ML16340A408

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IE Insp Rept 50-275/79-04 on 790201-23.No Noncompliance Noted.Major Areas Inspected:Preoperational Testing,Plant Tour,Witnessing of Sys Verification Testing & Other Testing in Progress
ML16340A408
Person / Time
Site: Diablo Canyon 
Issue date: 03/06/1979
From: Johnston G, Sternberg D, Thomas Young
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16340A409 List:
References
50-275-79-04, 50-275-79-4, NUDOCS 7904190192
Download: ML16340A408 (8)


See also: IR 05000275/1979004

Text

~g

Repor t No

50 275/79

04

Docket

No. 50 27

U ~

ST

NUCLEAR REGULATORY COMMISSION

OFFICE

OF INSPECTION AND ENFORCEMENT

REGION V

License

No.

Gafaduarda

Group

Licensee:

Pacific

Gas

and Electric ComPany

77 Beale Street

San Francisco

'California

94106

FaciIity

Name ~

,

Diablo Canyon Unit

1

Inspection at:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

co

u ted;

, Fe rualy 1-'23,

1979

a

Inspectors:

T.

Youn

Jr.,

R

id nt

ctor I

6.

W. ~+hnsto

Reactor Inspector

spector

Date

igned

Da e Signed

ate Signed

Approved By:

Summary:

D.

l1. Sternberg,

Chs&g Realtor

Prospects

Sect

Reactor Operations

and Nuclear Support Branch

ion

1

ate Signed

Ins ection on Februar

1-23,

1979

Re ort No. 50-275 79-04

p

tp

1

ig.s

tour, witnessing of system verification testing

and other testing in

progress,

preoperational

test program controls

and quality assurance

for

preoperational

testing,

and review of special

report (CILRT).

This

inspection involved 82 inspector-hours

onsite

by one

NRC resident

inspector,

and

12 inspector-hours

onsite

by one regional

NRC inspector.

Results:

No items of noncompliance

or deviations

were identified.

RV Form ?19

(2

>904>so /9~

4

DETAILS

l.

Persons

Contacted

  • R. D. Ramsay,

Plant Superintendent

R.

D. Etzler, Project Superintendent

  • N. H. Horem, Resident Startup

Engineer

N.

E. Leppke,

gA Supervisor

  • J. S.

Diamonon,

gC Supervisor

R. Patterson,

Supervisor of Operations

  • D. A. Backeons,

Supervisor of Naintenance

  • J. N. Gisclon,

Power Plant Engineer

  • C. N. Seward,

gA Engineer

  • J.

D. Shiffer, Assistant to the Plant Superintendent

The inspector also talked with and interviewed

a number of

other'icensee

employees,

including members of general

construction,

the

operations staff and

gA organization

personnel.

  • Denotes

those attending

the exit interview.

2.

Preo erational

Testin

a.

Portions of the following tests

were witnessed

by the inspector:

21.2 A-1

Reflush Diesel

Fuel Oil System Lines

16.2 A-1

Reflush Primary Water Line to

PRT

\\

24.3

Purge

Gaseous

Radwaste

System

37.10

Steam

Dump Performance

Demonstration

37.4 A-1

Reactor

Coolant System Thermal

Expansion Test

b.

While witnessing the above testing (in some tests

only parts

of the tests

were being performed or redone),

the inspector

verified that the procedures

were technically adequate;

the

latest revisions

were available

and approved;

the overall

crew

performance

was adequate

and, in the case of completed tests,

the acceptance

criteria were met.

Administrative controls for

design

change

and documentation

were followed.

Ho items of noncompliance

or deviations

were identified.

Plant Tour

The inspector walked through various areas of the plant on

a weekly

basis

to observe activities in progress;

to inspect the general

state of cleanliness,

housekeeping

and adherence

to fire protection

rules; to check the proper approval of "tlan on the line, Caution

and Clearance"

tags

on equipment;

and to review with operators

the

status of various

systems

in the plant.

The inspector

noted that the status of the systems

and the house-

keeping

appeared

consistent with construction activities.

Within

the past

two weeks, extra personnel

have

been assigned

to the

cleanup

crews

and housekeeping

is improving.

No items of noncompliance

or deviations

were identified.

S stem Verification Testin

SVT

SVT (Mini Hot Function Testing)

was started

on February

20,

1979

and is scheduled

to continue approximately thirty days.

During

this period,

the plant is to be brought up to operati ng temper-

atures

and pressures.

All subsystems

and/or components

which have

had corrective maintenance

and/or modifications will be retested

to

assure their operational

status.

At the conclusion of the in-

spection,

the primary system

(RCS) temperature

had

been raised to

120'

with a pressure

of 50 PSIG and

RCS venting was in process.

Ho items of noncompliance

or deviations

were identified.

Prep erational

Test Pro ram Controls

The inspector verified by record review and/or observation

that (a)

jurisdictional controls were being observed for system turnover,

(b) tagging

was being accomplished

consistent with jurisdictional

controls of the administrative

procedures

and (c) controls were

being observed prior to and subsequent

to testing.

A schedule for

preoperational

testing is being maintained

and updated

when necessary.

Ho items of noncompliance

or deviations

were identified.

Prep erational Testin

A

The inspector

examined all

gA audit reports of preoperational

testing audits

conducted within the last three months.

The audits

were conducted

in accordance

with approved

procedures

and corrective

actions for all discrepancies

had

been

taken.

System turnover from

1l

~I

construction to startup test group and to operations division was

being conducted

in accordance

with established

procedures

and

administrative controls.

No items of noncompliance

or deviations

were identified.

6.

Review of Periodic

and

S ecial

Re orts

A review was conducted

by the inspector of the Diablo Canyon Unit

1

Reactor

Containment Building Integrated

Leak Rate Test report for

October

30 - November 1, 1978.

This report also included

a summary

analysis of the Type

B and Type

C penetration tests.

The inspector

,reviewed this report and the supportive information to ascertain

whether this information appears

technically adequate.

The following

documents

were

used in the review:

a 0

Appendix J to 10 -CFR 50, "Primary Reactor

Containment-Leakage

Testing for Hater-Cooled

Power Reactors."

b.

American National Standard

N45.4-1972,

"Leakage

Rate Testing

of Containment Structures for Nuclear Reactors."

r

c.

Regulatory

Guide 1.68, "Preoperational

and Initial Startup

Test Programs for Hater-Cooled

Power Reactors."

d.

Topical Report BN-TOP-1, Revision

1, "Testing Criteria for

Integrated

Leakage

Rate Testing of Primary Containment Structures

for Nuclear

Power Plants,"

Bechtel

Corporation.

e.

Diablo Canyon Technical Specifications for Unit l.

'I

The inspector's

independent

calculations

over the time period of

the test

(1130 on 10/31/78 to 0730 on ll/ll/78) indicate

a mass

point leak rate of 0.0225 weight percent

per day;

as

opposed

to the

licensee's

figure of 0.0219 weight percent

per day.

Both figures

are within the allowable limit of 0.0354 weight percent per day for

the case of a reduced

pressure

test for the facility based

on a BN-

TOPl test procedure.

No items of noncompliance or deviations

were identified.

7.

Exit Interview

The inspector

met with a senior licensee

representative

on a weekly

basis

and with the representatives

denoted in Paragraph

1

on

February

23,

1979.

The scope

and findings of the inspection were

.

summarized

by the inspector.

h