found outside

limits.

f.

DURATION:

g.

How long did the violation(s) exist? 28 days

When did the licensee become aware of the violation(s)?

February 3, 1995

  • Should the licensee * have been aware of the problem

earlier?

No

SAFETY SIGNIFICANCE:

The upstream containment isolation valves are designed to

fail open on a loss of instrument air.

On a loss of

offsite power the instrument air system would have

depressurized in minutes.

In an accident scenario with

a loss of offsite power primary containment integrity

(0.6 La) would have been lost.

7

,*~SUE 1 - TECH. SPE *. 3.7 .A.2.b.(2}(a)

  • 3. 7 LIMITING CONDITION FOR OPERATION

(Cont 1d.)

(1) An overall

integrated

leakage rate

for Type A

tests of:

(a) L

less

tR~n or

equal t.o 75

percent of

La.

(b) Lt less

tri~n or

equal to 75

percent of

L .

(2) (a) A combined

leakage rate

of less than

or equal to

60 percent

of L for*

a 1i ~es table

and isola-

tion valves

subject to.

Type B and

C tests ex-

cept for

main steam

isolation

valves.

3/4.7-6

DRESDEN II

OPR-19

Amendment No. 122

4.7 SURVEILLANCE REQUIREMENTS

(Cont 1d.)

.*

DRESDEN CONTAINMENT BREECH

ITEM 1 NOTICE OF VIOLATION

1.

Technical Specification 3.7.A.2.b.(2). (a) states in part that

when primary containment integrity is required,

primary

containment leakage rates shall be limited to .*. a combined

leakage rate of less .than or equal to 60 percent of La for all

.u,1"'~testable penetrations and isolations valves subject to Type B

n

and c tests.

  • ,J ,_

t"

....

.

,. ,..((.,1-r'°r

,.!"*contrary to the above on January 6, . 1995,

the primary

V".

1

~ ti/' containment boundaries on valves 3-1601-31A & B were broken,

ile~ ~*

0

and when tes~ed on F~bruary 3,, 1995, the leakage rates were

r ~*

found to be indeterminately high.

These results exceeded 60

f *

percent of La for Type B and C leakage* on Unit 3.

2.

3 *.

10 CFR 50, Appendix B, criterion XVI, states in part that

measures shall be established to assure that conditions

adverse to quality are promptly identified and corrected. In

the case of signi'ficant conditions adverse to quality, the

measures shall assure that the cause of the condition is

. determined and corrective action taken to preclude repetition.

Contrary to the above, on January 6, 1995, a flange that was

part of the primary containment boundary was removed and

reinstalled on valves 3.-1601-31 A & B but no Type B local leak

rate test was performed.

On August 24, 1994, the licensee was

issued violation 50-249/94014-05 for failing to perforni. Type

B local leak rate tests on the same containment boundary

flanges.

Dresden Operating Surveillance (DOS). 1600-13, "Suppression

Chamber to Reactor building Vacuum Breaker Full Stroke

Exercise Test," ~evision 7, required that the 3-1601-31A & B

valves be checked by removing an access plate outside the

primary containment boundary and cycling the valve with an

extension tool.

Contrary to the above,

on January 6, 1995,

DOS 1600-13,

Revision 7, was inadequate in that the operator followed the

procedure as written and tested the 3-1601-31A&B valves by

opening an access plate that was part of the primary

containment boundary.

8

ITEM 2

~ RECIRC PUMP START

Facility:

ESCALATED ENFORCEMENT

BOARD QUESTIONNAIRE *

Dresden

Unit(s):

Unit 2

Docket No(s):

50-237

License No(s):

DPR-19

Insp. Dates:

Jan. 23 - Feb. 10, 1995

Lead Inspector:

Charles Phillips

BRIEF SUMMARY OF EVENT(S)

2B recirculation pump tripped because instrument maintenance

technicians

worked

on

the

wrong

motor

generator

set

temperature control valve.

Operations realized that the procedural requirement to have

less than a 145 degree temperature differential between the

bottom head thermal couple and the reactor steam space prior

to pump restart could not be met.

Operations

realized

that

the

technical

specification

requirement to have less than a. 145 degree temperature

differential between the bottom head drain line coolant and

the steam space could not be met.

Pump restart procedure temperature requirements differed from

the technical specificat~on requirements.

Shift personnel decided that using different temperature

indications met the intent of the technical specifications.

A site quality verification inspector was present in the

control room and questioned the operators as to whether their

course of action was in compliance with the procedure prior to

the pump restart.

Seal purge flow to the 2B recirculation pump was never

secured.

The pump trip procedure required isolating seal

purge flow if the pump was not restarted within an hour.

The pump was restarted 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 22 minutes after the trip

using temperature indications that were not listed in either

the procedure or the technical specification.

Operations

1

RECIRC PUMP START

management, station management, and engineering advice and

consent were not sought or obtained prior to the pump start.

In the last 12 months the NRC has identified 19 examples of

the licensee failing to follow procedure and two examples of

inadequate procedures.

Eight of these examples were within

the operations department and five of those examples were by

licensed operators. The NOV's are att.ached at the end of this

package.

Discussion:

On

January

10,

1995,

instrument maintenance

was

performin9

troubleshooting on the 2A recirculation pump motor generator set

temperature control valve (TCV) controller.

The technicians went

to the wrong controller. The technicians closed the TCV for the 2B

recirculation pump motor generator.

The motor generator (MG)

tripped on high temperature resulting in the loss of the 2B

recirculation pump.

The cause of the recirculation pump trip was quickly identified as

the maintenance error on the TCV.

The operators were preparing to

start the 2B recirculation pump when it was discovered that the

pump start procedure could not be met. Dresden Operating Procedure

(DOP)

0202-01,

"Unit 2 Reactor Recir,-culation System startup, II

Revision 14, stated that prior to sta~ting a second pump verify the

following temperature limitations, "If reactor pressure is greater

than or equal to 25 psig,

then reactor vessel bottom head

thermocouple temperature is within 145 degrees of the steam space

temperature."

Technical specification 3.6.H.5 states, "An idle

rec.:j.rculation pump . shall not be started * unless the temperature

differential between the reactor vessel steam space coolant and the

bottom head drain line is less than or equal to 145 degrees."

The

temperature differences between the bottom head drain line and

steam space, and the bottom head and the steam space were both

greater than 145 degrees.

However, the temperature differences

were greater than 145 degrees while the pumps were still operating.

Thus the restart of the pump was technically not possible via the

technical specifications or.the procedure.

The shift determined that alternate temperature indications could

be used to meet the technical specification and procedural intent.

A site quality verification inspector present in the control room

pointed out the procedural problem to the operating crew prior to

the pump start.

The operators interviewed all stated that the

problem had been discussed and the course of action agreed upon.

However, there appeared to be a difference between what the reactor

operator understood and what the unit supervisor understood.

The

unit operators log stated that the temperature difference between

the bottom head and the active recirculation loop discharge

2

RECIRC PUMP START

temperature was used and was less that 145 degrees.

The shift

managers log stated that the temperature difference between the

running recirculation pump discharge and the steam space was used.

The

shift managers

log

also

stated that this

temperature

differential met the intent of the technical specification. *

The shift did not isolate seal purge flow to the 2B recirculation

pump.

The pump trip procedure stated that * if the pump was not

planned to be restarted within an hour than isolate the seal purge

flow.

The purpose for isolating seal purge flow was that the loop

cooled down at about 22 degrees per hour with seal purge flow on

and also may not be seen by the operator because the loop has spots

below the thermocouple.

In fact, the idle loop recirculation

discharge temperature did take an eight degree step change downward

when the pump was started.

However, the loop to loop differential

temperature was still within technical specification requirements.

The

licensee

has

demonstrated

significant

problems

in the

preparation and adherence to procedures.

Technical Specification

Amendment

127

which

introduced

the

requirement

to

verify

differential temperatures from the drain line coolant to the steam

space became effective on July 17, 1994.

The procedure revision

that was

intended to

implement the technical specification

requirements did not agree with the technical *specifications and

were not made until November 3, 1994.

In addition, there was no

documentation that the operations department was ever trained on

the procedure change.

Over the past 12 months the NRC_identified

19

examples

of failing to

follow

procedure

and

inadequate

procedures.

2.

[x)

A Notice of Violation (without "boilerplate"), including

recommended severity levels, is attached.

[ x)

This NOV has been reviewed by the Branch Chief or

Di vision Director and each violation includes appropriate

specificity including how and when the requirement was

violated.

3.

[x]

Copies of the appropriate. technical specifications or

license conditions are attached.

4.

Identify the enforcement policy supplement(s) that best fits

the violation(s):

Supplement I.C.7

3

RECIRC PUMP START

5.

What.is the apparent root cause of the problem?

operators have a

long standing belief that technical and

procedural problems can be worked aro2und.

station has an ineffective training program.

6.

What actions have been taken by the licensee to correct the

specific violation(s)?

Operations manager talked to the unit supervisor and the

.shift manager about procedural adherence the week of

January 10.

Operations

procedural

discussions.

managers

began

talking

to

adherence

during

weekly

crews

about

operations

The shift operations supervisor held a meeting with the

shift managers

on January 25

on human performance

problems and used the 2B MG set problem as an example.

Shift operations supervisor sent a message via electronic

mail to all shift managers that discussed the technical

specifications as a matter of law. It was re-emphasized

that 100 percent procedure adherence is expected.

The Vice President of BWRs held a lengthy discussion with

upper station management that detailed his disappointment

with the way the event was reviewed.

station management designated a full root cause analysis

team on January 28.

All-station meetings were conducted on February 8 by the

station managers concerning the importance of procedural

adherence.

SEE LER 50-237-95003-00

7.

Briefly state the message that should be given to the licensee

through this enforcement action.

Procedural and technical specification adherence is required

for safe operation of the plant.

4

...

RECIRC PUMP START

8.

Factual information related to civil penalty ESCALATION or

MITIGATION factors:

a.

IDENTIFICATION AND REPORTING:

Violation (s) identified by licensee or NRC? Licensee/NRC

The licensee identified after the fact that the procedure

and technical specifications were not met.

Reported? Yes

(If so, LER #) 50-249-95003-00

Report required? Yes

b.

CORRECTIVE ACTION TO PREVENT RECURRENCE;

SEE LER

c.

PAST PERFORMANCE:

Numerous

NOVs

issued last 12 months for procedural

adherence problems.

See HANDOUT.

Identify pertinent SALP category and rating for last two

SALP periods.

Operations 3,3

d.

PRIOR NOTICE OF SIMILAR EVENTS:

Did the licensee have prior knowledge of this problem as

result

of

review

of

specific

NRC

or

industry

notification, and fail to take effective preventive

steps?

If yes, describe:

e.

MULTIPLE OCCURRENCES:

f.

DURATION:

g.

SAFETY SIGNIFICANCE:

5

ISSUE 2 - TECH. SPE *. 3.6.H.5

LIMITING CONDITION FOR OPERATION

(Cont'd.)

g.

The MAPLHGR Operating

Limit shall be reduced

by the appropriate

multiplicative factor

from the Core Operating

Limits Report

(Specification 3.5.I).

!ff. concurrently, one

Au omatic Pressure

Relief Subsystem relief

valve is out-of-service,

the MAPLHGR Operating

Limit shall be reduced

by the appropriate

multiplicative factor

from the Core Operating

Limits Report.

4.

With no reactor coolant system

recirculation loops in

operation~ reduce core thermal

power to 1ess than 25% of rated

within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and place the

unit in hot shutdown within the

following 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

5.

Idle Recirculation Loop Startup

An idle recirculation pump shall

not be started unless the

temperature differential between

the reactor vessel steam space

coolant and the bottom heaa

drain line coolant is less than

a.

equal to 145°F*, .and:

When both pumps have been

idle, unless the temperature

differential between the

reactor coolant within the

idle loop to be started up

and the coolant in the

reactor pressure vessel is

less than or equal to S0°F,

or

b.

When only one loop has been

idle, unless the temperature

differential between the

reactor coolant within the

idle and operating

recirculation loops is less

than or equal to 50°F and

the speed of the operating

pump is less than or equal

to 43% of rated pump speed.

I. Snubbers (Shock Suppressors}

DRESDEN.

DPR-19

Amendment No .. 127

4.6

SURVEILLANCE REQUIREMENT

(Cont'd.)

5.

Idle Recirculation Loop Startup

The temperature differentials and flow

rates shall be determined to be within

the limits within 15 minutes prior to

startup of an idle recirculation loop.

I. Snubbers (Shock Suppressors)

The following surveillance

requirements apply to safety related

snubbers.

3/4.6-16

RECIRC PUMP START

1.

ISSUE 2 -

NOTICE OF VIOLATION

,:,*I).!' Je* //"'"'"'-'- ~n1 }-

Technical Specification ~

states in part that the

temperature differential eween the reactor vessel steam

space and the bottom head drain line coolant must be verified

to be less than 145 degrees within 15 minutes prior to

starting a recirculation pump in an idle loop.

Contrary to the

above,

on

January

10,

1995,

the

2B

recirculation pump was started in an idle loop when the bottom

head coolant drain line temperature was not within 145 degrees

of the reactor vessel steam space temperature.

2.

Technical Specification 6. 2 .A.1 states in part that written *

procedures shall be established, implemented and maintained

covering applicable procedures recommended in Appendix A of

Regulatory Guide 1.33, Revision 2, February 1978.

Regulatory

Guide

1. 33,

Appendix A,

Section 4. a

recommends startup

procedures for the recirculating system.

a.

Technical Sp.ecif ication~f:1:~r ~~res in part that the

temperature differential between the reactor vessel steam

space and the bottom head drain iine cooiant [EMPHASIS

ADDED]

must be verified to be less than 145 degrees

within 15 minutes prior to starting a recirculation pump

in an idle loop.

Dresden Operating Procedure

(DOP)

0202-01,

"Unit

2

Reactor Recirculation System startup," Revision 14, step

G.10

states

in

part that

if starting

a

second

recirculation pump, then within 15 minutes of starting

the pump verify . that the bottom head thermocouple

temperature is within 145 degrees of the steam space

temperature.

Contrary to the above, when the 2B recirculation* pump was

started on January 10, 1995, the procedure did not meet

the requirements of the technical specification.

b.

Dresden Operating Abnormal (DOA) 0202-01, "Recirculation

Pump Trip -.One or Both Pumps," Revision 10, step D.12

~ 0

states, "If idle loop starts are not~ithin one

~

t d

,L/hour, then isolate seal purge flow to~le loop per

r

DOP 0202-11."

.

.

V"'

.

,L'} I

I

.

~JG

~

Contrary to the* above, on January 10, 1995, the 2B

recirculation pump tripped and was restarted 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and

22 minutes later without securing seal purge flow.

,VP~ IJ- I Y ,,Jr.,,...-

.

,

~*

6

'.*

ISSUE 1 & 2 NOTICE OF VIOLATION

Technical Specification 6.2.A.1 states in part that written

procedures shall

be established,

implemented

and maintained

covering applicable procedures

recommended in Appendix A of

Regulatory Guide 1. 33, Revision 2, February 1978. Regulatory Guide

1.33, Appendix A, Section 4.a recommends startup procedures for the

recirculating system.

a.

Technical Specification 4. 6. H. 5 states in part that the

temperature differential between the reactor vessel steam

space and the bottom head drain line coolant must be verified

to be less* than 145 degrees within 15 minutes prior to

starting a recirculation pump in an idle loop.

Dresden Operating Procedure (DOP)

0202-01, "Unit 2 Reactor

Recirculation system startup," Revision 14, step G.10 states

in .part that if starting a second recirculation pump then

within 15 minutes of starting the pump verify that the bottom

head thermocouple temperature is within 145 degrees of the

steam space temperature.

Contrary to the above, when the 2B recirculation pump was

started on January 10, 1995, the procedure did not meet the

requirements of the technical specification.

b.

Dresden Operating Abnormal (DOA) 0202-01, "Recirculation Pump

Trip - One or Both Pumps," Revision 10, step D.12 states, "If

idle loop starts are not planned within one hour, then isolate

seal purge flow to the idle loop per DOP 0202-11. 11

Contrary to the

above,

on

January

10,

1995,

the

2B

recirculation pump tripped and was restarted 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 22

minutes later without securing seal purge flow.

c.

Dresden Operating Surveillance (DOS)

1600-13, "Suppression

Chamber to Reactor building Vacuum Breaker Full Stroke

Exercise Test," Revision 7, required that the 3-1601-31A & B

valve~ are checked by removing an access plate -0utside the

primary containment boundary and cycling the valve with an

e~tension tool.

Contrary to the above,

on January 6, 1995,

DOS 1600-13,

Revision 7, was inadequate in that the operator followed the

proc

rit~.§n, and tested the 3-1601-31A&B valves :Oy

opening an access !plate that was part of the primary

6ontainment boundary.

\\

1