ML17157C536

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Insp Repts 50-387/93-18 & 50-388/93-18 on 930927-1001.No Violations Noted.Major Areas Inspected:Licensee Records, Interviews W/Personnel
ML17157C536
Person / Time
Site: Susquehanna  
Issue date: 10/18/1993
From: Conte R, Sisco C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17157C535 List:
References
50-387-93-18, 50-388-93-18, NUDOCS 9311010113
Download: ML17157C536 (9)


See also: IR 05000387/1993018

Text

REPORT NOS:

LICENSE NOS:

LICENSEE:

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

50-387; 388/93-18

NPF-14, NPF-22

Pennsylvania Power &Light Company

2 North Ninth Street

Allentown, Pennsylvania

81801

FACILITY:

Susquehanna

Steam Electric Station

INSPECTION DATES:

September 27-October

1, 1993

INSPECTORS:

LEAD INSPECTOR:

C. Sisco, Operations Engineer

D. Mannai, Resident Inspector

C. Sisco, Operations Engineer

REVIEWED BY:

C. S', Operations Engineer

BWR Section, Operations Branch

Division of Reactor Safety

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Date

APPROVED BY:

Richard J. Conte,

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BWR Section, Operations Branch

Division of Reactor Safety

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Date

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93iiOiOii3 931022

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ADOCK OS000387

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In

ection Summa:

Inspection conducted from September 27-October

1, 1993 (Report

Nos. 50-387/93-18; 50-388/93-18)

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personnel,

and observations by the inspectors

was conducted.

Results:

The inspectors concluded control room operations are conducted in accordance with

station procedures.

In addition, operations management

was present in the control room

providing adequate

management

oversight.

Likewise, maintenance activities were performed

in accordance with station procedures

and with appropriate supervisory oversight.

I

The continuation of status control events with low safety consequences

indicated that the

licensee's corrective actions have been ineffective.

In addition, the repetitive nature of

mispositioned valves indicated that the licensee's root cause analysis of mispositioned

valve(s) may not have been sufficiently independent or thorough enough to include all

human performance aspects.

0

0

I

DETAILS

1.0

INTRODUCTIONAND SCOPE

The purpose of this inspection was to review licensee actions to control equipment status.

This initiative inspection was performed to evaluate the effectiveness of the licensee's root

cause evaluations and corrective action implementation for events status was not maintained.

These events, in some cases,

led to adverse consequences

such as primary containment

leakpaths; minor, uncontrolled releases;

and system trips or degradations.

Many of these

events were caused by valve.mispositionings.

The inspection consisted of a review of selective records, interviews with personnel,

and

observations of plant activities by the inspectors.

The inspectors used inspection procedures

71715 and 92720 during the course of this inspection.

2.0

FINDINGS

2.1

Observations of Plant Activities

The purpose of this review was to assure that safety-related activities were conducted in

accordance with approved station procedures

and that management

was involved in routine

activities including event reviews.

The inspectors observed licensee activities in,the control room during 100% power

operations of Unit 2, and shutdown activities of Unit 1.

The inspectors noted that activities

were conducted in a professional manner in accordance with station procedures,

and

management

oversight of control room activities were conducted on a routine basis.

The inspectors conducted observations of maintenance activities in the reactor building of

Unit 1.

The inspectors observed

the repacking of valves at the hydraulic control units and

work preparations

to remove the drywell equipment hatch.

The work activities were

conducted in accordance

with station procedures,

and these procedures

were located at the

work sites.

Maintenance supervision was observed in the work areas providing management

oversight.

2.2

Control of Valve Positions

The licensee has long identified the issue of maintaining the correct valve positions as a

problem in their facility. The inspectors reviewed several of the licensee's Nuclear Safety

Assessment

Group (NSAG) annual summary assessments

that identified valve position control

as a weakness.,

In 1992, the licensee formed a Status Control Review Team that issued a

report detailing the team's findings and corrective action recommendations.

The Status

Control Review Team Report was reviewed by the inspectors,

In addition, the inspectors

reviewed facility generated Significant Operating Occurrence Reports (SOORs).

Based on a

'v

review of these documents,

and past NRC Inspection Reports, the licensee's control of valve

positions continues to be less than effective.

Examples of this continuing problem are listed

below.

In July 1992 and during power operations at Unit 1, the licensee identified that five

containment atmosphere

sampling lines were disconnected

at the "B" containment

radiation monitoring (CRM) panel by the removal of five solenoid operated valves.

The valves were inadvertently removed during a maintenance activity (past unresolved

item No; 387,388/92-20-01).

The primary containment penetration isolation valve

was operable while these sample valves were removed from the system.

In April 1993, an NRC inspector identified that a High Pressure

Coolant Injectio'n

(HPCI) turbine exhaust vacuum breaker test valve was closed, capped and

containment tagged, but was not chain locked closed as required by facility procedure

on Unit 1. This event resulted in a Notice of Violation and is detailed in NRC

Inspection Report 50-387/93-07.

In June 1993 and during power operation at Unit 2, the licensee identified that a 3/8"

drain valve on the suppression

chamber narrow range pressure instrument line was

found open and the end uncapped.

This uncapped

and open drain valve allowed a

leak path between the primary and secondary containments.

The leakage amount was

within regulatory limits and was of minor safety significance.

In July 1993, the licensee identified that a drain valve at the Condensate

Storage Tank

berm of Unit 2 was mispositioned by being open.

This event resulted in a small

unmonitored and uncontrolled release (low level) of radioactivity from the berm area.

In August 1993, the licensee identified that a valve in the Containment Instrument Gas

(CIG) system was mispositioned.

This event caused

the CIG system to transfer

automatically to the gas bottle backup system.

The gas bottles provide an emergency

backup supply of nitrogen pressure for the Automatic Depressurization

System.

In September

1993, the licensee identified that the vent valves on the Main Generator

exciter heat exchanger were mispositioned by being closed on Unit 2.

In September

1993, the licensee identified that a valve in the Fuel Pool Cooling

(FPC) system was mispositioned by being open.

This event resulted in a low level in

the skimmer surge tank of the FPC system and the resultant trip of the FPC system

pumps.

The licensee took immediate corrective action(s) to restore the mispositioned valve(s) and

plant systems to the correct configuration once identified for each of these cases.

With

'

respect to long-term corrective actions, the licensee's NSAG group has long identified and

tracked equipment status control events.

The licensee's

1992 report identified status control

events as needing additional management

attention.

The licensee has implemented several additional corrective actions since mid-1993.

However, the inspectors noted that these corrective actions could have been implemented in a

more timely fashion since the licensee's

Status Control Review Team Report was issued in

September

1992.

Based on recent examples,

these actions have not prevented recurrence.

The individual examples of mispositioned valves by themselves

has low safety consequences.

However, the continuing nature of valve mispositioning events that have occurred indicated

that licensee's corrective actions have been ineffective in maintaining complete control of

valve positions.

In addition, the repetitive nature of mispositioned valves indicated that the

licensee's root cause analysis of mispositioned valve{s) may not have been sufficiently

independent or thorough enough to include all human performance aspects.

3.0

SUMMARY

The inspectors concluded control room operations are conducted in accordance with station

procedures.

In addition, operations management

was present in the control room providing

adequate

management

oversight.

Likewise maintenance activities were performed in

accordance with station procedures

and with appropriate supervisory oversight.

The continuation of status control events with low safety consequences

indicated that the

licensee's corrective actions have been ineffective. In addition, the repetitive nature of

mispositioned valves indicated that the licensee's root cause analysis of mispositioned

valve{s) may not have been sufficiently independent or thorough enough to include all human

performance aspects.

4.0

EXIT

MEETING'n

exit meeting was conducted October 1, 1993, at the Susquehanna

Steam Electric Station.

The inspector's findings and conclusions were discussed

at this meeting.

Those in attendance

are listed below.

At the meeting, the NRC staff focused on its concern with the ineffectiveness of the

licensee's corrective actions with respect to status configuration control on valve positions.

In response

to the staff's request,

the licensee representatives

agreed to a written response

detailing additional actions and controls to minimize further valve mispositioning events.

The area addressed

in this report is unresolved pending NRC staff review of the licensee's

response

as noted above (387,388/93-18-01).

(An unresolved item is an area in which more

information is needed to determine ifthe item is acceptable,

a violation, or a deviation.)

PENN YLVANIAPOWER Ec LIGHT

MPANY

G. Stanley

G. Kuczynski

B. Saccone

H. Palmer

T. Dalpiaz

K. Chambliss

R. Breslin

S. Laskos

D. McGann

A. Dominquez

F. Guscavage

M. Golden

J. Meter

T. Clymer

Vice-President Nuclear Operations

Manager-Plant Services

'anager-NSE

Manager-Operations

Manager-Maintenance

Supervisor-Maintenance

Chemistry Supervisor

Scheduling Supervisor

Supervisor-Compliance

Supervisor-NSAG

Supervisor-Operations

Engineering

Supervisor-NSE - PAT

Compliance

NQA-Audits

LEAR RE

LAT RY

MMI I N

L. Bettenhausen

C. Sisco

D. Mannai

Chief, Operations Branch, Division of Reactor Safety

Operations Engineer

Resident Inspector