ML17139C679
| ML17139C679 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna, 05003878 |
| Issue date: | 11/15/1984 |
| From: | Jacobs R, Plisco L, Strosnider J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17139C678 | List: |
| References | |
| 50-387-84-35, 50-388-84-44, NUDOCS 8411200194 | |
| Download: ML17139C679 (28) | |
See also: IR 05000387/1984035
Text
U.S.
NUCLEAR REGULATORY COMMISSION
REGION I
Report Nos.
50-387/84-35.
30-388/84-44
Docket Nos.
50-387
CAT
C
50-388
CAT B2
License
Nos.
NPF-22
Licensee:
Penns
lvania Power and Li ht
Com an
2 North Ninth Street
Al 1 entown
Penns
1 vani a
18101
Facility Name:
Sus
uehanna
Steam Electric Station
Inspection At: Salem
Townshi
Penns
lvania
Inspection
Conducted:
October
13
22
1984
Inspectors:
H. Jac
bs,
Senior Resident
Inspector
R. Plis o, Resident
Inspector
Approved by:
ack Strosnider,
Chief, Reactor
Projects
Section
1C,
DPRP
i/ rd/~~
date
/I//o-/d4
date
riys/~~
date
Ins ection Summar:
Ins ection conducted
on October
13 - 22
1984
Re ort No.
->>/
Areas
Ins ected:
A special
safety inspection
was performed
by the Resident
Inspectors
93 hours0.00108 days <br />0.0258 hours <br />1.537698e-4 weeks <br />3.53865e-5 months <br />) of the circumstances
involved with the failure of four
scram pilot solenoid valves during individual rod scram testing
on Unit
1 on
October 6,
1984.
The inspection consisted of a review and evaluation of: scram
pilot solenoid valve
(SPSV) function, licensee
actions following identification
of the
SPSV failures,
scram time surveillance testing,
SPSV maintenance
history
and Unit
1 scram discharge
volume vent and drain pilot valve inoperability.
8411200194
841115
ADOCK 05000387
~
~
4
Qi
DETAILS
1.0
Se uence of Events
10/06/84
Unit 1 at 60% power.
Individual rod scram testing performed
on
10% of rods
on Unit 1.
Two rods failed to
Testing
was
expanded to include all
185 rods.
Final results
were
4 rods
failed to scram
and
9 rods hesitated
before
scramming.
10/07
The four failures were determined to be caused
by the scram
pilot solenoid
valve
(SPSV).
These
four valves
were
replaced.
10/07
Licensee
formed a task force to investigate
SPSV failures.
One
valve was sent to
GE and one to Franklin Institute for analysis.
10/12
GE informed PPKL that the SPSV fai lures were due to the disc
holder subassembly
adhering to the valve seat.
The disc material
was
polyurethane.
recommended
that the polyurethane
be re-
placed with Viton-A.
10/12
Unit 1 commenced
a reactor
shutdown at 9: 10 p.m.
since all other
SPSVs
also
had polyurethane
discs.
Unit 2
commenced
a reactor
shutdown at 9:50
p.m.
Ninety-three of the
185 Unit 2 SPSVs
had
polyurethane
disc material.
ENS calls were properly made
on the
above.
10/13
Unit 1 in Hot Shutdown at 4:00 a.m., Unit 2 in Hot Shutdown at
5:12 a.m.
10/14-15
New disc holder subassemblies
with the Viton-A material were
installed in all
185
SPSVs
on Unit
1
~
10/16
Meeting in Bethesda with PP&L, GE, Region I and
NRR to discuss
SPSY problem.
10/17
Unit 1 reactor critical at 12:34 a.m.
Unit 2 reactor critical
at
9:45
p.m.
following replacement
(and/or
inspection)
of all
SPSV disc holder
subassemblies.
NRC issued
Confirmatory Action
Letter (CAL).
10/18
Unit 1 conducting individual rod scram testing of all rods.
The licensee
discovered
that the
18 month surveillance
interval
on the
scram discharge
volume
(SDV) vent
and drain valve timing
was past
due.
At 9:21 p.m.,
Unit
1
was manually
scrammed
from
55 percent
power to perform the surveillance.
The
SDV vent valve
closed in 32.4 seconds
exceeding
the Technical limit of 30 seconds.
10/19-20
The pilot solenoid valve for the Unit 1 SDV vent valve'was
replaced
with
a pilot solenoid
valve
manufactured
by Valcor.
Unit 2 conducting
rod testing.
0
a
d
1
10/21
Unit 1 returned to criticality at 3:52 a.m.
and was scrammed at
1:29
p.m.
to 'meet
the
SDV vent
and drain
valve
surveillance
requirement following the pilot valve replacement.
10/22
Unit returned to criticality at 12:35 a.m.
and increased
power
to continue
rod testing.
2.0
Descri tion of Scram Pilot Solenoid Valves
The
Scram Pilot Solenoid Valves
(SPSV) are
a three-way,
solenoid-operated,
normally energized
valve.
During normal
reactor
operations,
each of the
two channels
of the
Reactor
Protection
System
(RPS)
energizes
one of the
pilot valve solenoids.
When energized,
the pilot valve allows instrument
air to be supplied to the diaphragm actuators
of the inlet and outlet scram
valves,
holding these
valves shut.
Upon initiation of a scram,
both chan-
nels
of the
de-energize
and
both pilot valve solenoids
de-energize,
rapidly venting air pressure
from the
scram inlet and outlet valves,
and
allowing them to open to scram the control rod.
To prevent
inadvertent
of a single rod, both pilot valve solenoids
must
be de-energized
before air is vented
from the
scram valves.
De-ener-
gizing only
one of the
two solenoids will not result
in
a
because
the remaining coi 1 is sufficient to maintain
the valve in
a configuration
that allows air to continue to be supplied to the
scram valves through the
pilot valve.
There are
185 scram pilot solenoid
valves installed
on
each
unit (1 per control rod.)
For added reliability, the Control
Rod Drive (CRD) Instrument Air System
has
two
DC solenoid operated,
three-way air valves installed
on the supply
called
backup
scram valves.
The air supplied to the Hydraulic Con-
trol Units
(HCUs)
and
the
discharge
volume
vent
and
drain
valves
passes
through
these
two valves.
As
a
backup to the individual
SPSV and
scram discharge
volume vent and 'drain valves,
the
backup
valves
are
energized
by the
Reactor
Protection
System
(RPS)
on
a
and vent the
entire
CRD Instrument Air System.
Units
1
and
2 utilize an Automatic Switch
Company
(ASCO) three-way, dia-
phragm type,
redundant piloted solenoid valve
(ASCO Part
No. HV-176-816-1,
GE Part
No. 9220138) for the
SPSV.
The valves
are of brass
construction.
Figure
1
shows internal
components
of the valve.
When the valve is ener-
gized (both solenoids),
the inlet port from the external
air
supply (in-
strument air) is open to the
scram inlet and outlet valves,
and the exhaust
port is closed.
The disc holder
subassembly
contains
a polyurethane
disc
which covers
the valve exhaust
port
on the 'B'olenoid side.
When both
solenoids
de-energize,
the disc
holder
subassembly
moves
away
from the
exhaust port and the core assembly of the
A solenoid
closes
the air inlet
port, this action allows air to bleed off the
scram inlet and outlet valves
thus causing control rod insertion.
/
0
3.0
Licensee Actions
3.1
October
6
1984 Surveillance Test
and Followu
Actions
On
October
6,
1984,
the
licensee
commenced
quarterly individual rod
scram testing
on ten percent of the Unit 1 rods
as
required
by Tech-
nical Specification (T.S.)
4. 1.3.2.
At approximately
9:05 a.m.
con-
trol rod 42-23 failed to insert after 'the test
switches
were placed
in the test
position.
The test
was
repeated
three
times
and
each
time the rod failed to scram.
Instrument
and Controls (I&C) technicians
investigated
the problem
and
when they tapped
the solenoid valve the
rod
scrammed.
The
rod
was
then full withdrawn
and
retested.
The
retest
at
9:40
a.m.
was
satisfactory.
When
rod testing
continued,
rod 42-39 also initially failed to insert at
10:30
a.m.
and when
an
operator
tapped
the
solenoid
valve,
the
rod
inserted
as
designed,
The licensee
then
decided
to individually scram test all
185 Unit
1
rods.
Two additional
rods (i.e.
58-31
and
38-39) failed to
during this testing
and
9 other
rods hesitated initially when tested.
and 58-31 subsequently
scrammed
when operators
tapped their
solenoid
valves
and
then
passed
a retest
when
withdrawn
again.
Of
the rods that hesitated,
none exceeded
the required
maximum insertion
time of seven
seconds.
During the testing the appropriate
T.S. Limiting Condition for Opera-
tion
(LCO) was properly entered
when individual rods were determined
to be inoperable.
The
LCO',s were cleared following successful
retests.
On October 7, the
scram pilot solenoid valves
(SPSV) were replaced
on
the four rods which did not
The licensee
set
up
a task force
consisting of plant staff and Nuclear Plant Engineering
(NPE) engineers
to investigate
the
SPSV failures.
One of the replaced
SPSVs
was
sent
to GE,
San Jose,
California for analysis of the failure mechanism
and
another
was sent to Franklin Institute.
3.2
GE Anal sis Results
and Plant Shutdowns
On October
12,
1984,
GE informed PP5L that it was GE's judgement that
the
SPSV failed due to the disc holder
subassembly
disc sticking to
the seat
on the valve body.
The sticking was
due to
a degradation
of
the polyurethane
disc material.
GE,
as
a product upgrade
changed
the
disc material
to Viton-A.
The Viton-A material
was
subsequently
in-
corporated
into
ASCO spare
part kits for these
valves,
beginning
in
1982, although
an immediate
replacement for existing valves apparently
was not
deemed
necessary.
Viton-A was
an
environmentally qualified
material.
The polyurethane
disc
was designed
for temperatures
up to
220'.
However,
based
on
the
service
temperatures
of the
valves,
the
polyurethane
material
apparently
degrades
at
temperatures
near
160 F.
Licensee testing
found that the skin temperature
of the
SPSV
when energized
was approximately
140~
F.
Based
on this information
and the determination that most if not all
of the
SPSVs
on
both units
were affected,
the
licensee
decided
to
shutdown
both Units
1
and
2.
Unit
1 shutdown
was
commenced at about
9: 10 p.m.
on October
12 and the unit was in Hot Shutdown at 4:00 a.m.
October
13.
Unit
2
shutdown
was
commenced
at
about
9:50
p.m.
on
October
12
and
Hot
Shutdown
was
achieved
at
5: 17
a.m.
October
13.
Unit 2 subsequently
went to Cold Shutdown at about 5:00 p.m. to con-
duct unrelated
maintenance.
3.3
Com onent
Re lacement
ASCO spare part kits containing the Viton-A disc were obtained
by the
licensee
and
the disc
holder
subassemblies
were extracted
from the
spare part kits and installed in all
185
SPSVs
on Unit
1 during October
13 thru October
15.
These
valves were functionally tested
by observ-
ing the
scram inlet
and outlet valves
stroking
when the individual
rod test
switches
were actuated.
Additionally, individual rod testing
was
performed while shutdown.
The
backup
scram valves
and the
discharge
volume
(SDV) vent
and drain pilot valves
on Unit
1
were
also rebuilt with
new Viton-A discs.
Subsequently,
on
October
17,
Unit
1 returned
to
power
and individual rod testing
on all rods
was
conducted at approximately
50 percent
power.
On
Unit 2,
the
licensee
determined
that
93 of the
SPSVs
had
been
previously rebuilt in April 1983 using
ASCO spare part kits containing
the Viton-A disc.
The licensee installed the
new disc subassembly
in
the remaining
SPSVs
and also
inspected
the ones that were previously
rebuilt to
ensure
that
they
contained
the
Viton-A disc.
New disc
holder
subassemblies
were also installed in the backup
scram valves.
The Unit 2 scram discharge
volume vent
and drain pilot valves,
manu-
factured
by Valcor were not affected.
Inspector
review of these activities identified no unacceptable
con-
ditions.
4.0
NRC Res
onse
Re ion I and
Head uarters
NRC Headquarters
was notified, via
ENS call
on October
12, of the defective
SPSVs
and of the licensee's
decision to shutdown Units
1 and 2.
On October
15, at the request of Region. I, the licensee
committed to remain
below
5%
power pending
the results
of
a meeting
in Bethesda,
Haryland
on the fol-
lowing day to discuss
the
SPSV problem.
At the meeting,
the licensee
com-
mitted to the following actions:
scram-time
test all
185
rods,
on
each
unit,
when
a
50 -
60% power
level is reached
develop
a surveillance
procedure
to unambiguously
assess
scram pilot
valve operability,
to
be
submitted
to and
approved
by
NRC prior to
implementation,
and performed every
4 to 6 weeks
trend
and report immediately to NRC, via the
ENS network,
any failures
or anomalies
found during scram
solenoid
valve operability tests,
or
individual control
rod
time testing
(normally performed for
a
10% rod sample every
4 months)
provide
the failure analysis
results
from Franklin
Research
Center
and
General
Electric
testing
on
the
original
valves
.which failed
On October
17,
Region I issued
a Confirmatory Action Letter confirming the
above
commitments.
These actions will be reviewed in subsequent
inspections.
(387/84-35-01)
5.0
NRC Followu
Review
Resident
Onsite
Inspector
review of the
SPSV failures
focused
on the following aspects:
(1) monitoring licensee
actions to replace
the
SPSV disc holder
subassem-
blies,
(2) determining
the
reportabi lity aspects
of the
October
6
SPSV
failures, (3) review of maintenance
history of SPSVs
(4) review of scram
timing history,
and (5) post-maintenance
testing.
Item (1) was discussed
in section 3.0.
The remaining
items are discussed
below.
Following discovery of the
SPSV failures
on October
6, the licensee
prepared
Significant
Operating
Occurrence
Report
(SOOR)
1-84-370.
The
SOOR did not indicate that this occurrence
was reportable
by
and
no
ENS call was made.
The inspector
reviewed the 50.72
reportability criteria and di scussed
reportabi lity with the licensee,
Based
on
the inspector's
review,
no report of this
occurrence
was
required
per 50.72.
reports
were
made
on
October
12,
informing the
NRC of initiation of plant shutdown.
5.2
Maintenance
Histor
The
inspector
reviewed
maintenance
records
of
SPSV
maintenance
on
Units
1
and
2 to determine if previous
indications of
SPSV sticking
existed.
In August
1981, prior to licensing,
new
SPSVs
were installed in all
Unit
1
HCUs because
of a powdered granular
substance
(apparently rust)
found in four of the valves.
In June
and July 1982, just prior to
Unit
1 licensing,
new SPSVs were installed
on half of the Unit
1
and the other half were obtained
from Unit 2, rebuilt and installed
on Unit
1.
This action
was
taken
because
of
a concern with Buna-N
parts.
GE Service Information Letter (SIL) 128 recommended
rebuilding
these
valves periodically to ensure
Buna-N parts are not used in excess
of seven
years.
The rebuild kits did not contain
the
Viton-A disc
material.
Other
maintenance
on
SPSVs
since that time
has
consisted
of replacement
of SPSVs
on several
HCUs due to air leaks
and
burned
up solenoids.
No maintenance
due to sticking
SPSVs
was
noted
in the
document review on Unit 1.
I
1f
r
With respect
to Unit 2,
as noted in Section 3.3, only one half of the
SPSVs
had polyurethane
discs.
In April 1983,
18C personnel
had re-
built about
one half of the Unit 2
SPSVs for replacement
of
Buna-N
parts.
The
spare
part kits
used
for these
valves
contained
discs
made of Viton-A material.
The remainder
of the Unit
2 valves
were
replaced
with new
SPSVs
which apparently did not contain the Viton-A
disc.
These actions
were taken
because
of recommendations
in SIL No.
128.
Other
maintenance
involved replacement
of SPSVs
on several
due
to air leaks.
In April 1984,
during
rod testing
conducted
during
initial fuel loading,
two rods (i.e., 38-03
and 58-23) failed to in-
sert
when the test switches
were replaced
in test.
The
SPSVs for these
HCUs were replaced.
The inspector
examined
the
removed valves.
These
valves
had
small
crimps
in
one
solenoid
shaft
which
may
have
been
caused
by
someone
stepping
on
the
valves
during construction.
The
polyurethane disc in the valves
was not degraded.
Hence, this valve
problem is not considered
a precursor
to the October
6
SPSV problem.
Another rod (rod 38-15)
had
a
slow scram
time during
the April rod
testing.
Valve stroking of scram valves
on this
HCU was checked with
no problems
found.
5.3
Time Histor
5.3. 1
Surveillance Testin
The inspector
reviewed
the licensee's
surveillance
testing
program utilized to measure
the
maximum
and
average
insertion times of each control rod in accordance
with Tech-
nical Specifications
4. 1.3.2,
4. 1.3.3,
and
4. 1.3.4,
which
delineate
the
timing
requirements
for the
control
rods.
Surveillance
Requirement
4. 1.3.2- states
that
the
insertion
time of the control
rods
shall
be demonstrated
through measurement,
with reactor coolant
pressure
greater
than
or
equal
to
950 psig for: (1) all control
rods prior
to exceeding
40 percent
thermal
power after reactor
shutdowns
greater
than
120 days;
(2) specifically affected individual
control rods following maintenance
or modification; and (3)
at least
10% of the control 'rods,
on
a rotating basis,
at
least
once
per
120
days
of operation.
The
maximum
insertion time is measured
from the de-energization
of the
scram pilot valve solenoids
as time zero, with the rod fully
withdrawn.
The following three
surveillance
procedures
were
reviewed
to ascertain
whether the procedure
was adequate
to meet the
Technical Specification requirements:
SR-155-001,
Revision 0, Scram Time Measurement of All
Control
Rods
SR-155-002,
Revision 0,
Scram Time Measurement
of Rods
Following Maintenance
or Modification
SR-155-003,
Revision 0,
Scram Time Measurement
of Rods
Every 120 Days
Due to Susquehanna's
unique configuration,
the
scram times
can
be obtained
by two different methods.
One method util-
izes
a recorder
plugged into the Control
Rod Test Instrument
Panel
in the control
room.
The panel
senses
when the
pilot solenoids
are de-energized,
and records
the
odd (i.e.,
45,
39, etc.) notch positions of the rod as it inserts into
the core.
The insertion
times
are calculated
by analyzing
the
strip
charts
from
the
recorder.
The
second
method
utilizes the
General
Electric Transient Analysis Recording
System
(GETARS) computer,
which monitors
sensor
inputs
and
stores
the applicable data,
even during an unscheduled full
reactor
This
method
must
be corrected
due
to the
GETARS
scan
rate,
and
because
of the time response
of the
relays that the
computer
senses.
This time correction
is
properly reflected in the procedure.
The inspector
reviewed
the
completed
documentation
for the
last
three
Unit
1 -surveillance
tests
which
were
used
to
meet
the
Technical
Specification
requirements
performed
prior to October 6, 1984.
On
June
13,
1984,
Unit
1
scrammed
from full power
due to
the loss of startup transformer T-10.
During the unscheduled
trip,
GETARS obtained
time data for the
147 control
rods that were fully withdrawn.
On June
25, this data
was
utilized to
meet
Technical
Specification
surveillance
re-
quirements
4. 1.3.2,
4. 1.3.3,
and 4. 1.3.4.
The surveillance
was
signed off as
being
complete
and
meeting all of the
acceptance
criteria
on July 26 by the individual performing
the surveillance
and his supervisor.
NRC review of the completed surveillance
data
on October
18
determined that
one of the
acceptance
criteria of the sur-
veillance
was
not
satisfied.
Technical
Specification
3. 1.3.4 establishes
maximum
average
insertion
times
from the fully withdrawn position
to four specific
notch
positions for the three fastest
control
rods
in each
group
of four control rods arranged
in a two-by-two array.
During
'he
scram of June
13, the four rod array containing control rods 38-39,
38-43,
42-39
and
42-43
exceeded
the
allowable
average
scram insertion time from the fully w'ithdrawn posi-
tion (notch
48) to notch
45.
The
Technical .Specification
requires
the
average
insertion
time
not
to
exceed
0.45
seconds,
but the average
scram insertion
time of the three
fastest
rods in this array was 0.462
seconds.
The following
table
shows the applicable data;
Position Inserted
from Fully With-
dr awn
45
39
25
05
TS Limit on
Average
Insertion
Time
(Sec)
0.45
0.92
2.05
3.70
Average
Insertion
Time
During June
13
for
4
Rod
Array (Sec)
0.462
0.795
1.561
2.641
These data indicated
a hesitation of the rods at the initia-
tion of the
but the
rods fully inserted within the
required
time.
The
two slowest
rods
(38-39
and
42-39) of
the
four rod array later failed to insert during the
rod
testing
on
October
6,
1984.
The
anomaly
in
the
June
13
times
appears
to
be
a
precursor
to
the
October
6 event.
The calculations
which determined
the
scram insertion data
were
performed
by
computer.
One
page
of
the
computer
printout specifically indicated that this rod array exceeded
the required
average
scram insertion
times.
The four rods
and the average
time were listed under
a page
heading which
stated:
"Four
Rod Array with Average
Three
Fastest
Rods
Exceeding
T.S.
3. 1.3.4 Limit".
On the test data
sheet for
the surveillance,
the individual who performed the surveil-
lance,
was required to indicate (by circling YES and initi-
aling)
that
the
acceptance
criteria
had
been
satisfied.
The fact that the four rod array did not meet the Technical
Specification
was not noted
by either the
individual per-
forming the surveillance
nor
the applicable
supervisor
who
reviewed
the
completed
surveillance.
In discussions
held
with
the
individual
who
performed
the
surveillance,
he
indicated that
he
had assumed
that since the rods
had satis-
factorilyy
met the
maximum and average
scram insertion times
that the two-by-two array
numbers
would also
be satisfied.
This surveillance test
was
the first time the individual,
and the work group (i.e.
Reactor
Engineering)
had performed
the test.
Previously it had
been
performed
by the plant
engineering staff.
The Technical Specifications
required that the control
rods
with the
slower
than
average
insertion
times
be
declared
unti 1
an
analysis
was
performed
to
determine
that the required
scram reactivity
remained
for
the
slow
four
control
rod
group
and
to
increase
the
surveillance
frequency
to
at
least
once
per
60
days.
Otherwise,
the plant
was
to
be
in at least
Hot
Shutdown
within the next
12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
K
10
During the
scram of June
13,
1984, five rods were signifi-
cantly
slower
in reaching
the
notch
45 position
than
the
average
of all of the rods.
The
average
time for all of
the
rods to reach
notch
45 was
301 milliseconds,
but these
five rods
exceeded
500 milliseconds.
Of these
five rods,
four of
them
were
the
same
four that failed to
and
one
was
one of the nine that hesitated
during the surveil-
lance testing
on October 6.
The plant restarted
on June
14, but the
scram timing data
was not analyzed
until
June
25
when
the
surveillance
was
performed.
Therefore,
the
inoperability
of
the
four rod
array was not identified prior to the startup.
A thorough
review of the
time data
is normally not
performed
after each
nor is it required.
On June
25
when the
surveillance
was completed,
the appropriate Action Statement
was not entered
since the inoperability was not identified.
The plant
operated
continuously until another
unscheduled
occurred
on July
3,
1984;
Inspector
review of rod
insertion
data for that
indicated that all rod scram
insertion times met the Technical Specification
requirements'ata
was also
obtained
on
a July
15
which indicated
that
all
Technical
Specification
requirements
were
met.
The data
from the July
15
was also
used
to meet
the
surveillance
requirement.
With the capabilities of the
GETARS, all of the fully with-
drawn
rods
are
timed
on
each
and far
more
data
is
available
than
required
by Technical Specifications'or
example,
on the June
13,
1984 scram,
data for 147
rods
was
input into
the
computer
for analysis,
but
the
Technical
Specifications
only require
19 rods to
be tested
every
120
days.
If the
normal quarterly surveillance
had
been
per-
formed instead
of using all of the
scram data, it is very
probable
that
the
Technical
Specification
nonconformance
would not
have
been
detected.
During the October
6,
1984
surveillance,
the
problem again
may not have
been detected
if two of the four failed rods
had not
been
in the
20 rod
sample
selected.
It should
be
noted
that
the
data
reviewed indicates
that
the pilot valve hesitation
and sticking phenomenon
occurred
during
the June
13
after
an
82 day continuous
run,
and during the October 6,
1984 testing, after
a 78 day con-
,
t ~
tinuous
run.
The
mechanism
appears
to
be
time
dependent
and
primarily
occurs
after
a
long
period
of operation.
5.3.2
Scram Data Review
The inspector
reviewed the
GETARS scram insertion time data
for eleven
on Unit
1 which. occurred in the
18 months.
prior to the October 6,
1984 surveillance testing.
Several
of the
were utilized to
meet the surveillance
re-
quirements
as
noted
in section
5'. 1.
The
data
not
utilized for the surveillance
was
reviewed to determine if
any evidence of hesitation
occurred during previous
Additionally, the computer generated
control rod scram time
history file for each
individual control
rod was
reviewed.
The
average
time of all the control rods to reach
notch
45
from the fully withdrawn position
was approximately
260 to
270 milliseconds
throughout
the
18 month
t'ime period.
The
average
scram insertion time required
by Technical Specifi-
cations for the
same position is 430 milliseconds.
Several
occurrences
of rod insertion times greater
than
430
milliseconds
were noted during the data review:
DATE
Narch 22,
1983
October 31,
1983
June
13,
1984
July 3,
1984
July 15,
1984
42-27
42-23
54-47
58-31
42-39
38-39
58-31
54-47
54-47
TINE NS
626
432
584
752
975
891
668
507
556
Although the
above
rods
apparently
hesitated,
all of the
rods
met
the
Technical
Specification
maximum
and
average
insertion
times
(except
for the
four rod
array
on
June
13 noted in section 5.3. 1).
Of the six rods that hes-
0
'L
12
itated,
four of them failed to
and
two hesitated
on
October 6,
1984.
5.4
Post Maintenance
Test Witnessin
Between
October
18
and
24,
1984,
the
licensee
conducted
individual
rod scram testing
on both Units
1 and
2 from power levels between
50%
and
60%.
The testing
was
conducted
in accordance
with Surveillance
Procedures
SR-155-002
and SR255-002,
Time Measurement
of Rods
Following Maintenance
or Modification", Revision
0.
The inspectors
witnessed
portions of the testing.
No
unacceptable
conditions
were
noted.
The
inspectors will review the test results
when available.
6.0
Scram Dischar
e Volume Vent and Drain Pilot Valve Ino erabilit
At 2: 15 p.m.
on October
18,
1984,
the licensee
discovered that surveillance
procedure
S0-155-003,
SDV Vent and Drain Valve Eighteen
Month Operability,
was
overdue
by approximately
15 months.
A documentation
review identified
that the surveillance,
which is required
by Technical Specification
4. 1.3. 1.4
every
18 months,
was last performed
on January
23,
1982.
At some
unknown
time during
1983, it was identified that the original surveillance
docu-
mentation
was misplaced,
and
on June
2,
1983,
a
new surveillance
author-
ization cover sheet,
with the associated
test data attached
was generated
and
signed.
Due to
an administrative
error,
the
date
the
form was
re-
produced (i.e.
June
2,
1983)
was entered
into the surveillance
tracking
system
as
the completion
date of the surveillance.
Therefore,
according
to the tracking
system,
the
surveillance
was
not
due until
December
2,
1984 instead of July 23,
1984.
Technical
Specification
Surveillance
Requirement '4. 1.3. 1.4.a
states
that
the
discharge
volume shall
be determined
by verifying that
the drain
and vent valves close within 30 seconds after receipt of a signal
for control
rods to
and
open
when
the
signal
is reset,
at
least
once .per
18 months
from
a
normal
control
rod configuration of less
than or equal
to
50%
rod density.
With the
system
the
Action statement
requires
the plant to be in at least Hot Shutdown within
12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
The licensee
immediately declared
the
SDV system inoperable
when the over-
due surveillance
was identified
and
made the appropriate
notification.
The licensee
conducted
a data
search
to determine if docu-
mentation
was available
from previous reactor .scrams
to show that the vent
and drain val,ves
had operated
properly,
but
none
was
found.
At 9:21
p.m.
October
18,
1984,
the plant
was manually
scrammed
from 55% power in order
to conduct the surveillance test.
During the
the
SDV vent valve closed in 32.4 seconds
and the drain
valve closed in 26:9 seconds.
Since the vent valve did not meet the accep-
tance criteria of 30 seconds,
the
SDV remained
and investigation
commenced
on
the
cause
for the
slow stroke
time of the vent valve.
NRC
Region I requested
the licensee
to inform them of the corrective actions
yA
P
a'
4
k
~
~
13
completed to resolved
the inoperability,
and to demonstrate
that the valves
operated
in less
than
30 seconds prior to the Unit 1 startup.
Two redundant
vent valves
(XV-1F010A and XV-1F010B) are installed
on the
1
inch
SDV vent line and each is operated
by
a
separate
dual
solenoid pilot
valve
(SV-1F009A and
SV-1F009B).
The pilot valves also operate their as-
sociated
drain valve.
Currently
one vent
and
one drain valve
(XV-1F010B
and
(XV-1F011B) are mechanically
locked
open,
based
on
a commitment
made
in licensee letter PLA-1038, dated April 7,
1981,
which discussed
IE Bul-
letin 80-17.
The valves are blocked open pending completion of the instal-
lation of the
redundant
vent
and drain valve
systems
required
by the end
of the first refueling outage
by license
condition 2.C(17).
The redundant
valves
are
to
ensure
that
an uncontrolled
loss of reactor
coolant
would
not result
in the
event of
a single active fai lure.
The
SDV vent
and
drain pilot
solenoid
valves
are
ASCO,
dual-solenoid
valves
(Part
No.
HT8323A22),
and the vent valves are
Hammeldahl
Conoflow 500 Series
1 inch
On October
18 the licensee
issued
Work Authorization S44954 to investigate
the
cause
for
vent
valve
XV-1F010A
slow
stroking.
The
maintenance
technicians
initially lubricated
the
stem
and
checked
the
packing,
and
the
valve
then
operated
in
31.5
seconds.
Next
the
air
actuator
was
disassembled,
with
no deficiencies
identified.
To retest
the vent valve
a temporary rig consisting of eight feet of 1/4 inch plastic
tubing
was
used
to operate
the valve.
The vent valve operated
in eight seconds.
The
normal
supply line was reinstalled,
and the valve operated
in
32
seconds.
Based
on this information the
problem was
assumed
to be with the time re-
quired for the pilot valve to vent the approximately
45 feet of one
inch
air supply header.
A different
model
of pilot solenoid
valve is installed
in Unit 2,
and
preoperational
test data indicated that these valves,
which are
much larger
than the
ASCO valve, vented the air header significantly faster.
The Unit
2
preoperational
test,
P255. 1A,
performed
on
September
24,
1983,
found
that the vent valve closed in 7.46
seconds
from when the
signal
was
initiated.
The associated
drain valve operated
in 14.7 seconds.
Initially, it was
conceived
that this
problem
could
be
related
to the
scram pilot solenoid valve disc material
phenomenon,
since the pilot valve
was also
an
ASCO pilot solenoid of similar design to the
SPSVs.
Based
on
the test
data
showing
the valve consistently
operated
in
32 seconds,
and
the fact that the polyurethane
disc subassemblies
originally installed in
the valve were replaced with Viton-A, the reason for the failures does not
appear to be related to the
SPSV failures.
In order to correct
the venting problem,
the licensee
replaced
the
ASCO
pilot solenoid valve with a Valcor 3-way solenoid valve (Part
No. V70900-45)
on October 20,
1984.
Shutdown testing of the valve following the instal-
lation demonstrated
that the vent valve would close
in approximately
six
seconds after pilot de-energization.
In addition to replacing
the pilot solenoid valve, the licensee
conducted
a
100 percent
documentation
review to ensure that
no other similar admini-
strative errors
were
present
in their surveillance
tracking
system.
No
other deficiencies
were found.
The licensee
also modified the surveillance
documentation
forms to
emphasize
the
date
on which the surveillance
was
performed rather than the date of the form and created
a full time survei 1-
lance documentation
auditor position.
These actions
are intended to reduce
the potential for incorrect data entries
in the surveillance tracking com-
puter system.
The licensee
required
an emergency
Technical Specification
change prior to
startup,
which
was
issued
on
October
19,
because
the
Unit
1
Technical
Specifications
did not allow the unit to
be started
up with the
SDV vent
and drain valves inoperable,
but the surveillance
test required
the plant
to
be at
less
than
50 percent
rod density.
The Technical
Specification
change
allowed the unit to enter Operational
Condition
2 provided the sur-
veillance
was
performed within
12
hours
after
achieving
50
percent
rod
density.
Based
on
a review of the test results
and discussions
with Region I, the
licensee
restarted
Unit
1 and reached criticality at 3:52 a.m.
October 21,
1984.
At 1:29
p.m.
on
October
21,
the unit
was
manually
scrammed
from
approximately
7 percent
power to perform the Technical Specification sur-
veillancee
test.
The vent valve closure time for the test
was 5.2
seconds.
Unit
1 returned to criticality at 12:35 a.m.
on October
22.
7.0
Technical
S ecification Adherence
As noted in section 5.3. 1, the Technical Specifications
require that while
in Operational
Condition
1 or 2, the
average
insertion
time,
from
the fully withdrawn position for the three fastest
control
rods
in each
group of four control
rods
arranged
in
a two-by-two array,
based
on
de-
energization
of the
scram pilot valve solenoids
as
time zero,
shall
not
exceed
0.45
seconds
for notch position 45.
The applicable action statement
requires
that with the
average
insertion
times
of control
rods
exceeding
the insertion time limits, the control
rods with the slower
than
average
insertion
times
are
to
be
declared
until
an
analysis is performed to determine
that required
scram reactivity remains
for
the
slow
four
control
rod
group.
Additionally,
the
surveillance
frequency
for
insertion
times
is
to
be
increased
to
60
days.
Otherwise
the plant is to
be in at least
Hot Shutdown within the next
12
hours.
Contrary to the above,
on June
25,
1984, Surveillance
Procedure
SR-155-003
was
performed
using data
from
a June
13
scram to meet the requirement of
Technical
Specification
3. 1.3.4.
The
data
indicated
that
the
four
rod
array containing control rods 38-39,
38-43,
42-39
and
42-43
exceeded
the
allowable average
scram insertion time to notch
45,
in that the insertion
time of the three fastest
rods
was 0.462
seconds.
Since the data
was not
properly reviewed,
and
the inoperability not identified,
the
applicable
Action requirements
were not completed.
This condition
remained until
a
4
4
4-
15
subsequent
reactor
on July 3,
1984.
The surveillance
was
not re-
performed until July 15,
1984.
As noted
in section
6.0,
Technical Specification Surveillance
Requirement
4. 1.3 . 1.4.a
states
that
the
discharge
volume
shall
be
determined
by verifying that the drain and vent valves close within 30 seconds
after receipt of
a signal for control
rods to
scram at least
once per
18
months
from a normal control rod configuration of less
than or equal
to 50
percent
rod density.
Contrary
to
the
above,
at
2: 15
p.m.
on
October
18,
1984,
the
licensee
discovered that Surveillance
Procedure
S0-155-003,
SDV Vent and Drain Valve
Eighteen
Month Operability,
was last
performed
on
January
23,
1982,
and
was therefore
overdue
by approximately
15 months.
This violation was iden-
tified by the licensee
and promptly reported to the
NRC by an
ENS notifi-
cation.
Inspector review determined
that the corrective action
completed
and
planned
should prevent
recurrence.
Additionally, it was not a viola-
tion that
could
reasonably
be
expected
to
have
been
prevented
by
the
licensee's
corrective action for a previous violation.
Since
the criteria for licensee
identified violations
stated
in
10 CFR Part 2 Appendix
C
have
been satisfied,
a notice of violation will not be
issued,
but
the corrective
actions
implemented
by the 'licensee
will be
reviewed in a subsequent
inspection.
(387/84-35-03)
Safet
Si nificance
The
event discussed
in section
5.2
and 7.0 involved
one
2
x- 2 rod array
exceeding
the
average
insertion
time
from
the
fully withdrawn
position to notch 45.
The rods exceeded
this time by
10 milliseconds
and
they
met
the
insertion
times for the
remainder
of the
rod travel.
The inspector
discussed
the significance of this event with
NRR (members
of the
Reactor
Systems
and
Core
Performance
Branches)
and
reviewed T.S.
bases
and the
FSAR.
The purpose of the T.S.
scram insertion
times
are to
ensure that the control rods insert reactivity at
a rate within the bounds
of that assumed
in transient
and accident analysis.
The reactivity inser-
tion rates
must bring the
reactor
subcritical
at
a rate fast
enough
to
prevent
the
Minimum Control
Power
Ratio
(MCPR)
from becoming
less
than
1.06 during the limiting power transient
analyzed
in
FSAR chapter
15.
The
NRR reviewers
indicated that
exceeding
the
average
insertion
time
during the first few notches
of rod insertion
has
no effect on transient
and
accident
analysis
since
very little reactivity
is
inserted.
The
reactivity insertion rates
assumed
in analyses
are not affected unless
the
rods
are
slow in reaching
approximately
50 percent
rod insertion
to the
core.
t
1$
'1
P
1
p 7
16
The
rod
time data for the July
3
and July
15
indicate that
this four rod array met T.S. insertion times.
Based
on the time dependency
of the failure
mechanism
of the
SPSVs
(section
5.3. 1), it can
also
be
assumed
that
these
rods
would
have
met
the
insertion
time
requirements
immediately after the
June
13
Hence,
the
safety
significance
of
these
rods not inserting within the required time is minimal.
Nevertheless,
the
event
is significant
from the point of view that it
involved the improper review of surveillance
data
and the fact that two of
the affected
rods identified in this
occurrence
later failed to insert
during testing
on October 6,
1984.
Since
each control
rod drive mechanism
has its
own scram
and pilot valves,
only one drive
can
be affected if a
valve fails to open.
In other
words,
a single failure in
a hydraulic control unit would result
i n the
failure of only
one control
rod.
Due to the
presence
of the
inadequate
polyurethane
material in the
SPSV,
the potential
did exist,
however,
that
a
common
mode failure could have
caused
a significant number of rods to be
The mechanism that could have possibly identified the
problem
earlier,
the surveillance
procedure,
was not properly reviewed,
and there-
fore the precursor
event
on June
13
was
not investigated.
It should also
be
noted
that
due
to the
superior
capabilities
of the
plants
computer
systems,
significantly
more
data
is available,
and
much
more
than
the
required testing is actually completed.
In the event that
a large
number of individual SPSV's
were to fail to open
on
a scram,
the entire air
that supplies
the
SPSV
can
be depress-
urized
by either
Backup
valve
(SV-1F110A and
SV-1F110B).
Although
the
rods would
scram at
a
much
slower rate,
due to the
venting
process,
the
control
rods
would insert.
The
four rods did not
during
the
October
6 surveillance
testing,
because
only the local test
switches
were
utilized to
the rod.
During the preoperational
testing of Unit 1,
the time to depressurize
the air header
for each
backup
valve
was
43.3
seconds
for
F110A
and
28.21
seconds
for
F100B.
The
backup
valves
are
not
included
in
T.S.
required
surveillance
testing.
In
response
to
an unrelated
issue,
the plant intends to test these
valves
on
a refueling interval basis
although they have
not, yet
been
retested
since
the preoperational
test program.
9.0
Exit Meetin
On
October
26,
1984,
the
inspectors
discussed
their findings with the
Assistant Plant Superintendent
and
members of his staff.
~I
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