05000416/LER-2016-007
11-7-2016 | On September 4, 2016 at 02:58, Grand Gulf Nuclear Station entered three TS LCO Action Statements because RHR 'A' pump was declared inoperable.
LCO Actions entered: 1) 3.5.1 for one low pressure ECCS injection/spray subsystem, 2) 3.6.1.7 for one RHR containment spray subsystem, and 3) 3.6.2.3 for one RHR suppression pool cooling subsystem. All have 7 day Completion Times A decision was made to shutdown the plant to repair the RHR 'A' pump because, based on the troubleshooting and testing plan, the pump could not be repaired and returned to service within the LCO Completion Times. At 0300 CDT on 09/08/16, GGNS initiated the transition to Mode 4. The pump was removed from service and sent to the vendor facility for decontamination, disassembly and failure analysis. The 'A' pump was then replaced and tested satisfactorily. RHR 'A' was returned to operable. APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Intocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may 366A U.S. NUCLEAR REGULATORY COMMISSION ContentsCONTINUATION SHEET2. DOCKET 3. LER NUMBER 05000 416 PLANT CONDITIONS PRIOR TO THE EVENTAt the time of the event, Grand Gulf Nuclear Station (GGNS) Unit 1 was in Mode 1, at 100% rated thermal power. All systems, structures and components, with the exception of the RHR 'A' pump, that were necessary to mitigate, reduce the consequences of, or limit the safety implications of the event were available. No other safety significant components were out of service. DESCRIPTIONOn September 4, 2016, GGNS was performing a Residual Heat Removal (RHR) 'A' quarterly Technical Specification (TS) Surveillance Requirement (SR). At 02:58, The RHR pump failed to meet its TS SR Acceptance Criteria for flow and differential pressure (d/p) and was therefore declared Inoperable. Action Statements for TS Limiting Conditions for Operation (LCOs) 3.5.1, 3.6.1.7 and 3.6.2.3 were entered, each having Completion Times of 7 days. LCO Action Statements entered: 1) 3.5.1 for one low pressure ECCS injection/spray subsystem, 2) 3.6.1.7 for one RHR containment spray subsystem, and 3) 3.6.2.3 for one RHR suppression pool cooling subsystem. Initial troubleshooting verified that the pump was incapable of meeting the flow requirement of 7756 gpm and d/p of 131 psid simultaneously. The observed pump flow and discharge pressures were verified to be correct via a temporarily installed ultrasonic flow meter and pressure gauge. RHR system valves and lines were verified not to be clogged or leaking. The pump motor was confirmed to be operating at the proper speed. Further troubleshooting and testing lead station management to the conclusion that RHR 'A' would not be returned to operable status within the 7 day Completion Time. A decision was made to commence an orderly shutdown. On September 8, 2016 at 0300, GGNS began the transition to Mode 4. No other systems were out of service that would have complicated an orderly shutdown to Mode 4. REPORTABILITYEvent Notification 52225 was made to the U.S. Nuclear Regulatory Commission (NRC) Operations Center. This LER is being submitted pursuant to Title 10 Code of Federal Regulations 10 CFR 50.73(a)(2)(i)(A) for the completion of any nuclear plant shutdown required by the plant's Technical Specifications. Telephonic notification was made to the NRC Emergency Notification System on September 8, 2016, at 03:27, pursuant to 10 CFR 50.72(b)(2)(i) for the initiation of any nuclear plant shutdown required by the plant's Technical Specifications. CAUSEDirect Cause: The RHR 'A' pump was unable to provide its required flow at the required differential pressure in order to perform its safety function. APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs. NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may NRC FORM366A U.S. NUCLEAR REGULATORY COMMISSION CONTINUATION SHEETGrand Gulf Nuclear Station, Unit 1 05000 416 Apparent Cause: Subsequent investigation suggests internal pump degradation but the Apparent Cause is ongoing. A supplemental report to this LER will be provided when the Apparent Cause investigation is complete. EXTENT OF CONDITIONQuarterly surveillance data of similar Emergency Core Cooling System (ECCS) pumps showed no evidence of degradation. Data was re-examined from the following pumps: Low Pressure Core Spray (LPCS), High Pressure Core Spray (HPCS) and RHR 'B' and 'C.' GGNS also performed a partial quarterly surveillance on the RHR 'B' which was completed satisfactorily. CORRECTIVE ACTIONSThe RHR 'A' pump was replaced and retested satisfactorily. The pump removed from service has been sent to the vendor facility for failure analysis. SAFETY SIGNIFICANCEThe event posed no threat to the health and safety of the general public or to nuclear safety as safety- systems performed as designed. No Technical Specification safety limits were violated. Industrial safety was not challenged, and there was no potential or actual radiological release during the event. PREVIOUS SIMILAR EVENTSPrevious similar events. will be discussed in the supplemental report upon completion of the Apparent Cause investigation. |
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Grand Gulf Nuclear Station, Unit 1 | |
Event date: | 9-8-2016 |
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Report date: | 11-7-2016 |
Reporting criterion: | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown |
4162016007R00 - NRC Website | |
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