ML16343A234

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Insp Repts 50-275/94-17 & 50-323/94-17 on 940606-10.No Violations Noted.Major Areas Inspected:Mov Program in Response to GL 89-10
ML16343A234
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 06/30/1994
From: Westerman T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342C611 List:
References
50-275-94-17, 50-323-94-17, GL-89-10, NUDOCS 9407110063
Download: ML16343A234 (28)


See also: IR 05000275/1994017

Text

APPENDIX

U.S.

NUCLEAR REGULATORY COHHISSION

REGION IV

Inspection Report:

50-275/94-17

50-323/94-17

Licenses:

DPR-80

DPR-82

Licensee:

Pacific

Gas

and Electric Company

77 Beale Street,

Room

1451

P.O.

Box 770000

San Francisco,

California

Facility Name:

Diablo Canyon Nuclear Generating Station, Units

1 and

2

Inspection At:

Diablo Canyon Site,

San Luis Obispo Coun.y, California

Inspection

Conducted:

June 6-10,

1994

Inspectors:

C. Hyers,

Reactor Inspector,

Engineering

Branch

Division of Reactor Safety

H. Runyan,

Reactor

Inspector,

Engineering

Branch

Division of Reactor Safety

Approved:

esterman,

ie

,

ngineenng

rane

Division of Reactor Safety

ate

Ins ection

Summar

Areas

Ins ected

Units

1 and

2

Routine,

announced

inspection of open

items

from previous

NRC inspections of the licensee's

motor-operated

valve program

in response

to Generic Letter 89-10.

Temporary Instruction 2515/109

and

Inspection

Hodules

93903

and

40500 were used

as guidance during the

inspection.

Results

Units

1 and

2

The licensee

has

shown good progress

toward the closure of their Generic Letter 89-10 program.

Host of the previously open inspection

issues

from NRC

Inspection

Report 50-275; 323/93-19

were closed

and

one of two open inspection

issues

from NRC Inspection

Report 50-275; 323/91-39.

These include the

following issues:

~

Hotor-operated

valve trending (Section 1.2),

94071l00b3

940705

PDR

ADOCN 05000275

8

PDR

0

~

Corrective action for Motor-Operated

Valve 2-LCV-109 (Section 1.3),

I

~

Evaluation of diagnostic signature for Motor-Operated

Valve 2-FCV-37

(Section 1.5),

Use of valve specific values in calculations

(Section 1.6),

Extrapol.ation of peak opening thrust for rising stem valves

(Section 1.7),

and

~

Clarification of the torque switch setpoints for limit-seated motor

control logic (Section 1.8).

Issues

remaining open,

which will be addressed

during the

NRC closure review

of Generic Letter 89-10 actions,, include the following:

~

Periodic verification of motor-operated

valve design. basis capability

(Section 1.1),

and

Pressure

locking and thermal

binding (Section 1.4);

Two observations

from the inspection include:

Licensee self assessments

of the motor-operated

valve program were

observed to be comprehensive

and technically oriented

(Section 2).

~

Two instances

were identified where the troubleshooting

performed did

not identify .the root cause of the operational

failures of

motor-operated

valves prior to returning the valves to operation

(Section 3).

Summar

of Ins ection Findin s:

Inspection

Followup Item 275;323/91-39-02 will remain

open

(Section 1.1).

Inspection

Followup Item 275;323/91-39-03

was closed

(Section 1.2).

Unresolved

Item 323/93-19-01

was closed

(Section 1.3).

Inspection

Followup Item 275;323/93-19-02 will remain

open

(Section 1.4).

Inspection

Followup Item 275;323/9319-03

was closed

(Section 1.5).

Inspection

Followup Item 275;323/9319-04

was closed

(Section 1.6).

Inspection

Followup Item 275;323/9319-05

was closed

(Section 1.7).

P

~

Inspection

Followup Item 275;323/9319-06

was closed

(Section 1.8).

t

Attachment:

~

Attachment

Persons

Contacted

and Exit Meeting

Detail s

1

FOLLOWUP OF

OPEN

ITEMS FROM PREVIOUS

NRC INSPECTIONS (93903)

1.1

0 en

Ins ection Followu

Item 275 323 9139-02:

eriodic Verification

During previous

NRC inspections,

the inspectors

had found that the licensee-

had not developed

a program for periodic verification of motor-operated

(HOV)

design basis capability.

Through discussions

with licensee

personnel

during this inspection,

the

inspectors

found that the licensee's

program for periodic verification was

still under development.

The licensee's

program for periodic verification was

scheduled

to be implemented

by December

1994, consistent

with their

commitments

in response

to Generic Letter (GL) 89-10.

The licensee currently

planned to verify the design basis capability of each

HOV in their

GL 89-10

program every three refueling outages

by static diagnostic testing.

The

licensee

stated that probablistic risk analysi~

wo~ld be used to prioritize

valves for testing

based

on safety significance.

The inspectors

discussed

with the licensee

the weaknesses

in the use of static testing only to verify

design basis capability.

The licensee

acknowledged

the inspectors'oncern

and stated that they were monitoring industry efforts in this area.

This 'item will remain

open pending the development

and implementation of the

licensee's

periodic verification program in December

1994.

Closing of this

item will be included

as part of the

NRC review for closure of GL 89-10.

NRC

acceptance

of static diagnostic testing for periodic verification of HOV

design basis capability is dependent

on the licensee

developing

an adequate

technical

basis.

1.2

Closed

Ins ection Followu

Item 275 323 9139-03:

HOV Trendin

During

a previous

NRC inspection,

the inspectors

noted that the licensee

had

not yet implemented a'rogram for HOV trending.

During this inspection,

the inspectors

found that Procedure

HA1. ID4, "Control

and Trending of Hotor-Operated

Valve Diagnostic Information," Revision 0,

had

been

issued

on September

28,

1993.

This procedure

provided guidance for

evaluating diagnostic test results

and identifying trends that

may indicate

impending problems.

The procedure

also provided

a method for trending

HOV

failures.

The inspectors

found that the licensee

had implemented

a computerized

trending

program.

The inspectors

observed

a demonstration

of the'program's

capabilities.

The trending information was used primarily as

a qualitative

indicator of degrading conditions.

According to the licensee,

quantitative

limits on allowable deviation

and degradation will be developed

as

more data

is accumulated.

HOV diagnostic test data

was=- loaded into the trending program

and evaluated within approximately

2 to

6 months following the test date.

The

I)

Ii[

r'

trended

parameters

included running load thrust,

unseating thrust, thrust at

torque switch trip, maximum thrust;- elapsed

time between

motor start

and

hammerblow,

current at torque switch trip,

and limit switch actuation points.

The inspectors

noted that valve factor,

stem friction coefficient, rate-of-

loading,(ROL),

and springpack

compression

were not trended.

The licensee

stated that adverse

trends related to these

parameters

could

be detected

indirectly by analyzing the other trended

parameters.

The inspectors

determined

that the trending

program

was acceptably

formulated

and sufficiently implemented to'permit closure of this part of the licensee's

commitment to

GL 89-10.

The fact that the trending

program was fully

implemented well in advance of the licensee's

GL 89-10 closure

commitment, date

(December

1994)

was considered

a program strength.

1.3

Closed

Unresolved

Item 323 9319-01:

Corrective Actions for

MOV 2-LCV-109

During

a previous

NRC inspection,

the inspectors

found that the licensee's

roubleshooting

and in'tial corrective actions for ar operational

failure of

MOV 2-LCV-109 in July

1993 did not appear

to be adequate

to identify and

correct the root cause of the failure prior to return of the

MOV to service.

The failure mode

was not reproducible

and the cause of the failure was not

evident during initial maintenance

troubleshooting.

The licensee

had

originally diagnosed

the cause of the failure to be

a faulty torque switch.

However, the torque switch was

found to be performing correctly during

troubleshooting.

Without finding any other obvious

component

problems,

the

licensee

continued to focus

on the torque switch

as being the cause

of the

failure and rationalized that the Failure

mode of the torque switch was

intermittent.

The licensee

replaced

the torque switch

as corrective action.

The inspectors

had con'sidered

the. adequacy

of the licensee's

corrective

actions to be

an unresolved

item pending review of open

Nonconformance

Report

(NCR)

No. DC2-93-EM-N037, which the licensee

had initiated to further

investigate

the root cause of the failure.

During this inspection,

the inspectors

found that the licensee

had originally

documented

the problem

and the initial corrective maintenance

performed in .a

quality evaluation

(gE) at the time the

MOV was returned to service.

After

technical

review of the

gE by the plant review board

(PRB), the licensee

had

determined that additional electrical

troubleshooting

was warranted

to rule

out potential

causes

other than the torque switch.

NCR No.

DC2-93-EM-N037

was written for the additional troubleshooting.

The licensee

had initiated

the

NCR within 5 days after return to service

in accordance

with their gE

review procedure.

The

MOV was

removed

from service for additional electrical

troubleshooting,

which identified

an intermittent high contact resistance

in

an auxiliary contact

in the motor starter.

The licensee

replaced

the

auxiliary contacts

and performed diagnostic testing prior to returning the

valve to service..

In addition,

increased

frequency surveillance testing with

diagnostic

instrumentation

was conducted for approximately

3 months without

any repeat of the problem.

. The inspectors

found the licensee's

corrective actions

'under

NCR

No. DC-2-93-EM-N037 to be adequate.

The inspectors

found that the licensee's

initial maintenance

troubleshooting activities

had

been

narrow and prejudiced

toward the preconceived

cause

at the time.

The troubleshooting

had not been

expanded

in

a controlled

and systematic

fashion

when the original diagnosis

failed to be confirmed.

The inspectors

observed

that the

MOV appeared

to have

been initially returned to service

on the basis that the maintenance activity

of replacing the torque switch

had

been

performed adequately

rather than

on

the basis that the root cause of the failure had

been corrected.

The

inspectors

considered this to be

an example of a weakness

in the control

and

technical

depth of troubleshooting activities

and the acceptance

criteria for

returning

MOVs to service following troubleshooting.

Another example of this

weakness

is discussed

in Section

3.

Based

on the adequacy of the root cause

evaluation

conducted

under

NCR

No. DC-2-93-EM-N037, which the licensee

had initiated

as

a result of their

gE

evaluation

and the licensee's

commitment

as discussed

in Section

3, this item

is closed.

1.4

0 en

Ins ection Followu

Item 275 323 9319-02:

Pressure

Lockin

During previous

NRC inspections,

the inspectors

had found that corrective

action's for six MOVs were planned to be

implemented at the next available

outage.

The licensee

had determined that the six MOVs were susceptible

to

pressure

locking.

During this inspection,

the inspectors

found that the licensee

had modified

MOV 1-8703 during the

1R6 outage=by drilling a hole in the valve disk to

preclude

pressure

locking.

The remaining five MOVs were Unit 2

MOVs which

were planned to be modified in an identical

manner during the

2R6 outage

in

. September

1994.

i

This item will remain

open pending

completi'on of the modifications of the

Unit 2

MOVs in September

1994.

1.5

Closed

Iris ection Followu

Item 275 323 9319-03:

Evaluation of

Dia nostic Si nature for MOV 2-FCV-37

During

a previous

NRC inspection,

the inspectors

had questioned

the accuracy

of the licensee's

diagnostic thrust signature

analysis for MOV 2-FCV-37.

The

licensee

had performed the analysis of thrust data obtained

from differential

pressure

testing to demonstrate

the design basis capability of the

MOV under

their

GL 89-10 program.

Specifically, the inspectors

had questioned

an apparent

non-conservative

'dentification of the zero-thrust point on the diagnostic thrust signature.

Proper, identification of the zero-thrust

event

was important in the analysis

of the thrust signature

in order to accurately

determine

the magnitude of

thrust during key events

in the operating cycle of the

MOV.

Typically the

zero-thrust point was identified using the closing thrust trace.

If not

evident in the closing trace,

an alternate identification was possible

using

the opening thrust trace.

The inspectors

had reviewed the thrust signature

for NOV 2-FCV-37

and noted that the licensee

had marked the zero point using

the opening thrust trace.

However,

the inspectors

had noted

a prominent

zero-thrust

plateau

evident in the closing thrust trace which appeared

to be

a

more conservative

determination of the zero-thrust point.

This thrust plateau

was offset 1600 pounds-force (lbf) in the compressive direction from the zero

point selected

by the licensee.

Using the more conservative

apparent

zero

point from the closing trace,

the inspectors

had been

concerned

that the

NOV

may not have demonstrated

adequate

capability because

the resulting

indicated

thrust at torque switch trip was approximately

200 lbf less

than the

calculated

minimum thrust required to close the valve under design

basis

conditions.

In response

to the inspectors'oncern,

the licensee

contacted

Liberty

Technologies,

the supplier of the

VOTES diagnostic

system.

The licensee

stated that Liberty Technologies

concurred with their original selection of

the zero-thrust point.

During this inspection,

the inspectors

examined

the thrust trace for the

identical Unit

1

NOV I-FCV-37.

The inspectors

noted the

same general

shape of

a thrust plateau

evident in the closing trace

as

had

been

noted in

HOV 2-FCV-37.

The licensee

had also

used the opening trace for HOV I-FCV-37

to identify the zero-thrust point as they had done in the case of

HOV 2-FCV-37.

The inspectors

further reviewed both valve signatures for other confirmatory

indications of the appropriate

zero point.

The inspectors

noted that use of

the more conservative

zero-thrust point from the closing trace would result in

indicated running loads inconsistent with the effects of stem ejection forces.

Further,

the inspectors

found that use of the licensee's

zero point was

consistent

with the assumption

that stem ejection loads

exceeded

packing

loads.

Based

on these

observations

and the vendor concurrence,

the inspectors

determined that the licensee's

selection of the zero point was acceptably

justified.

The inspectors

noted that the unexplained thrust plateaus

in the closing

signatures

of both valves

were not documented

as anomalies

for. the purposes

of

evaluation

and trending.

The licensee

stated that they had not originally

considered

the trace characteristics

to be anomalies.

The licensee

stated

that they would review their documentation

of unexpectec

trace characteristics

to assure

that their signature

analysis

was adequately justified and

documented,

and that anomalous

conditions

were appropriately identified.

The

inspectors

did not consider the anomalous

thrust plateaus

in the closing

traces for HOV I/2-FCV-37 to constitute

an immediate operability concern.

0

h

1.6

Closed

Ins ection Followu

Item 275 323 9319-04:

Use of Valve

S ecific

Values in Calculations

4

During

a previous

NRC inspection,

the inspectors

had noted that the licensee's

program did not provide for feedback of test results to validate the value for

rate-of-loading

(ROL) assumed

in the licensee's

HOV setpoint calculations.

ROL (also

known as load-sensitive

behavior)

was

a dynamic operating

characteristic

displayed

by some

HOVs in which the torque switch actuates

prematurely during closure

under differential pressure

conditions.

A ROL

allowance

was incorporated

in the licensee's

setpoint calculations to account

for this difference in HOV performance

under differential pressure

conditions

compared

to the static conditions

under which the torque switch was adjusted.

ROL was defined

as the difference in thrust at torque

swit'ch trip measured

under static testing

and dyna'mic testing,

expressed

as

a percentage

of static

thrust.

Licensee

Procedure

ICE-12,

"ILC Engineering

Procedure for Preparation

of

Hotor-Operated

Valve Sizing

and Switch Setpoint Calculations,"

Revision 4,

as

umed

a value of 15 percent for ROL in establishing

an allowable setpoint

range for the torque switch setting.

While the licensee

found this value to

be conservative

in most cases,

some

HOVs displayed

ROL in excess

15 percent

during testing.

For these

MOVs, the minimum thrust setpoint would not have

been revised to account for actual

valve performance

which exceeded

assumptions.

Even though testing demonstrated

the adequacy of the existing torque switch

setting,

the inspectors

had

been

concerned

that torque switch settings

could

be lowered after differential pressure

testing to the minimum thrust setpoint.

Without appropriate

revision of the minimum thrust setpoint for higher than

expected

ROL, the lower range of allowable torque switch settings

would not be

adequate

to assure

design basis capability.

During the original inspection,

the licensee

was in the process

of revising

Procedure

ICE-12 to incorporate test results.

The licensee

committed to

review existing test data to justify their use of a

15 per'cent

margin for ROL

and ensure that current torque switch settings

based

on that assumption

were

valid.

During this inspection,

the inspectors

found that the licensee

had completed

the review of existing test data

and

had verified that all existing torque

switch settings

were valid.

The thrust setpoint

windows for several

HOVs had

been revised to account for ROL greater

than

15 percent.

Until the revised

setpoints

were fully implemented,

the licensee

had instituted administrative

restrictions to prevent

any adjustment of the torque switch setting of

GL 89-10

HOVs without engineering

approval.

The inspectors

reviewed

Procedure

ICE-12, Revision 7,

and verified that the

licensee

had incorporated

valve specific

ROL in the thrust setpoint

window if

the observed

ROL exceeded

the

assumed

value of 15 percent.

In addition,

the

minimum required setpoint

included

a nominal margin of 20 percent to account

for torque switch repeatability

and

stem lubrication degradation.

To justify their generic

assumption of 15 percent for ROL, the licensee

performed

a review of the existing test data.

The licensee

documented this

review in a letter dated

September

3,

1993.

The licensee's

review indicated

that all but one gate valve had

an

ROL less than.15 percent.

The inspectors

reviewed the licensee's justification and found it to be adequate for gate

valves.

However, the licensee

determined that

6 of 18 globe valves displayed

a

ROL in

excess of 15 percent.

The licensee

had

used yoke-mounted

sensors

during

dynamic testing of these valves.

The licensee

performed

seven repeat

diagnostic tests of globe valves using stem-mounted

sensors

and found the

ROL

value: to differ significan'

from those determined

using yoke-mounted

sensors.

The

ROL determined

from these

repeat tests

ranged

from -4.75 percent

to 7.54 percent.

In one case for NOV 1-8105,

ROL wa's determined

to be

51 percent

using the yoke-mounted

sensor

but only 4.84 percent

using the

stom-mounted

sensor.

Likewise, the

ROL for HOV 1-8974B appeared

to change

from 55 to 5.37 percent.

The lower

ROL found was attributed to the higher

indicated thrust at torque switch trip measured

under dynamic conditions using

stem-mounted

sensors.

The licensee

had preliminarily determined that the high

ROL observed with the yoke-mounted

sensors

was erroneous,

resulting from an

interaction

between

the sensor

and the anti-rotation device installed

on these

valves.

The licensee

concluded that the actual

load sensitive

behavior of the

globe valves determined

from stem-mounted

sensors

was consistent with the

15 percent

assumption.

The inspectors

reviewed this material

and concluded

that the licensee

was justified in maintaining

a generic

15 percent

ROL

assumption for globe valves.

According to the licensee,

the anomalous

behavior of the

VOTES sensors

would

be pursued with the vendor (Liberty Technologies)

to determine

the extent of

the generic

problem in applications

involving similar anti-rotation devices.

The inspectors

concluded that the licensee

had satisfactorily addressed

the

concerns related to

ROL.

1.7

Closed

Ins ection Followu

Item 275 323 9319-05:

Review of Previous

Test Data

During

a previous

NRC inspection,

the inspectors

had noted that licensee

Procedure

ICE-12, Figure 8, "Rising Stem

HOV Test Evaluation Sheet,"

Revision 3, did not extrapolate

the peak opening thrust after pullout to

assure

adequate

NOV capability under design basis conditions.

A later

Revision

4 to the evaluation

sheet

had incorporated this extrapolation.

The

licensee

committed to review previous test data using the Revision

4 criteria

by October 30,

1993.

The inspectors verified that extrapolation of peak opening thrust was required

through the current Revision

7 to Procedure

ICE-12.

The licensee

had

-10-

completed

the review. of previous test data

and

had not identified any

resulting operability concerns.

The inspectors

concluded that the licensee

had acceptably

addressed

this issue.

1.8

Closed

Ins ection Followu

Item 275 323 9319-06:

Review of Limit

Seated

MOV Tor ue Switch Settin

During

a previous

NRC inspection,

the inspectors

were concerned that the

licensee

did not include

a margin for ROL for limit-closed HOVs in their

determination of the minimum required thrust setpoint.

The licensee's

limit-closed motor control logic used the closed limit switch for closure

control.

The torque switch was set at the maximum achievable setting

permitted

by the limiter plate to act

as

a backup for the limit switch.

Since

the torque switch was in series with the limit switch and enabled for the

entire closing stroke,

the insnectors

were concerned

that the torque switch

setting

may not

be adequate

to assure that it did not inadvertently actuate

under design basis conditions

due to

ROL and prematurely interrupt the valve

closure.

During this inspection

the licensee clarified that

a l5 percent

margin was

incorporated

in the minimum required setpoint for ROL in limit-seated

HOVs but

not for bypass-seated

HOVs.

The licensee

defined bypass-seating

as

a

variation of limit-seating motor control logic in which the torque switch was

bypassed

during closure until the point of valve seat contact.

The inspectors

reviewed

Procedure

ICE-12, Revision 7,

and verified the

licensee's

clarification of the torque switch setpoint determination for MOVs

using limit-seated motor control logic.

No additional

concerns

were

identified.

2

QUALITY ASSURANCE INVOLVEMENT (40500)

The inspectors

reviewed the following assessments

of HOV related activities

performed

by the site quality assurance

organization:

Electrical Maintenance

Surveillance

Report

No. SQA-94-0006,

Maintenance Quality Audit No. 94-0101,

and

GL 89-10 Management

Prerogative Audit No. 94-0161.

Although Audit

No. 94-0161

was still in progress,

the inspectors

discussed

the extent. and

preliminary findings of this effort with the audit team leader.

The inspectors

found that Audit No. 94-0161

was

a self-assessment

of the

licensee's

GL 89-10 program.

The audit had

been started

in February

1994

and

included approximately

5 man-months of inspection.

The audit reviewed the

licensee's

program for preparation of MOV sizing

and switch setpoint

calculations,

specifically focusing

on the adequacy of design basis reviews,

MOV calculations,

as-left torque switch settings,.flow test evaluations,

and

corrective actions

taken in response

to the previous

NRC

MOV inspection.

Each

of the auditors

attended

a 5-day team training course

provided

by a contractor

(General

Physics) prior to the start of the audit.

0

I

The inspectors

reviewed several

documents detailing the methodology

used in

assessing

MOV sizing

and torque switch settings

and design basis calculations,

including the determination of maximum expected differential pressure,

maximum

expected

flow rate,

and minimum anticipated

voltage.

Based

on this review and

discussions

with the audit team leader,

the inspectors

concluded that the

MOV

self-assessment

was

a comprehensive,

technically-oriented effort.

At the exit

the inspectors

encouraged

the licensee

to be responsive

to the quality

assurance

audit findings to assure

adequate

resolution of any deficiencies

within the committed program schedule.

3

-FAILURE OF

NOV 2-FCV-37

During this inspection,

the inspectors

reviewed

an operational

failure of

HOV 2-FCV-37, which occurred

in January

1993, prior to

GL 89-10 differential

pressure

testing in March 1993.

During

a routine

pump surveillance test

on January

31,

1993,

HOV 2-FCV-37,

a

turbine-driven auxiliary feedwater

steam supply isolation valve, failed to

close.

The torque switch tripped prematurely

at the start of the closing

stroke.

Valve motion stopped

at

a valve position approximately

95 percent

fully open

when the limit switch enabled

the torque switch in the motor

control circuit.

During initial troubleshooting activities performed

by the licensee's

maintenance

personnel,

the valve was stroked manually

and

was noted to be

difficult to operate

over

a portion of the closing stroke.

The valve was then

stroked electrically, with the observation that the torque switch was

"bouncing."

On the third electrical 'stroke,

the failure was duplicated with

the valve stopping after closing only five percent of the full stroke.

Inspection of the

stem revealed

marginal lubrication.

After the

stem

had

been

relubricated,

four successful

electrical

strokes

were conducted,

and torque

switch bouncing

was

no longer evident.

The immediate root cause

was

determined

to be

a sticking valve stem resulting

from degraded

lubrication.

The valve was returned to service

on February

1,

1993.

Diagnostic testing

was

not performed at this time.

On February

5,

1993,

gE 90010397

was initiated to address

the quality concerns

related to the event.

Over the next month,

VOTES diagnostic tests

were

conducted

under static conditions with satisfactory results.

'During subsequent

actuator

overhaul

on March 12,

1993,

in preparation for

GL 89-10 testing,

an internal

inspection

revealed significant corrosion of the

upper thrust bearing

and extensive lubrication contamination

and degradation.

The corrosion

was apparently

caused

by moisture intrusion that resulted

from

an earlier improper maintenance

activity in April 1990.

At that time,

an

environmental

seal'(quad

ring) was not installed

and another

was replaced with

a quad ring of improper fit.

NCR DC2-93-EH-N014

was issued.

The licensee

determined that the previous failure in January

1993

was

due to excessive

internal operating

torque in the actuator

which reduced

the output thrust

capability.

The licensee

determined

the root cause to be

an inadequate

0

0

-12-

maintenance

procedure that did not have sufficient detail to ensure that the

seals

were properly .rei'nstalled following operator disassembly.

Procedure

HP E-53. 10M, "Limitorque SHB-00 and SB-'0 Valve Operator

Maintenance,"

was revised to contain detailed

steps

and

a composite

assembly

drawing for reassembly

of the operators.

The inspectors

reviewed

NCR DC2-93-EM-N014

and discussed

the event with the

licensee.

The inspectors

found that once the actual

cause of the valve

failure was determined

during overhaul,

the licensee

took effective correction

actions.

However,

the inspectors

were concerned

that the immediate actions

taken

by the licensee

before the valve was returned to service in February

1993 appeared

to treat only the

symptoms of the problem

and not the root

cause.

Based

on the information available at the time, the inspectors

concluded that the licensee's

troubleshooting

appeared

to focus more

on

correcting observable

deficiencies rather than identifying the cause of the

failure in a controlled

and systematic

manner.

Without an obvious

component

failure, proper diagnosis of operational

HOV failures requires

consideration

of design basis capability.

However,

in this case,

the determination of

design

basis capability using diagnostic

i;est'...y

~:as not used prior to

returning the

MOV to service.

Although the lubrication of the stem appeared

marginal, this condition alone

could not have

caused

the torque switch to actuate

during the running portion

of the strok'e.

The licensee later determined that the effective stem friction

coefficient would have

had to be 0.7 for the

stem lubrication to have

caused

the torque switch trip.

Poor stem lubrication typically r'esults

in a friction

coefficient of 0.2 or slightly higher.

The inspectors

were concerned

that the

licensee failed. to verify that the immediate

proposed

root cause

was

consistent

with the available information.

In this case,

the inspectors

concluded that the mismatch

between

the failure mode

and the postulated

cause

should

have alerted the licensee that the actual root cause of the event

had

not been identified.

As

a result of superficial 'troubleshooting,.

MOV 2-FCV-37 was returned to

service in

a degraded

condition.

The inspectors

identified this

and

a similar

incident with HOV 1-LCV-109 (paragraph

1.3)

as two examples of a weakness

in

the licensee's

program for evaluating

nonconforming conditions prior to

returning equipment to service.

Within the review of the failures of MOVs 1-LCV-109 and 2-FCV-37, the

inspectors

observed

a tendency

on the part of the licensee

to curtail

troubleshooting efforts once the first discrepancy

was identified.

At this

point, the licensee

did not search for the presence

of other problems

nor

verify that the identified discrepancy,

by itself, could have

caused

the

observed failure.

The inspectors

were concerned

that despite

the licensee's

previous experience

with the failures of MOVs 2-FCV-37 and

2-LCV 109, there

had

been

no

programmatic'hanges

to incorporate

lessons

learned

in the control of

0

'

-13-

troubleshooting.

The licensee

acknowledged that the failures'ould probably

be handled

in

a similar manner if they were to occur today.

At the exit meeting,

the licensee

acknowledged

the inspectors'oncern

and

committed to procedural

revisions to assure

that design basis capability is

maintained

as

a condition for returning

HOVs to service,

The inspectors

found

the licensee's

commitment to be adequate.

1

0

ATTACHMENT

1

PERSONS

CONTACTED

1.1

L'icensee

Personnel

  • H. Hurgess,

Director, Technical

and Support Services

  • W. Crockett,

Manager,

Technical

and Support Services

H. Frauenheim,

Engineer,

Electrical Maintenance

  • R. Goel,

Engineer,

Nuclear Engineering

Services

  • C. Groff, Director, Technical

Services

  • K. Hubbard,

Engineer,

Regulatory Compliance

  • C. Lewis, Engineer,

Nuclear Quality Services / Site Quality Assurance

  • D. Hiklush, Manager,

Operation Services / Acting Plant Manager

  • R. Powers,

Manager,

Nuclear Quality Services

L. Pulley,

Engineer,

Nuclear Engineering

Services

  • J. Shoulders,

Director, Nuclear Engineering

Services

  • D. Taggart, Director, Nuclear Quality Services / Site Quality Assurance
  • A. Toy, Engineer,

Predictive Maintenance

  • M. Williamson, Engineer,

Electrical Maintenance

1.2

NRC Personnel

  • H. Hiller, Senior Resident

Inspector

  • Denotes those attending

the exit meeting

In addition to the personnel

listed above,

the inspectors

contacted

other

personnel

during this inspection.

2

EXIT MEETING

An exit meeting

was conducted

on June

10,

1994.

During this meeting,

the

inspectors

reviewed the

scope

and findings of the report.

The licensee

acknowledged

the inspection findings documented

in this report.

The licensee

did not identify as proprietary

any information provided to, or reviewed

by,

the inspectors.

1

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