ML16341G537

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Insp Repts 50-275-92-05 & 50-323/92-05 on 920204-0316.No Violations Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance Activities,Followup of Onsite Events, Open Items & LERs
ML16341G537
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 04/17/1992
From: Johnson P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341G538 List:
References
50-275-92-05, 50-275-92-5, 50-323-92-05, 50-323-92-5, NUDOCS 9205050132
Download: ML16341G537 (32)


See also: IR 05000275/1992005

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION

V

Report Nos:

50-275/92-05

and 50-323/92-05

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80

and

DPR-82

Licensee:

Pacific

Gas

and Electric Company

77 Beale Street,

Room 1451

San Franci sco,

Californi a 94106

Facility Name: Diablo Canyon Units

1

and

2

Inspected at:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

February

4 through March 16, 1992-

Inspectors:

H. Wong, Senior Resident

Inspector

M. Miller, Resident

Inspector

Approved by:

P.

H. Jo

son, Chief, Reactor Projects

Section

0(I7fgz

Date Signed

Summary:

Ins ection from Februar

4 throu

h March

16

1992

Re ort Nos. 50-275/92-05

and 50-323 92-05

A~1: lt

i

i

i

1dd

i

i

i

f

operations,

maintenance

and surveillance activities, followup of onsite

events,

open items,

and licensee

event reports

(LERs),

as well as selected

independent

inspection activities.

Inspection

Procedures

61726,

62703,

71707,

71710,

92701,

and

92703 were

used

as guidance

during this inspection.

Safet

Issues

Mana ement

S stem

(SIMS

Items:

None

Results:

General

Conclusions

on Stren ths

and Weaknesses:

Strengths-

The licensee

organizations

quickly responded

to the unexpected

outage of

Unit 1 after the reactor trip of March 6,

1992.

The meetings

conducted

appeared

effective in determining the actions

necessary

to determine

the

cause of the feedwater

pump loss

and reactor trip and in prioritizing

work, activities.

9205050l32

V204l7

PDR

ADOCK 05000275

8

PDR

0

The licensee

response

to

a quadrant

power tilt alarm during

a power

reduction in Unit 2 on February

16,

1992 was timely and accurate.

Licensee

personnel

discussed

the matter with Westinghouse re~sartatives

and carefully monitored core flux parameters

to assure that the reason

for the alarm was understood

and that core flux behavior

was

as expected.

Weaknesses-

During investigation of the problems with containment

fan cooler units

(CFCUs), it was identified that installation errors

had occurred

which

had

gone undetected

and

had

caused

the

CFCUs to be inoperable for a

significant period of time.

In addition,

a problem with reverse rotation

of a

CFCU had

been identified, but had not been considered

abnormal

and,

therefore,

no actions

were taken to correct the problem.

This appears

to

indicate

a need for greater attention to those

work activities considered

relatively simple

and the

need for more thorough

and timely corrective

actions for deficient conditions.

This matter is still being reviewed

and will be discussed

in

a future

inspection report.

Si nificant Safet

Matters:

None

Summar

of Violations:

None

'

en Items

Summar

1 new item opened,

7 items closed,

and

2 items remain open.

DETAILS

Persons

Contacted

Pacific

Gas

and Electric

Com

an

!

  • G. M. Rueger,

Senior Vice President

and General

Manager,

Nuclear

Power

Generation

Business

Unit

J.

D. Townsend,

Vice President

and Plant Manager,

Diablo Canyon

Operations

  • W. H. Fujimoto, Vice President,

Nuclear Technical

Services

  • D. B. Miklush, Manager,

Operations

Services

  • M. J. Angus,

Manager,

Technical

Services

  • B. W. Giffin, Manager,

Maintenance

Services

  • W. G. Crockett,

Manager,

Support Services

J.

E. Molden, Instrumentation

and Controls Director

  • W. D. Barkhuff, Quality Control Director

R. P.

Powers,

Mechanical

Maintenance Director

  • D. A. Taggart, Quality Performance

and Assessment

Director

  • T. L. Grebel,

Regulatory Compliance Supervisor

H. J. Phillips, Electrical Maintenance

Director

  • R. C. Anderson,

Manager,

Nuclear Engineering

and Construction

Services

  • M. R. Tresler,

Project Engineer,

Nuclear Engineering

and Construction

Services

J. A. Shoulders,

Onsite Project Engineering

Group Manager

S. R. Fridley, Operations

Director

R.

Gray, Radiation Protection Director

  • J. J. Griffin, Senior Engineer,

Regulatory Compliance

J.

V. Boots,

Chemistry Director

  • 0. B. Hoch, Manager,

Nuclear Safety

and Regulatory Affairs

  • T. A. Moulia, Assistant to Vice President

Diablo Canyon Operations

  • C. A. Dougherty, Quality Assurance

Senior Supervisor

  • J. E. Tompkins, Nuclear Safety

and Regulatory Affairs Director

  • R. C. Russell,

Nuclear Safety

and Regulatory Affairs

  • B. A. Dettman, Director Nuclear Operations

and Support,

and Assistant to

Senior Vice President

Nuclear

Re ulator

Commission

  • S. A. Richards,

Chief, Reactor Projects

Branch,

Region

V

  • Denotes those attending the exit interview.

The inspectors

interviewed several

other licensee

employees

including

shift supervisors,

shift foremen

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

and quality

assurance

personnel.

2.

0 erational

Status of Diablo Can

on Units

1

and

2

During the inspection period, Unit 1 operated

at

lOOX power, except

between

March

6 and 10,

1992

when

a plant trip occurred

due to the loss of

a main feedwater

pump.

This event is discussed

in paragraph

4.a belo'w.

Unit 2 operated essentially

at 100K power,

except for February

16-17

,

and March 14-15,

1992.

On February 16-17, Unit 2 reduced

power to

approximately

50K for condenser

cleaning.

On March 14-15, Unit 2 reduced

power to 55K to install

a wiring change to the power supply eir cd'ts to

speed

sensors

of both main feedwater

pumps.

On February

16,

1992, at 10:30 p.m.

when Unit 2 reduced

power to 50K,,

a

quadrant

power tilt ratio alarm was received.

The power tilt ratio

increased

to 1.048 at about 1:30 a.m.

on February

17

and then steadily

decreased.

The licensee,

in consultation with Westinghouse,

determined

that the power tilt was

a result of slightly different efficiencies of

the secondary

loops, resulting in uneven

power distribution in the core.

This causes

about

a 0.5X power tilt during normal

100% power operation,

which is within the requirements

of Technical Specifications.

The

decrease

in power resulted

in an uneven

xenon transient in the core,

which exaggerated

the power tilt.

The licensee

decreased

power below 505

as required

by Technical Specifications

and the power tilt decreased

during power ascension

and stayed within Technical Specification limits.

On March 14,

1992, Unit 2 again reduced

power

and

a similar power tilt

occurred

and

exceeded

the Technical Specifications limit of 1.02 at 11:30

p.m.

The tilt decreased

to less

than 1.02 at 1:05 p.m.

on March 15.

During this time, the licensee

reduced

the high flux trip points to 94K

as required

by Technical Specifications.

0 erational

Safet

Verification (71707)

a.

General

During the inspection period, the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations

of those activities

were conducted

on

a daily, weekly or monthly basis.

On

a daily basis,

the inspectors

observed

control

room activities to

verify compliance with selected

Limiting Conditions for Operations

(LCOs)

as prescribed

in the facility Technical Specifications

(TS).

Logs, instrumentation,

recorder traces,

and other operational

records

were examined to obtain information on plant conditions

and

to evaluate

trends.

This operational

information was then evaluated

to determine if regulatory requirements

were satisfied.

Shift

turnovers

were observed

on

a sample basis to verify that all

pertinent information on plant status

was relayed to the oncoming

crew.

During each

week, the inspectors

toured the accessible

areas

of the facility to observe

the following:

(a)

General

plant

and equipment conditions

(b)

Fire hazards

and fire fighting equipment

(c)

Conduct of selected

activities for compliance with the

licensee's

administrative controls

and approved

procedures

(d)

Interiors of electrical

and control panels

(e)

Plant housekeeping

and cleanliness

(f)

Engineered

safety feature

equipment

alignment

and conditions

(g)

Storage of pressurized

gas bottles

0

b.

The inspectors

talked with operators

in the control

room and other

plant personnel.

The discussions

centered

on pertinent '-TVpfcs of

general

plant conditions,

procedures,

security, training,

and other

aspects

of the work activities.

Radiolo ical Protection

c ~

The inspectors periodically observed radiological protection

practices

to determine

whether the licensee's

program

was being

implemented

in conformance with facility policies

and procedures

and

in compliance with regulatory requirements.

The inspectors verified

that health physics supervisors

and professionals

conducted

frequent

plant tours to observe activities in progress

and were aware of

significant plant activities, particularly those related to

radiological conditions

and/or challenges.

ALARA considerations

were

found 'to be

an integral part of each

RWP (Radiation

Work Permit).

Ph sical Securit

Security activities were observed for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative

procedures

including vehicle

and personnel

access

screening,

personnel

badging, site security force manning,

compensatory

measures,

and protective

and vital area integrity.

Exterior lighting was checked

during backshift inspections.

No violations or deviations

were identified.

4.

Onsite Event Followu

93702

a ~

Unit

1 Loss of Main Feedwater

Pum

and Reactor Tri

On March 6,

1992 at approximately 10:30

am, with Unit 1 operating at

lOOX power,

main feedwater

pump l-l tripped

on overspeed

due to the

failure of the power supply to the speed

sensors

of the

pump.

At

the time of the event,

licensee

personnel

were working on

a lube oil

cooler for the

pump which was adjacent to the

speed

sensor

power

supply cabinet.

On the loss of the power supply to the speed

sensors

of feedwater

pump 1-1

and the failure of the transfer to the

power supply of the other feedwater

pump, the sensed

speed of pump

l-l went to zero

and the

pump control

system

attempted

to increase

pump speed.

This led to feedwater

pump 1-1 reaching

the overspeed

trip setpoint of approximately

6400 rpm.

The other feedwater

pump

decreased

its speed

due to the increased

speed of feedwater

pump

l-l.

Control

room operators initially reduced turbine load in

response

to an expected

main feedwater

pump loss.

During the load

reduction,

feedwater

pump 1-1 tripped.

On the loss of feedwater

pump 1-1, control

room operators initiated

a rapid reduction of turbine load

and had lowered load to

approximately

50K, with the '40% steam

dump valves (to cdmhhser)

modulating

open

as designed.

However, this

was not enough to

prevent

a reactor trip on low-low steam generator

water level

approximately

one

and one-half minutes after the trip of feedwater

pump 1-1.

Contributing to the difficulty in recovering

steam

generator

water level

was the fact that the operating feedwater

pump

(1-2)

had reduced its speed

due to the increased

speed

and flow from

'he

overspeeding

feedwater

pump 1-1.

Plant response

to the reactor trip was for the most part

uncomplicated

and there

was

no initiation of safety injection.

The

issues

requiring resolution were:

(1) the identification of the

cause of the

speed

sensor

power supply failure to feedwater

pump

1-1; (2) determination of the cause of three

10K steam

dump valves

(to atmosphere)

opening after the reactor trip; and (3)

determination of the cause of the start of diesel

generator

1-1

approximately

32 seconds

after the reactor trip.

These

issues

are

discussed

below.

1)

The cause of the power supply failure of the

speed

sensors

to

feedwater

pump l-l was identified to be the opening of

a

fusible link in an inverter.

The cause of the link opening

was

not determined,

but was possibly due to vibration when

a

portion of platform grating adjacent to the power supply

cabinet

was dropped into position, or due to overheating

due to

the high ambient temperature.

The opening of the fusible link

caused

excessive

current to be drawn

and the input fuses

were

blown resulting in the failure of the power supply.

A single

power supply provides

power to both speed

sensors

of a

feedwater

pump.

A transfer

scheme

from the other feedwater

pump power supply was intended to provide redundancy.

The failure to transfer to the power supply of feedwater

pump

1-2 was found by the licensee

to be due to

a small plastic

shaving discovered

between relay contacts.

This shaving

appeared

to be from the terminal insulation

on the relay and

appears

to have fallen into the contact

area during

installation of the wiring.

A new inverter was installed for feedwater

pump 1-1

and relays

and fusible links were inspected

in feedwater

pumps

1-1

and

1-2.

The primary corrective action to prevent another

loss of

power supply, possibly resulting in a similar event,

was

a

wiring change to provide independent

power supplies for the two

speed

sensors

on each feedwater

pump.

This change

provided for

one

speed

sensor

on each

pump to be powered from an inverter,

with a transfer

scheme to the other feedwater

pump power supply

if necessary

(same

as in the past configuration).

In addition,

the other

speed

sensor

on each

pump would be powered

by other

AC sources.

This change

in power supply configuration

was

installed

on the Unit

1 feedwater

pumps prior to the restart of

Unit 1

and

was also completed

on the Unit 2 feedwater

pumps

during

a power reduction

on March 14-15,

1992.

The opening of three of the four lOX steam

dump valves

was

found to be due to the sensitivity of the steam

dump valve

control

system.

Volume boosters

had

been

added to the

pneumatic portion of the control

system during the last outage,

but the boosters

had not been tested to assure

that adverse

effects were not present

during transient conditions.

During the March 6,

1992 event,

the steam

dump control system

switched from the load reject

mode of control (during the

manual

load reduction) to the steam pressure

mode of control,

(after the reactor trip).

In the load reject

mode of control

the

no-demand

pressure

in the actuator lines is 0.5 psig

and in

the steam pressure

control

mode the no-demand

pressure

in the

actuator lines is 3.0 psig.

In the switch from load reject to

steam pressure

mode of control,

a pressure

perturbation

was

started

(on the change

from 0.5 to 3.0 psig) in the actuator

lines which was amplified by the recently

added

volume

boosters.

Because

the

steam

dump valves will begin to open at

approximately 3.5 psig, this caused

the slight opening of the

10K steam

dump valves during the event.

This was demonstrated

in subsequent

testing of the steam

dump valve control system.

The opening of three

10K steam

dump valves rather than four was

because

one valve

(PCV-22, the one which had not opened

during

the event)

was found to be set at

a lower no-demand

pressure

(1.0 psi g) rather than at the intended 3.0 psig.

If necessary,

control

room operators

could have

opened or

closed

the

10K steam

dump valves using manual

switches

in the

control room.

By March 19,

1992,

adjustments

had

been

made to

all of the

steam

dump valves in Units

1 and

2 to tune out the

pressure

perturbation.

The start of diesel

generator l-l was

due to the relatively

light loading of its associated

bus

(Bus

H) and the fact that

its voltage drops slower than the other two safety-related

4160

V buses.

This causes

the other

buses

to load first onto

the startup

bus which momentarily brings

down the voltage of

the startup

bus.

The drop

and recovery of startup

bus voltage

was sufficiently long to initiate the start of diesel

generator

1-1 without loading it onto Bus

H.

Bus

H successfully

transferred

from the auxiliary transformer to the startup

bus

in this event.

This condition had

been

seen

before at Diablo

Canyon

and

was evaluated

in

NCR DC2-88-EM-N095.

The licensee

concluded

in this

NCR that

an unnecessary

diesel

generator

start

was considered

an acceptable

occurrence

when considering

the ineffectiveness

and cost of

a possible

design

change.

Because

a design

change

could possibly prevent

a necessary

diesel

generator start,

licensee

management

considers

the start

of a diesel

generator

when it may not be needed

to be less of

a

concern

than the failure of a diesel

generator to start

when

required.

Other activities accomplished

during the unit outage

included

inspectio~

and repair of the backdraft

dampers

associated

with the

Unit 1 containment fan cooler units

(CFCUs).

The

CFCU work included post-maintenance

testing after completion of

all work to assure

there

was

no reverse rotation of the fans

when

shut down.

The licensee

also identified

a cracked

packing gland

flange

on

a manual drain valve (513)

on the pressurizer

spray line.

The manual drain valve had wedges installed

as

a temporary measure

to retain pressure

on the packing by transmitting force through the

packing follower ring.

The valve is also normally closed with

system pressure

under the valve disc.

The plant resumed

operation

on March 9, 1992, after repairs

and work

activities were completed,

and

lOOX power was reached

on March 10,

1992.

The reactor trip event is described

in

NCR DC1-92-EM-N010,

and

a Licensee

Event Report will be submitted to the

NRC.

Inspector Findings-

1.

The inspector

observed

the response

to this event several

minutes after the indication of feedwater

pump problems.

Control

room operators

responded

appropriately

and utilized

proper procedures.

Control

room instructions

and guidance

were

clear

and concise.

Sufficient management

and licensed

personnel

were present

to provide assistance

during the event.

2.

The inspector

observed

several

management

meetings

which were

conducted following the event.

These

meetings

were to evaluate

the cause

of the feedwater

pump trip and reactor trip and

determine corrective actions.

Meetings

were also conducted

to

determine

the scope

and priority of work to be accomplished

during this unexpected

outage.

These meetings

were successful

in making licensee

management

aware of the root cause

determinations,

obtaining, agreement

on necessary

corrective

actions,

and in coordinating

and prioritizing work activities.

3.

The inspector

reviewed the past history of feedwater

pump

-inverter failures.

This review indicated that there

have

been

several

inverter failures in the past which appear to be

indicative of

a long standing

problem.

The inspector will

continue to review the inverter history during the next

inspection period.

b.

Diesel

Generator

1-3 Test with Cardox

S stem Initiation

On March ll, 1992, during routine surveillance

testing of diesel

generator

1-3, the carbon dioxide fire suppression

(Cardox)

system

actuated

shortly after the diesel

generator

started.

Because

the

actuation of the carbon dioxide system

causes

roll-down doors to

shut

and thus deprive the generator

of cooling, operators

immediately shut

down the diesel,

opened

the roll-down doors,

and

started

troubleshooting

the failure.

The licensee

also tested

the

other diesel

generators

in both units within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to confirm

operability as required

by Technical Specifications.

The licensee

0

was unable to confirm the cause of the failure and has sent

a

circuit card from the carbon dioxide system to the vendor for root

cause

analysis.

The licensee's

determination of the ca~67 this

failure and whether it is considered

a valid failure of the diesel

generator will be reviewed in

a subsequent

inspection

(Followup Item

50-275/92-05-01).

No violations or deviations

were identified.

5.

Maintenance

62703)

The inspectors

observed

portions of, and reviewed records

on, selected

maintenance

activities to assure

compliance with approved

procedures,

Technical Specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified maintenance

activities were

performed

by qualified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and replacement

parts

were appropriately

certified.

These activities included:

Work Order R0091799,

Unit 2

RHR Pump 2-2 Motor Oil Sampling

Work Order C0096975,

Unit

1

CFCU 1-2 Backdraft

Oamper Repair

Work Order C0096844,

Unit 2 Inspection

and Repair of FCV-372

(AFW

Check Valve)

Work Order C0096503,

Unit

1 Investigation

and Repair of

DG 1-2

Engine Temperature

Indicator

Work Order C0097368,

Unit 2 Inspection

and Cleaning of Main

Condenser

On February

25,

1992, the inspector

observed oil sampling of the

Unit 2 residual

heat

removal

(RHR)

pump motor 2-2.

The associated

work order

(WO R0091799)

specified that the sampling

be performed in

accordance

with maintenance

procedure

MP M-56.7, Steps 7.l.a through

7.1.g.

Included in these

steps

was

a note that the "oil samples

should

be taken while the equipment is operating or shortly after

the equipment is shutdown."

The person taking the oil sample

was

unsure of how the note

was to be interpreted

because

there were

no

specific steps

in the work order calling for the operation of the

RHR pump.

The

RHR pump had not been recently run prior to drawing

the oil samples.

The inspector

discussed

the intent of the work order

and maintenance

procedure with an electrical

maintenance

manager

and the sponsor of

the procedure.

The conclusion

was that the intent was to obtain

an

oil sample after

a pump run, but it was recognized that the

procedure,and

work order were inconsistent

and that appropriate

scheduling

guidance

had not been

communicated

to properly coordinate

the

pump run

and drawing of the oil samples.

Licensee

management

stated that the procedure

would be clarified, particularly Appendix

8.2,

and that scheduling

guidance

would be provided to properly

coordinate

the oil sampling.

In addition,

guidance

would be

provided to maintenance

personnel

to assure

that work orders

and

procedures

are understood prior to continuing work activities.

'o

violations or deviations

were identified.

6.

Surveillance

61726)

a ~

Observations

By direct observation

and record review of selected

surveillance

testing,

the inspectors

checked

compliance with TS requirements

and

plant procedures.

The inspectors verified that test equipment

was

calibrated,

and that test results

met acceptance

criteria or were

appropriately dispositioned.

These tests

included:

STP

M-9A

Unit 1 Monthly DG Test

(DG 1-2)

STP

M-8A2 Unit 1 Emergency Air Lock Leak Test

STP

V-3R5 Unit

1 Stroke Test of FCV-95

(AFW Steam Admission

Valve)

STP

N-16C Unit 2 Train

A Slave Relay Test

STP

M-8A1 Unit

1 Personnel

Air Lock Leak Test

b.

During the testing of the steam

admission

valve (FCV-95) to the Unit

1 turbine-driven auxiliary feedwater

pump

on March 10,

1992,

licensee

personnel

identified that on the closure of valve FCV-95

there

was

a larger than expected

amount of stem bending.

Stem

bending in the past

had

been

viewed

as

one indicator that

a higher

force would be required to open the valve the next time.

Licensee

engineering

personnel

concluded that

FCV-95 should

be restroked

and

monitored with the expectation that the bending stress

would be

reduced.

The valve opened successfully

(11.89

amps for pullout);

however,

on closing,

licensee

personnel

noted

even higher bending

stresses

than previously seen

and also

a deeper

seating position

than previously.

This valve position

was also considered

undesirable

in that both conditions indicated

a higher force would

be required to open the valve.

The valve was cycled

open again, with 15.65

amps

measured

to open

the valve.

On closure of the valve, while an even deeper

seat

position

was noted,

only slight stem bending occurred.

This was

considered

acceptable

by licensee

engineering

personnel.

The next

test of FCV-95 occurred

on March 17,

1992

and resulted

in successful

opening of the valve

and approximately

15.5

amps

on pullout.

The licensee's

engineering

organization

(NECS)

has

been evaluating

the data obtained during the testing of FCV-95.

In

a memorandum

dated

March 5, 1992,

NECS has

proposed that the weekly testing of

FCV-95 in Unit

1 be extended to every two weeks for March

and April

0

and then to monthly beginning in Nay 1992,

due to the identification

of a reliable indicator of the potential for high pullout force

(stem position),

and to a lesser

degree

the reliability'Ut'tem

bending

as

an indicator.

These indicators

have

been correlated,

with stem position being more consistent.

An additional

reason for

reducing the testing frequency is the gearing

changeout

done after

the

December

24,

1991, failure of FCV-95 to open.

This change

has

increased

the opening capability of the operator

such that there is

added

assurance

that the valve will open

when intended.

NECS has

recommended

that thermography

and certain diagnostic

equipment

no

longer

be required during valve testing

as the information gathered

by these

instruments

is no longer of use.

Further,

NECS indicates that the valve has

begun to show

evidence of wear during the weekly testing.

There

has

been

a

gradual

increase

in the pullout current to open the valve and

a

decrease

in the seating thrust in closing the valve.

This is

attributed to greater

stem friction as the valve is cycled

and is

postulated

by NECS to be due to the gradual

reduction of lubrication

on the stem threads.

No

7.

En

The March 5,

1992

memorandum

also

recommends

that

FCV-95 in Unit 2

be instrumented

to monitor only stem position rather than the full

set of instrumentation

now provided

on the Unit

1 valve.

Based

on

a review of the licensee's

data correlating

stem position

and pullout current,

the gearing

changeout

made,

and the fact that

Unit 2 opening current data

are relatively consistent

(6.2 - 12.5

amps),

the licensee's

proposal

appears

appropriate.

violations or deviations

were identified.

ineered

Safet

Feature Verification

71710)

During the inspection period, selected

portions of the auxiliary

feedwater

system for Units

1 and

2 were inspected

to verify that system

configuration,

equipment condition, valve

and electrical

lineups,

and

local breaker positions

were in accordance

with plant drawings

and

Technical Specifications.

violations or deviations

were identified.

8.

0 en Item Followu

92703

ao

Unresolved

Item 50-275/91-01-01:

Licensee

A

endix

R Audit

Open)

In December

1990,

the Nuclear Operations

Support

(NOS) group

performed

an audit of safe

shutdown

systems

and procedures.

This

audit was described

in

a memorandum to the plant manager

dated

January

29, 1991.

Followup by the

NRC inspector is described

below.

Licensee corrective actions to date

and planned corrective actions

are included with each

issue.

10

After completion of design

basis

documentation

in the areas

of

electrical circuitry and safe

shutdown methodology,

which are

estimated

to be completed

around

June

1992,

the license~Tans

to

start the second

phase of the Appendix

R validation budgeted

under

BLI No. 453.

This will include validation of the safe

shutdown time

line; emergency lighting locations,

including availability of

emergency lighting during outages

(formerly NRC Open Item 91-03-03,

closed

in this report);

equipment repair procedures;

and

use of

auxiliary equipment.

As

a result of the

1990

NOS audit, the licensee identified improper

implementation of configuration control in the following areas:

o

Emergency

Procedures

- Procedures

are currently being reviewed

for agreement

with design basis

documentation.

o

Combustible

Loading - The licensee is evaluating the need for

control over small (less

than

one percent)

changes

in the

combustible loading.

o

Safe

Shutdown Circuit Analysis - The licensee

is completing

validation of the original safe

shutdown circuit analysis.

Several

issues

regarding circuit separation

have

been

identified, including the inadequate

separation

in the Unit 2

reactor trip switchgear

room

( Inspection

Report 50-275/92-01,

paragraph 5.b.),

inadequate

protection of cables

in the

Unit 2 diesel

generator

room corridor,

and inadequate

separation

of circuits in containment,

which the licensee

plans.

to report in a future LER.

Additional specific concerns

being followed by the

NRC are listed

below:

o

Remote

Shutdown

Panel - The licensee

stated that surveillance

testing of hot shutdown

panel

mechanical

components

would be in

place

by December

31,

1991.

Most of this testing is in place;

however, testing for some valves

has not been

implemented..

The

licensee

stated that testing would be implemented

by July 15,

1992.

For the testing which has

been

implemented,

no failures

have

been

noted to date.

o

Operator Training - The licensee

documented

that the training

for procedure

M-10, "Fire Protection of Safe

Shutdown

Equipment,"

has occurred

and

has

now been included in biennial

review for operator requalification training.

Therefore, this

specific concern is closed.

o

Heat Trace - Heat tracing circuity for the Appendix

R emergency

boration flow path

was not reviewed to validate appropriate

circuit separation.

The circuity runs through various

areas

of

the auxiliary building,

and

may not be properly separated.

The

licensee

agreed to address

this issue.

The licensee

stated

that boration

can

be accomplished

using the

RWST for all fire

areas.

Therefore,

redundant capability is available.

11

o

Failure Trending of Emergency Lighting Units - Although the

licensee

now has the capability to trend failures of individual

lighting units, there

has

been

no assigned

responsibi I'ity for

this function.

o

Equipment Operability Evaluations - Revision

6 of Justification

for Continued Operation

(JCO) 90-17 addressed

inoperability of

the positive displacement

charging

pump, which would be used

for a safe

shutdown during

a fire in the centrifugal charging

pump room.

The

JCO did not specifically identify the safe

shutdown

method nor its associated

circuit analysis to be used

as

compensatory

measures.

The licensee

agreed that the

JCO

could have

been written more clearly.

The licensee

plans to

rewrite the

JCO by mid-April 1992

and will discuss

the issues

at that time.

Since the licensee

stated that fire protection

compensatory

measures

are in place in the centrifugal charging

pump room, including suppression,

detection,

and hourly fire

watches,

the safety significance of this issue is low.

o

Root Cause - The preliminary 1991 audit conclusion for these

discrepancies

involved

a disconnect

between

NECS

and the actual

plant configuration

and procedures.

The licensee

stated

during

this report period that that root cause still appeared

to be

valid.

b.

Followu

Item 50-275/92-01-01:

Removal of Conduit Bracket Durin

Unit

Refuelin

Outa

e

C ose

This issue

involved the discovery

by the

NRC inspector of a pair of

conduit brackets

which had

been

removed during the Unit 1 refueling

outage

in 1991

and

had not been reinstalled.

The licensee initiated

QE Q0009474 to document the corrective actions taken.

These actions

included reinstallation of the brackets,

discussions

with the

personnel

involved in the incident,

and the initiation of a training

improvement plan specific to this event which will be included in

the quarterly maintenance

training.

Based

on these actions, this

item is closed.

c ~

Followu

Item 50-275/92-01-02:

Timin

of Inde endent Verification

Durin

Surveillance Testin

C osed

This issue

involved the inspector's

observation that personnel

did

not clearly understand

the appropriate

timing of the performance of

independent verification during surveillance testing.

The licensee

initiated

QE Q0009487 to document the issue

and the required

corrective actions.

These

actions

include the revision of selected

surveillance

procedures;

revision of procedure

NPAP C-104,

Independent

Verification of Operating Activities, to clarify the

intent of the independent verification during surveillance testing;

development of

a checklist to be used during interdepartmental

reviews of surveillance testing procedures;

and revision of the

Operations

Policy documents

to place guidance

regarding

independent

verification in the proper location.

Based

on these actions, this

. item is closed.

0

12

Unresolved

Item 50-275/91-24-01:

Floodin

of Com onent Coolin

Water

CCW

Heat

Exchan er

Room

C ose

On August 2, 1991, during preparations for a routine cleaning of the

CCW heat exchanger,

maintenance

workers failed to properly follow

the work order clearance

instructions.

This resulted in flooding of

the Unit

1

CCW heat exchanger

room.

The work order required

that the auxiliary saltwater

system inlet valve to the heat

exchanger

be gagged before'he

heat exchanger

manway was opened.

Instead,

with the inlet valve shut but not gagged,

workers

opened

the manway,

entered

and exited the heat exchanger,

and then

attempted to gag the valve shut.

The workers thought the work order

steps

were in the wrong sequence.

The manway

was left open.

During

the attempt to gag the valve, the valve opened,

flooding the heat

exchanger

area.

This could have

caused

a significant personnel

safety hazard

had

an individual been in the heat exchanger

when the

inlet valve opened.

The licensee

determined that there

was only minor significance to

plant safety,

since the redundant

safety train was available.

The licensee

determined that the root cause

of the problem was

personal

error, in that the instructions in the work order were not

followed in sequence.

Corrective actions

taken include issuance

of

two maintenance

bulletins; mandatory discussion

with all foremen

and

appropriate

journeymen

on the importance of reviewing clearances

to

ensure isolation of energy sources

from the work area,

and

on the

importance of constructive

and timely feedback to Work Planning

when

a work order is not correct;

and counseling of the specific

individuals involved.

The licensee

has also identified other

prudent,

peripheral

actions.

Based

on the corrective actions, this item is closed.

Followu

Item 50-275/91-09-03:

Normal Li htin

and Public Address

PA

S stem

Power

Su

Closed

During the March 7, 1991, loss of offsite power event,

the Unit 1

normal lighting and

PA systems

became

inoperable.

In addition,

emergency lighting in containment

was unavailable

due to

maintenance.

The

NRC Augmented Inspection

Team (AIT) identified

a

need for the licensee to investigate

the adequacy of lighting and

communications.

The licensee

had earlier identified (in December

1989) that emergency

lighting for safe

shutdown

may not be adequate

in all areas

of the

plant.

Additional walkdowns were performed after the March

7 event.

Investigation

and corrective action is being implemented

under

a

budget line item for fire protection safe

shutdown,

discussed

in

this report.

As interim compensatory

measures,

portable lighting

has

been provided to operators.

Further followup of the lighting

issue will be followed under Followup Item 50-275/91-01-01.

13

The AIT concern for the failure of the

PA system

was reviewed,

including the containment

evacuation

alarm function.

The licensee

determined that the

PA system,

by design, is not safety-Ptlated,

and

that placing the

PA system

on vital power or on

an uninterruptable

power supply was not

a warranted

expenditure

in comparison with

other projects providing more safety benefit.

Based

on the

above

discussion

and inclusion of the lighting issue in Followup Item

50-275/91-01-01,

this item is closed.

Unresolved

Item 50-275/91-27-01:

Containment Air Lock Leak Tester-

Unct

C ose

The issues

remaining

open regarding this followup item were:

(1)

whether the non-quality classification of the automatic

leak tester

was appropriate

even though it is used to satisfy Technical

Specifications

requirements,

and (2) whether

a revision to the current

training program

was needed.

The non-quality classification of the tester

appears

appropriate

in

that the licensee's g-list document specifies that testing devices

are not classified,

but are covered in the

gA program to maintain

accuracy within necessary

limits.

This is consistent

with 10 CFR Part 50, Appendix B, Criterion XII, Control of Measuring

and Test

Equipment.

A revision to the training program regarding the air lock had

been

issued just prior to the event.

It had

been considered

that the

recently revised training was sufficient to cover the event.

Based

on further questions

by the inspector,

the licensee

issued Training

Improvement

Proposal

k'2300 to emphasize

the

need to perform

a

manual test if the automatic tester fails.

This training will be

included in upcoming licensed

and non-licensed

operator training

and

also will be included in the next revision of the training lesson

guides.

Based

on this, this unresolved

item is closed.

Unresolved

Item 50-275/91-20-02:

Missed Surveillance Test

Closed

This issue

was described

in Licensee

Event Report 50-275/91-012-00

and

was reviewed

and closed in Inspection

Report 50- 275/91-40.

Therefore, this unresolved

item is closed.

Followu

Item 50-275/92-17-02:

Site Strate

for Personnel

rrors

0 en

This issue

involved the inspector's

observation that between

August

and October

1991 there

appeared

to be

a high number of noteworthy

personnel

error events.

The licensee initiated

a human error

reduction plan which includes letters

and meetings to express

management's

expectations for human performance,

review training

regarding

independent verification and provide recommendations,

develop

a training video, provide

a policy on pre-job briefings,

and

develop

a tracking mechanism for human errors contained

in HCRs .and

gEs for review with department directors.

This plan is described

in

Diablo Canyon Objective 3000.01/017.1.

0

14

Most items are currently on schedule,

with the only item behind

schedule

being the development

of an independent verification

training video tape.

This tape is scheduled

to be comPB;ed

by the

end of March 1992.

9.

Exit

One March 18,

1992,

several

personnel

errors occurred in Unit 2 which

resulted

in the isolation of the number

1 seal leakoff line of

reactor coolant

pump 2-4 for approximately

63 minutes.

This event

was initiated during troubleshooting of the leakoff line flow

transmitter.

While the licensee

is reviewing this event,

preliminary information indicates

the following errors occurred:

Inadequate tai lboard discussion for the involved parties to

understand

the scope of the work being performed.

Assumption of shared responsibilities for the troubleshooting

activities;

however, there

was

no communication of who was

responsible for what aspects

of the job.

Communications

with control

room personnel

during the work did

not develop

an understanding

of the actions actually being

performed.

An alarm for high number

2 seal leakoff received

in the control

room should

have alerted control

room operators

of the

incorrect valve alignment.

It appears

that

pump performance

parameters

(seal leakoff

temperatures,

seal differential pressure,

and

pump vibration

measurements)

returned to normal after the event

and Westinghouse

is

being consulted to determine

whether

any significant

pump

degradation

occurred.

These

personnel

errors

are significant in that

a number of barriers

failed to detect the incorrect valve alignment.

Based

on errors

evident during this event

and pending the licensee's

evaluation of

the root causes

and whether additional corrective actions

are

appropriate,

this followup item will remain open.

On March 19,

1992,

an exit meeting

was conducted with the licensee's

representatives

identified in Paragraph

1.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.

g