ML17138B431
| ML17138B431 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 04/20/1980 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17138B428 | List: |
| References | |
| 50-387-80-05, 50-387-80-5, 50-388-80-03, 50-388-80-3, NUDOCS 8008120613 | |
| Download: ML17138B431 (1) | |
Text
'APPENDIX A
'NOTICE'OF 'VIOL'ATION Pennsylvania Power and=Light Company Docket No. 50-387 This refers to the inspection conducted by a'representative of the Region I (Philadelphia) office at the Susquehanna Steam Electric Station, Unit 1, Berwick, Pennsylvania, of activities authorized by NRC License No.
CPPR-101.
During this inspection, conducted on March 24-28, 1980, the following apparent item of noncompliance was identified:
10 CFR 50, Appendix B, Criterion XV, requires, in part, that:
"Nonconforming items shall be reviewed and accepted,
- rejected, repaired; or rewor ked in accordance with documented procedures."
The Susquehanna PSAR, Appendix'D,. paragraph D.3.3.13, states, in part, that:
"For nonconforming'items which may be made usable through rework, repairs or modification of requirements, reports are prepared and submitted to the project engineering team for resolution."
The Bechtel guality. Assurance Manual, ASME-Section III, Division 1, Section 5723, states, in part,.:
"1) An NCR is prepared when, a nonconformance is identified by inspection'r another means."
Contrary to the above, on March 27,
- 1980, a quality control inspector identified the root gap spacing as being in excess of 5/32" on pipe weld joint GBB-104-1-Fll-16-Rl.
The specified welding procedure Pl-AT-LH-RO requires a maximum root gap spacing of 5/32".
The inspector released the weld joint for processing and did not issue a nonconformance report.
This item is an infraction.
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