ML17053A698

From kanterella
Jump to navigation Jump to search
Forwards LER-010/03L-0
ML17053A698
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 05/23/1979
From: Lempges T
NIAGARA MOHAWK POWER CORP.
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17053A699 List:
References
NMP-1123, NUDOCS 7905300486
Download: ML17053A698 (2)


Text

NMP-1123 NIAGARAMOHAWKPOWER CORPORATION/300 ERIE BOULEVARDWEST, SYRACUSE, N.Y. 13202/TELEPHONE (315) 474 1511 MaI/ 23, 1979 N,. Boyce H.

Gtu'.e/L Mr>ecto/L UnLted Statm Nuclea/L ReguLato/Ly Conun&dmn Regin I 631 Puck Avenue.

King o$ PtuLssm, PA.

19406 RE:

Sock& No.

50-220 Pea/L h(/L. Gtu'.e/L:

In acco/I.dance IoMh N~ne h4Le Pet Nu&ea/L Station Un'1 Tech'.ca1'peci.p.~es, uIe he/LebIJ sub~ Liceesee Event Repo/Lt LER 79-10, III.ch ~ an acco/cdance III'e~on b. 9. 26 (2) o( She Technical' peei.g.cation'.

TEA /Lepo/Lt wa5 completed an She (o/Immit designated ~

NUREG-Olbl, dated 3uLg 1977.

Ve/Ly Muddy you%6, T.E.

Lempge5 GenetutL Supetu.ntendent NucZea/L Gen~ion (o/L R.R. Schneide/L V~ce P/I.ee&mt-Fgectiu.c P/Lodu~on

'IItm AttachInent (3 cop~e5) xcI 17mecto/L, OI(p.ce o( ISE (30 cop~e5)

Vme&o/L, OtIpce o) MIPC (3 cop~m) t.

RE4uuTORY DOLNFT '-I'

(;OPy 7905 3 00+5'0

NRC FORM 366 I7 77)

CONTROL BLOCK:

,Q U. S. NUCLEAR REGULATORY COMMISSION LlCENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION)

~01 7

8 CON'T

~01 7

8 N

Y N

tl P

9 LICENSEE CODE 1 Q20 0

0 0

0 0

0 14 15 LICENSE NUMBER 0

0 Q3 4

1 1

1 QE~

QE 25 26 LICENSE TYPE 30 57 CAT 58 SDURcF ~LQB 0

5 0

0 0

2 Q7 0

4 2

4 7

9 Qs 5

QB 60 61 DOCKET NUMBER 68 69 EVENT PATE 74 75 REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 During refueling outage, containment vacuum relief valve (68 IV-10) f1 ange fai 1 ed its 1 eak rate test.

Thi s res ul ted in minimal safety implications since the unit was shutdown for refueling.

~OS

~06

~os 7

8 9

80 7

8 SYSTEM CAUSE CAUSE COMP.

VALVE CODE CODE SUBCOOE CON'IPONENTCODE SUBCOOE SUBCODE

~90 QTI E

Q12

~XQ13 V

A C

V E

X QE

~BQIE

~C Q16 9

10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LER Ro EVENTYEAR REPORT'NO.

CODE TYPE NO.

Q17 REPORT ~79

+

~01 0

U~ ~

U 0 U

21 22 23 24 26 27 28 29 30 31 32 ACTION. FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDP PRIME Coh1P.

COMPONENT TAKEN ACTION ON PLANT METHOD HOURS ~22 SUBMITTED FORM SUB.

SUPPLIER MANUFACTUR"R OIB~ QIB

~Q20

~Q2 0

0 0

0

~N Q23

~NQ24

~A Q2s A

1 8

0 Q26 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION ANDCORRECTIVE ACTIONS Q27 0-rings were replaced on flange of containment vacuum relief valve

'I (68'V-10), which subsequently passed its leak rate test.

3 ~

3 4

OTHER STATUS 7

8 9

11 12 LOSS OF OR DAMAGETO FACILITYQ43 TYPE DESCRIPTION 0

Z Q42 NA 7

8 9

10 P U8 LIC ITY ISSUED DESCRIPTIONQ CH LJNO NA 7

8 9

10 NAME OF PREPARER E.

Duda 7

8 9

FACILITY STATUS VEPOWER

~NQ>> ~00 0

QEE NA 7

8 9

10 12 13 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITY

~ls Z

Q33 Z

Q34 NA 7

8 9

10 11 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q30 7 ~00 0

Q37 ~ZQ33 NA 7

8 9

11 12 13 PERSONNEL INJURIFS NUMBER OESCRIPTIONQ41 3 ~00 0

Qo NA Q30 METHOD OF DISCOVERY 45 LBJQ>>

44 45 46 QBB DISCOVERY DESCRIPTION Q2 Leak Rate Test LOCATION OF RELEASE Q NRC USE ONI Y PHDNE(315)343-2110 Ext 1306 53 00 A'4 80 80 80 80 80 80 33 OE 7

80 o