ML16148A823

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Insp Repts 50-269/93-21,50-270/93-21 & 50-287/93-21 on 930627-0724.Violations Noted.Major Areas Inspected:Plant Operations,Surveillance Testing,Maint Activities,Keowee Issues,Insp of Open Items & Review of LER
ML16148A823
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 08/17/1993
From: Binoy Desai, Harmon P, Lesser M, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16148A822 List:
References
50-269-93-21, 50-270-93-21, 50-287-93-21, NUDOCS 9309070262
Download: ML16148A823 (9)


See also: IR 05000269/1993021

Text

RE4

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.: 50-269/93-21, 50-270/93-21 and 50-287/93-21

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.: 50-269, 50-270, 50-287, 72-4

License Nos.: DPR-38, DPR-47, DPR-55, SNM-2503

Facility Name: Oconee Nuclear Station

Inspection Conducted: June 27 - July 24, 1993

Inspector:

2q

tf

k P. E. Harmon, Senior Resident Inspector

Datt Signed

Y B. B Desai, Resident Inspector

Date Signed

- W. K.

rtner, Resident Inspector

Da

Signed

Approved by.

-//9 3

M. 5. esser, Section Chief

Date Signed

SUMMARY

Scope:

This resident inspection was conducted in the areas of plant

operations, surveillance testing, maintenance activities, Keowee

issues, inspection of open items, and review of licensee event

-reports.

Results:

One violation was identified involving an inadequate modification

procedure. The installation instructions and post modification

testing were inadequate and allowed valve 2RC-4 to be rewired with

the open indication light in the safe shutdown facility

disconnected. The modification was implemented in 1990.

9309070262 930818

PDR ADOCK 05000269

G

PDR

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • H. Barron, Station Manager

S. Benesole, Safety Review Manager

  • K. Chea, Instrument and Electrical Section Manager

D. Coyle, Systems Engineering Manager

  • J. Davis, Safety Assurance Manager

T. Coutu, Operations Support Manager

B. Dolan, Manager, Mechanical/Nuclear Engineering

W. Foster, Superintendent, Mechanical Maintenance

J. Hampton, Vice President, Oconee Site

D. Hubbard, Component Engineering Manager

  • H. Lefkowitz, System Engineer

C. Little, Superintendent, Instrument and Electrical (I&E)

M. Patrick,. Regulatory Compliance Manager

B. Peele, Engineering Manager

  • S. Perry, Regulatory Compliance
  • G. Ridgeway, Operations
  • K. Rohde, Electrical Engineer

G. Rothenberger, Operations Superintendent

R. Sweigart, Work Control Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors

b

Harmon

l

Poertner

B. Desai

NRC Personnel

W. Miller

  • Attended exit interview.

2.

Plant Operations (71707)

a.

General

The inspectors reviewed planteoperations throughout the reporting

period to verify conformance with regulatory requirements,

Technical Specifications (TS), and administrative controls.

Control room-logs, shift turnover records, the temporary

modification log and equipment removal and restoration records

were reviewed routinely. Discussions were conducted with plant

operations, maintenance, chemistry, health physics, instrument &

S electrical (I&E), and engineering personnel.

2

Activities within the control rooms were monitored on an almost

daily basis.

Inspections were conducted on day and night shifts,

during weekdays and on weekends. Inspectors attended some shift

changes to evaluate shift turnover performance. Actions observed

were conducted as required by the licensee's Administrative

Procedures. The number of licensed personnel on each shift

inspected met or surpassed the requirements of TS. Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a

routine basis. During the plant tours, ongoing activities,

housekeeping, security, equipment status, and radiation control

practices 'were observed

b.

Plant Status

Unit 1 operated at power during the entire reporting period.

Unit 2 commenced the reporting period in a power escalation from a

scheduled refueling outage and operated at power during the

remainder of the reporting period.

Unit 3 operated at power during the entire reporting period.

c.

Unit 2 Loss of Seal Injection

On June 30, 1993, at approximately 10:30 a.m., the Unit 2 control

room operator received a call from maintenance personnel

indicating that the packing gland stud for valve 2HP-64, reactor

coolant pump 2A1 seal injection throttle valve, had broken during

maintenance activities to adjust the packing gland. Approximately

two minutes later the packing blew out of the valve, resulting in

a contaminated seal injection system leak of approximately 25 gpm

into the auxiliary building and a subsequent contamination of two

workers in the area. The operators in the control room entered

abnormal operating procedure AP/2/1700/14, Loss of Normal Makeup

or Letdown. The operators isolated seal injection to all four

reactor coolant pumps and secured and isolated high pressure

injection (HPI) pump 2B to terminate the leakage. The RCS leak

was effectively terminated at approximately 11:00 a.m.

The

licensee determined that approximately 550 gallons of water had

spilled into the auxiliary building due to the packing leak from

2HP-64.

During the event the operators increased component cooling water

flow to the reactor coolant pump seals and stationed an operator

to monitor seal temperatures and flows until seal injection could

be reestablished. Seal temperatures increased approximately 30

degrees and stabilized. The licensee replaced the broken packing

gland stud and established normal reactor coolant pump seal

injection at approximately 10:38 p.m.

3

The licensee made a four-hour nonemergency event notification to

the NRC operations center at 12:58 p.m. The notification was made

because the licensee started the 2A HPI pump prior to securing and

isolating the 2B HPI pump. The licensee's initial interpretation

was that a manual engineered safety features actuation had

occurred when the second HPI pump was started. The licensee later

determined that the event was not reportable and retracted the

notification on July 20, 1993, after discussions with the NRC.

The licensee plans to submit a special report describing the event

and subsequent actions.

The licensee sent the failed studs to the materials lab for a

failure analysis. Preliminary results indicate that the stud

failure was induced by hydrogen embrittlement possibly caused by

an inadequately heat-treated cadmium-plated stud. Additionally,

there are indications that misalignment may result when the

packing is tightened. The licensee is still reviewing this item

and has initiated the problem investigation process to resolve and

document the problem.

d.

Unit 3 Low Pressure Service Water Pump Failure

On June 30, 1993, at 4:11 a.m., low pressure service water (LPSW)

pump 3A tripped during normal operation while energized and

supplying flow to the Unit 3 LPSW system.

LPSW pump 3B was

available for operation during this event.

Concurrent with the

trip at 4:11 a.m. several alarms were received in the Unit 3

control room and a momentary dimming of the control room lighting

occurred. The control room operators observed that the LPSW

header pressure low alarm was illuminated and that the 3A LPSW

pump had tripped. The operators immediately started the 3B LPSW

pump to restore flow and dispatched a non-licensed operator (NLO)

to the turbine building to investigate the 3A LPSW pump trip. The

NLO found the 3A LPSW pump motor discolored and the power leads

separated from the motor. The NLO also found the pump motor

breaker tripped from an instantaneous overcurrent on the X phase.

The licensee declared the 3A LPSW pump inoperable and commenced

preparations to replace the pump motor with a spare motor. -With

the 3A LPSW pump inoperable the licensee entered a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

limiting condition for operation (LCO). The licensee replaced the

3A LPSW pump motor and returned the pump to service at 11:46 p.m.

the same day.

The licensee determined that the 3A LPSW pump failed because of

pump motor winding insulation breakdown, which caused a short on

the X phase motor winding. The 3A LPSW motor had been installed

during initial plant construction and had not shown signs of

excessive degradation or wear prior to failing.

Se.-

Pressurizer Block Valve Open Indication not Available in the Safe

Shutdown Facility.

04

On June 30, the licensee determined that valve 2RC-4, pressurizer

relief block valve, had not been stroked from the safe shutdown

facility (SSF) before Unit 2 was returned to operation from the

scheduled refueling outage. PT/2/A/600/24, SSF Valve Control

Transfer Verification, was performed prior to restart of the unit;

however, the procedure step requiring that 2RC-4 be cycled from

the SSF control room contains a caution statement that the step

should not be performed if the pressurizer PORV is being utilized

as the low temperature overpressure requirement. Based on this

statement 2RC-4 was not cycled from the SSF control room. There

was nothing in the procedure to ensure that valve 2RC-4 is stroked

prior to startup.

While performing the PT on June 30 the operators noted that the

open indication light for 2RC-4 was not illuminated when power was

transferred to the SSF.

2RC-4 valve position indication at the

SSF is available only when the valve is powered through the SSF

control room. A work request was written to investigate why the

valve open indication light was not illuminated. Subsequent to

the restart of the unit the licensee determined that the valve

open light was not wired. The valve had been rewired in 1990 for

a torque switch bypass modification and the open indication had

been inadvertently deleted.

The inspectors reviewed the modification package for the torque

switch bypass modification and held discussions with design

engineering. Procedure TN/2/A/2622/01/CL5, Torque Switch Bypass

Modification for Valves 2HP-115, 2AS-102, 2MS-47, and 2RC-4,

implemented the design modification that deleted the valve open

indication in the SSF. The procedure was inadequate because the

modification rewired valve 2RC-4 and deleted the valve open limit

switch contacts without instruction to install the required jumper

to provide indication in the safe shutdown facility. The

engineering department was aware that jumper installation was

required and the jumper was indicated on the wiring diagrams.

However, the modification package did not contain instructions to

install the jumper. The modification was implemented and tested

in October 1990 and the post modification testing did not reveal

that the valve was wired incorrectly. The inspectors concluded

that multiple opportunities existed to either prevent or detect

the modification error. The failure to provide adequate

instructions to perform the torque switch bypass modification on

valve 2RC-4 is identified as Violation 270/93-21-01: Inadequate

Modification Procedure.

The licensee evaluated the operability of valve 2RC-4 with the

open indication light not wired and determined that the valve

could still perform its intended function. The licensee is

developing a procedure for installing the required electrical

jumper and cycling the valve from the SSF control room. The

licensee has initiated the problem investigation process and plans

5

to revise PT/2/600/24 to require that valve 2RC-4 be operated from

the SSF control room every refueling outage.

One violation was identified.

3.

Surveillance Testing (61726)

Surveillance tests were reviewed by the inspectors to verify procedural

and performance adequacy. The completed tests reviewed were examined

for necessary test prerequisites, instructions, acceptance criteria,

technical content, authorization to begin work, data collection,

independent verification if required, handling of deficiencies noted,

and review o'f completed work. The inspectors witnessed the tests, in

whole or in part, to verify that approved procedures were available;

test equipment was calibrated; prerequisites were met; tests were

conducted according to procedure; test results were acceptable; and

systems restoration was completed.

a.

MP/1/A/2000/33, Unit 1 Electro Mechanical Relay ACB Trip test.

This procedure prescribes a quarterly test on the electro

mechanical trip circuitry for Keowee Unit 1 air circuit breakers

(ACBs) 1 and 3. The inspectors reviewed the completed procedure

and verified that the acceptance criteria were met.

b.

PT/O/A/0400/05, SSF AuxiliaryService Water Pump Test. This

quarterly pump test is required by ASME Section XI and Technical

Specification 4.20.1. The inspectors witnessed the test

performance and verified that the acceptance criteria were met and

were in accordance with the licensee's inservice inspection

program.

No violations or deviations were identified.

4.

Maintenance Activities (62703)

Maintenance activities were observed and/or reviewed during the

reporting period to verify that (1)

work was performed by qualified

personnel, and (2) approved procedures adequately described work that

was not within the skill of the trade. Activities, procedures, and work

requests were examined to verify that proper authorization to begin work

was given, provisions for fire were made, cleanliness was maintained,

exposure was controlled, equipment was properly returned to service, and

limiting conditions for operation were met.

WR 38915C, Replace 3A LPSW Pump Motor. The inspectors monitored work

activities in progress and reviewed the post maintenance testing

performed prior to returning the pump to service. The work activities

were conducted proficiently and expeditiously.

No violations or deviations were identified.

5.

Keowee Issues

6

The inspector verified that procedural guidance was available for

operators at the Keowee Hydro Station covering emergency and off-normal

situations. Written procedures for abnormal station operations were not

available during the loss of offsite power event of October 19, 1992.

Abnormal Procedure AP/O/A/2000/001, Keowee Station Natural Disasters,

issued January 30, 1990, covers tornados and flooding. This procedure

was the only emergency or abnormal procedure available at the time of

the event.

Abnormal Procedure AP/0/2000/002, Keowee Station Emergency Start, issued

February 23, 1993, covers emergency starts, abnormal alignments, and

failures of the Keowee station to provide emergency power as designed.

This guidance includes verification of proper operation and alignments,

actions to manually align and start equipment, and notification to the

Oconee control room and Keowee technicians if actions taken are

unsuccessful.

Included in this procedure are instructions for the

Oconee control room to dispatch an Oconee operator to the Keowee station

to align the "Local-Remote" switch on the Keowee panel to "Remote" if

the Keowee operator is unable to start the Keowee units during emergency

situations. Transferring the controls to Remote allows operators to

manually start the Keowee units from the Oconee control room.

6.

Inspection of Open Items (92701) (92702)

The following open items were reviewed using licensee reports,

inspection record review, and discussions with licensee personnel, as

appropriate:

a.

(Closed) Violation 269/92-23-01: Containment Isolation Valve

Found Open. The licensee responded to this violation by letter

dated November 18, 1992. Licensee Event Report (LER) 269/92-13

was.also submitted to the NRC. The inspector reviewed the

corrective actions stated in the LER as well as the violation

response. Based on the inspector's review of the actions

pertaining to LER 269/92-13 as described in paragraph 7.a of this

report, this item is closed.

b.

(Closed) Unresolved Item 269,270,287/92-23-02: Keowee Single

Failure Criteria. This item addressed single failure requirements

for the Keowee emergency power sources and power paths. The

electrical distribution system functional inspection (EDSFI)

reviewed the operation and single failure requirements for the

Keowee units and emergency power paths. Based on the EDSFI review

the inspectors consider this item closed.

7.

Review of Licensee Event Reports (92700)

The Licensee Event Reports (LERs) listed in this section were reviewed

to determine if the information provided met NRC requirements. The

inspector considered the adequacy of description, compliance with

Technical Specification and regulatory requirements, corrective actions

7

taken, existence of potential generic problems, reporting requirements

satisfied, and the relative safety significance of each event. The

following LERs were reviewed:

a.

(Closed) LER 269/92-13, Technical Specification Violation Due to

Lack of Containment Integrity Resulting From A Defective

Procedure. Containment isolation valve 1N-107 was discovered in

the open position on September 8, 1992. The valve was immediately

returned to its closed position as required. The valve had been

in the open position since June 1992. A defective procedure was

identified as the root cause of the valve being in an abnormal

position. The inspectors verified that the following corrective

actions were taken to prevent recurrence:

-

OP/1/A/1103/02, RCS Filling and Venting, was revised to

require the valve to be verified closed.

-

OP/1/A/1102/01, Controlling Procedure for Unit Startup, was

revised to prescribe the performance of the containment

integrity checklist after procedures that affect manual

containment isolation valves have been completed.

b.

(Closed) LER 269/92-04, Reactor Trip Results From Low Main

Feedwater Pump Discharge Pressure Due to Management Deficiency.

The reactor trip that occurred on May 8, 1992, was caused by less

than-adequate'training and lack of a task specific procedure. The

inspectors verified the following corrective actions to prevent

recurrence:

OP/1/A/1106/02, Condensate and Feedwater System, was revised

to include guidance on reducing Hotwell level.

-

The Alarm response Manual for Hotwell Level Emergency High

Statalarm (1SA6/C-12) was revised to refer to

OP/1/A/1106/02.

-

The lesson plan for the condensate and feedwater system was

revised to include training on hotwell oscillations.

c.

(Closed) LER 269/92-08, Equipment Failure and Inappropriate Action

Result in the Concurrent Inoperability of Both Onsite Emergency

Power Sources and a Technical Specification Violation. This event

occurred on July 17, 1992. Keowee Unit 1 was out of service for

planned maintenance and Keowee Unit 2 was deemed to be inoperable

when a blown fuse associated with ACB 8 was discovered. Following

the discovery of the inoperability of both Keowee units the

Standby buses were not energized by Lee Gas Turbines within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />

as required by TS.

The blown fuse was eventually replaced and Keowee Unit 2 was

declared operable. The root causes associated with this event

were classified as Equipment Failure and Inappropriate Action.

8

The inspectors verified the following corrective actions

associated with this event.

Keowee's breaker status checklist was revised to include

additional breaker and indicator status for each breaker.

-

OP/O/A/1107/03 was revised to include notification to Lee

Steam Station of the time the gas turbines are required to

be in service; a notification step also was included earlier

in the procedure.

-

Training was given to Lee Steam Station personnel concerning

initiating a start of the second gas turbine if the primary

turbine does not start or trips after initial start.

-

A rounds and turnover procedure was initiated to enhance

monitoring of Keowee Hydro equipment.

Training was given to Keowee personnel on the new Keowee

procedures, checklists, and the time constraints of

Technical Specifications.

-

A root cause analysis was performed on the failed fuse.

Though the results were not conclusive, the licensee decided

to phase out this type of fuse. No target date has been

established.

-

The inspectors reviewed PIP 92-293, which is investigating

the possibility of modifying the circuit associated with

breaker indication.

8.

Exit Interview

The inspection scope and findings were summarized on July 27, 1993, with

those persons indicated in paragraph 1 above. The inspectors described

the areas inspected and discussed in detail the inspection findings.

The licensee did not identify as proprietary any of the material

provided to or reviewed by the inspectors during this inspection.

Item Number

Description/Reference Paragraph

Violation 270/93-21-01

Inadequate Modification Procedure

(Paragraph 2.e).