ML16161A898

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Insp Repts 50-269/87-37,50-270/87-37 & 50-287/87-37 on 870918 & 0921-24.No Violations or Deviations Noted.Major Areas Inspected:Inservice Insp,Including Observation of Ultrasonic Exam of Reactor Vessel flange-to-shell Weld
ML16161A898
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 10/14/1987
From: Blake J, Coley J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16161A899 List:
References
50-269-87-37, 50-270-87-37, 50-287-87-37, NUDOCS 8710270003
Download: ML16161A898 (8)


See also: IR 05000269/1987037

Text

V REG

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

)@

ATLANTA, GEORGIA 30323

Report Nos.:

50-269/87-37, 50-270/87-37, and 50-287/87-37

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242

Docket Nos.: 50-269, 50-270,

License Nos.: DPR-38, DPR-47, and

and 50-287

DPR-55

Facility Name:

Oconee 1, 2, and 3

Inspection Conducted:

September 18 and September 21-24, 1987

Inspector:

)c -ii- P7

J.

Date Signed

Approved by:

M

,o

q'2

J J. lake, Chief

Date Signed

at ials and Processes Section

Division of Reactor Safety

SUMMARY

Scope:

This routine, announced inspection was in the areas of inservice

inspection - observation of the ultrasonic examination of the reactor vessel

flange-to-shell weld, and review of the first interval hydrostatic testing

program for Unit 1 and, IE Bulletin 83-06.

Results:

No violations or deviations were identified.

8710270003 871016

PDR

ADOCK 05000269

PDR

REPORT DETAILS

1. Persons Contacted

Licensee Employees

M. S. Tuckman, Station Manager

  • L. V. Wilkie, Acting Station Manager
  • T. C. Mathews, Regulatory Compliance Specialist
  • W. R. Hunt, QA Engineer - ISI Coordinator
  • D. W. Denard, Performance Engineer
  • A. J. Hogge, Jr., General Office - QA

Other licensee employees contacted included construction craftsmen,

engineers, technicians, operators, mechanics, security force members, and

office personnel.

Other Organization

  • H. Stoppleman, Babcock and Wilcox (B&W) - ISI
  • M. Hacker, B&W -

Level III

NRC Resident Inspector

  • J. Bryant, Senior Resident Inspector
  • Attended exit interview

2. Exit Interview

The inspection scope and findings were summarized on September 24, 1987,

with those persons indicated in paragraph 1 above.

The inspector

described the areas inspected and discussed in detail the inspection

findings.

No dissenting comments were received from the licensee.

The

following new item was identified during this inspection:

(Open)

Unresolved Item 50-269/87-37-01, Hydrostatic Test Boundaries

Uncertain -

paragraph 6.

The licensee did not identify as proprietary any of the materials provided

to or reviewed by the inspector during this inspection.

3. Licensee Action on Previous Enforcement Matters

This subject was not addressed in the inspection.

2

4. Unresolved Items

Unresolved Items are matters about which more information is required to

determine whether .they

are acceptable or may involve violations or

deviations.

One unresolved item identified during this inspection is

discussed in paragraph 6.

5. Ultrasonic Examination of the Oconee Unit 1 Reactor Vessel Flange-to-Shell

Weld (57080)

During the 1986 outage of Oconee Unit 1, an ultrasonic examination of the

reactor vessel flange-to-shell weld was conducted from the flange face. A

total of 22 indications were recorded.

These indications appeared at

several elevations within the area of interest for the weld and all were

recorded from the clad side of the flange.

These indications were

evaluated as subsurface flaws for the purpose of disposition and were

acceptable to the requirements of either IWB-3500 or IWB-3600 of the ASME

Code.

Since these indications were not detected by any previous

examinations and they were not detected from the unclad side of the flange

when using the unclad calibration, there was speculation that they may not

indicate a flaw condition.

Subsequent investigations on a similar weld joint located at the B&W

Mr. Vernon facility indicated that it

was possible to obtain false

indications of similar magnitude to the Oconee indications when examining

through the clad surface of the flange face. The results of these efforts

have been previously documented

(B&W

Document

No.

1163186A-0).

An

improved ultrasonic examination procedure (ISI-187, Rev. 0) was developed

to minimize the occurrence of false indications. This procedure was used

at Oconee Unit 2 during 1986 and resulted in no false indications being

recorded.

The intent of this inspection was to properly characterize the previously

recorded indications on the Unit 1 reactor vessel flange-to-shell weld and

to provide a baseline for future inspections from the flange face.

The ultrasonic (UT)

instrument used during the 1986 examination was the

Krautkramer Model USIP-11. The reliability of the Krautkramer USIP-11 UT

instrument had been a problem for the contractor (B&W)

when used in an

environment where the instrument must be sealed to prevent contamination.

To eliminate the problem, a different UT instrument was used this outage.

The

Panametric Digital

UT

instrument

Model

EPOCH-2002

and the

Krautkramer-Branson, Inc., Model USD-10 were evaluated and compared to the

USIP-11 by B&W and the EPOCH-2002 was selected as the instrument best

suited for the examination.

As stated above, the examination of the flange-to-shell weld had two major

objectives.

The first was to establish a more accurate representation of

the actual condition of the flange-to-shell weld. this was to serve as a

baseline for future examinations.

The second objective was to properly

disposition the 22 indications recorded during the previous outage.

3

Since the examination was

on critical path,

two inspection teams,

designated as Teams A and B, were used for the examination.

Team A

performed the full 360 examination of the flange excluding the previously

recorded indications.

This examination was performed per the requirement

of ISI-187.

The results of this inspection and that performed by Team B

established the new baseline.

Team B was dedicated to the resolution of

the 22 previously recorded indications.

The objective was to duplicate as

closely as possible the examination performed in 1986 utilizing B&W

Procedure ISI-130.

Next, Procedure ISI-187 was used to acquire as much

data as possible using selected transducers of different size, frequency,

and a combination of straight beam and angle beam inspections where access

permitted.

The calibration block used for the examination was block #50304 which was

the same block used in the 1986 examination of Unit 1 and the examination

of Unit 2.

The following calibration setups were used to conduct the

examinations:

CALIBRATION SET-UPS

CALIBRATION BLOCK 50304

Calibration

Calibration

Number

Transducer

Surface

  1. 1

1" Dia. 0 -

Degree

Full Clad

2.25 mHz

(as welded)

  1. 2

1" Dia. 0 -

Degree

Clad Patch

2.25 mHz

(machined)

  1. 3

1.5" Dia. 0 -

Degree

Clad Patch

5.0 mHz

(machined)

  1. 4

1" Dia. 5 - Degree

Unclad

2.25 mHz

  1. 5

1" Dia. 10 -

Degree

Unclad

2.25 mHz

  1. 6

1" Dia. 15 -

Degree

Unclad

2.25 mHz

  1. 7

1.5" Dia. 0 -

Degree

Full Clad

5.0 mHz

(as welded)

Note calibration #7 was added by the licensee when the inspector noted

that the calibration setup for the 1.5 Dia., 5.0 mHz did not evaluate the

reflectors at the same sensitivity as the 1986 examinations. The setup in

the inspection plan was using the machined clad patch as the surface for

calibration in lieu of the "as welded" full clad surface.

The difference

between these surfaces represents approximately a 30 decibel drop with the

'@

4

as welded full clad calibration being the more sensitive examination.

In

NRC's safety evaluation report for Unit 1, NRC informed the licensee to

treat the reflectors in the weld as real cracks in reactor vessel and that

the issue could not be resolved by simply reducing the instrument gain

such that the flaws indications were no longer recordable by ASME

Section XI criteria.

Calibration #3 in the B&W plan did exactly that for

the evaluations using a 1.5 Dia., 5 mHz transducer. After the inspector

discussed the situation with the licensee's corporate QA technical

supervisor, the licensee decided to add calibration #7.

The inspector observed the UT calibrations, the examinations of the

vessel-flange weld,

and portions of each evaluation process.

The

examination process started approximately 1:00 a.m.,

on September 22,

1987, and completed at approximately 9:00 p.m., the same night. A break

of approximately four hours was taken when one examiner who was recording

data was overcome by the heat in the canal.

Prior to leaving the site on September 24,

1987, the inspector reviewed

B&W's preliminary examination data.

The re-examination of the flange

using the same techniques as the 1986 examinations were basically

representative of the previous examination with one exception where one

indication representing 500 DAC during the 1986 examination was less than

20 DAC during the present outage.

In this case, the examiner apparently

was not in the correct position; however, calibration #7 recorded the

indication at 70 DAC which is approximately the expected amplitude using

the larger transducer with a higher frequency to reduce the sound beam

spread. During the 1986 inspections, there was only one team of examiners

and they had to wear respirators which inhibited their ability to

communicate. This probably would account for the differences noted in the

recorded data. Calibration #7 still recorded five of the 22 reflectors;

however, their size and amplitude were reduced from that previously

recorded and angle beam calibrations (#4, #5, and #6) from the unclad

surface of the flange did not detect any of the five reflectors.

Calibrations #2 and #3, which include the new baseline, did not detect any

indication over 50% DAC.

B&W's preliminary evaluation of the data was that the reflectors are

caused by the geometry of the forged flange and the examination of the

flange in the 1986 examinations had been at too high a sensitivity level

to obtain meaningful results.

Although, the preliminary data appears to

support B&W's position, the inspector advised the licensee to be very

conservative in their evaluation approach to the five reflectors recorded

in the #7 calibration examinations.

The licensee informed the inspector that a final disposition of the

recorded indications would be available for NRC review within two weeks.

Within the area examined, no violations or deviations were identified.

4

5

6.

Review of First Interval Hydrostatic Testing Program - Unit 1 (73755)

The Duke Power Company (DPC)

inservice inspection (ISI)

program for the

first interval examinations and testing of components and piping was

conducted in accordance with the requirements of Section XI of the ASME

Code, 74S75 Edition and Addendas.

Section XI requires that piping and components of boiling and pressurized

water reactor plants be examined and pressure tested for the 40 year

service lifetime of the plant.

These examinations and tests are to be

completed during each of four ten-year intervals.

These ten-year

intervals are calculated from the start date of commercial operation of

the facility.

Oconee Unit 1 started commercial operation on July 15,

1973,

so the first interval examinations and testing should have been

completed in 1983.

However, since Section XI of the ASME Boiler and

Pressure Vessel Code allows extension of the interval of up to one year so

that the interval can be made to correspond to a plant's outage schedule,

the final completion date allowed by the Code for the first interval

examination and testing on Unit 1 would have been July 15, 1984.

The inspector reviewed select test procedures and quality records for the

first interval inspections to determine the adequacy and completeness of

the tests, the test procedures, and the records.

In order to obtain a clear perspective of hydrostatic testing with a

minimum sample, the inspector selected a test procedure from each code

class.

In addition, the sample selected represented two systems that the

inspector had found at other facilities to be susceptible to testing

errors. The following systems were chosen for this review:

System

Test Procedure

Class

Emergency Core Cooling

TT/1/A/450/25

1

Reactor Building Spray

TT/1/A/450/15

2

Reactor Building Cooling

TT/1/A/450/11

3

During the inspector's review of the emergency core cooling system, the

inspector noted isolation valves on instrumentation lines were not listed

in the test procedure valve alignment enclosure.

Failure to list the

position of these valves would normally indicate hydrostatic test boundary

uncertainty.

However, the drawings used by the inspector to perform the

review were updated OFD drawings and all modifications to the system were

incorporated.

The first interval hydrostatic tests were inspected to

marked up PO drawings that were kept in the Charlotte Corporate QA office.

The

licensee's cognizant performance engineer felt that the

instrumentation valves in question,

1RC-21,

1RC-27,

1RC-28,

1RC-33,

1RC-34, 1RC-35, and 1RC-84, were new modifications as a result of TMI, and

therefore,

would not have been listed in the test procedure valve

enclosure verification list. In addition to the instrumentation isolation

boundary valves, valve 1RC-46 was also not on the valve list for the test.

6

This valve should have isolated an instrument line and the reactor

building component drain header during the test.

The licensee felt that

this line may not have been a new modification; however, to resolve these

issues, the marked up PO drawings will have to be sent to the site for the

inspector's review. The inspector reported this item as Unresolved Item

50-269/87-37-01, Procedure Hydrostatic Boundaries Uncertain.

Within the areas examined, no violations or deviations were identified.

7.

IE Bulletin -

Units 1, 2 & 3 (92701)

(Closed)

83-BU-06:

Nonconforming Materials by Tube-Line Corporation

Facilities at Long Island City,

New York; Houston, Texas,

and Carol

Stream, Illinois.

By memoranda

dated November 18

and

December 9, 1983,

the licensee

responded to the action items requested by this Bulletin.

The response

stated that the only Tube-Line (T-L)

material supplied. to Oconee was

installed in the Unit 3 Auxiliary Feedwater System.

The material in

question involved weld-neck flanges, end caps and reducing tees - all of

which were made of carbon steel material.

Tests performed on a sample of

SA-234 WPB material produced from the same heat as the caps and tees, in

Oconee 3, showed the material properties equaled or exceeded the ASME Code

requirement. However, in the case of the three inch (3") weld-neck raised

face flanges, which are located on the risers that lead to the Auxiliary

Feedwater Steam Generator Nozzles, laboratory tests conducted by Babcock

and Wilcox (B&W), and T-L indicated that the material properties did not

meet B&W's purchase specification requirements. Specifically, the yield

and ultimate strength properties were below the

ASME Section III

standards.

The Code of Record, the 1967 USAS B 31.1 Code,

does not

require a specific flange analysis.

However,

it

does require that the

material meet ASTM and B 16.5 standards. The laboratory test results were

essentially identical to the material properties for materials which are

acceptable per ANSI B 16.5 for Oconee.

The reported test results and

Code/ANSI standard requirements are as follows:

Yield KSI at

Tensile KSI at

Ambient To

Ambient To

B&W Specified Material, ASME,

36

70

SA-105

USAS, B31.1/B 16.5 Required

Material Properties

ASTM A-105Gr.1

30

60

Flange Material

31.1

59.8

Properties

4

7

On the basis of these results, the licensee concluded the material meets

B31.1 Code requirements for ASTM A-105 Gr.1 but not ASTM A-105 Gr-11/ASME

SA-105 as specified.

Results of a rigorous analysis used to evaluate the subject flanges,

caused the licensee to conclude that one of the 12 installed flanges did

not meet Code stress allowables for the flange stresses and flange bolt

stresses during operating conditions.

However, the licensee concluded

that, on the basis of these evaluations, Unit 3 could return to power

until the spring 1984 Refueling Outage.

During that outage all the

flanges were visually inspected and checked for hardness.

All material

except one flange was found acceptable and the one that failed was

replaced.

This bulletin remained open,

however, because the licensee

could not provide stress analysis calculations for the inspector's review

and a description of the general concerns as expressed in paragraph 4 of

the bulletin, i.e., short-term and long-term corrective actions as

applicable was not included in the licensee's response.

Supplement

information was provided to the inspector during this inspection and

reviewed by cognizant inspector and this matter is considered closed.