ML16148A535

From kanterella
Jump to navigation Jump to search
Forwards Insp Repts 50-269/91-15,50-270/91-15 & 50-287/91-15 on 910709-11.No Violations or Deviations Noted
ML16148A535
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 08/08/1991
From: Cline W
NRC Office of Inspection & Enforcement (IE Region II)
To: Tuckman M
Duke Power Co
Shared Package
ML16148A536 List:
References
NUDOCS 9109100028
Download: ML16148A535 (7)


See also: IR 05000269/1991015

Text

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-269/91-16, 50-270/91-16 and 50-287/91-16

Licensee:

Duke Power Company

P. 0. Box 1007

Charlotte, NC 28201-1007

Docket Nos.:

50-269, 50-270, 50-287, 72-4

License Nos.:

DPR-38, DPR-47, DPR-55, SNM-2503

Facility Name:

Oconee Nuclear Station

Inspection Conducted: June 30 - July 27, 1991

Inspector:

P. E. Harmon, Senior

s'de

spector

Date Signed

B. B Desi, Rsldent

e~qyDate

Signed

W. K. Poertner Re ' en Is

or

Date Signed

Approved by:

'? 1-g

G. A. tb-sle5=

tion Chief-Dt

i'e

Da e Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine resident inspection was conducted in the areas of

operations, surveillance testing, maintenance activities, and review

of open items.

Results:

No violations or deviations were identified.

9109160028 910829

PDR ADOCK 05000269

PDR

I

REPORT DETAILS

1. Persons Contacted

Licensee Employees

  • H. Barron, Station Manager

D. Couch, Keowee Hydrostation Manager

  • T. Curtis, Compliance Manager
  • J. Davis, Technical Services Superintendent

D. Deatherage, Operations Support Manager

B. Dolan, Design Engineering Manager, Oconee Site Office

W. Foster, Maintenance Superintendent

T. Glenn, Engineering Supervisor

  • 0. Kohler, Compliance Engineer

C. Little, Instrument and Electrical Manager

H. Lowery, Chairman, Oconee Safety Review Group

B. Millsap, Maintenance Engineer

M. Patrick, Performance Engineer

D. Powell, Station Services Superintendent

  • G. Rothenberger, Integrated Scheduling Superintendent
  • R. Sweigart, Operations Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors:

  • P. Harmon
  • W. Poertner
  • B. Desai
  • Attended exit interview.

2. Plant Operations (71707)

a. General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements, Technical

Specifications (TS), and administrative controls.

Control room logs,

shift turnover records, temporary modification log and equipment

removal and restoration records were reviewed routinely. Discussions

were conducted with plant operations, maintenance, chemistry, health

physics, instrument & electrical (I&E), and performance personnel.

Activities within the control rooms were monitored on an almost daily

basis. Inspections were conducted on day and on night shifts, during

weekdays and on weekends.

Some inspections were made during shift

change in order to evaluate shift turnover performance.

Actions

  • I

2

observed were conducted as required by the licensee's Administrative

Procedures.

The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS.

Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a routine

basis. The areas toured included the following:

Turbine Building

Auxiliary Building

CCW Intake Structure

Independent Spent Fuel Storage Facility

Units 1, 2 and 3 Electrical Equipment Rooms

Units 1, 2 and 3 Cable Spreading Rooms

Units 1, 2 and 3 Penetration Rooms

Units 1, 2 and 3 Spent Fuel Pool Rooms

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Keowee Hydro Station

During the plant tours, ongoing activities, housekeeping, security,

equipment status, and radiation control practices were observed.

Within the areas inspected, licensee activities were satisfactory.

b. Plant Status

Unit 1 operated at power for the entire reporting period.

At

10:30 a.m., on July 28, a milestone was reached by Unit 1. This Unit

became the first nuclear unit in the country to reach the 100 million

megawatt-hours of electricity.

Reactor coolant pump 1A1 was secured on July 14,

due to a low oil

level alarm. Power level was reduced to approximately 40 percent to

allow maintenance personnel to enter the reactor building and add oil

to the pump motor.

Oil was added to the pump motor, the pump was

restarted and the unit returned to 100 percent power.

During the

building entry a small fire occurred when a plastic container melted

and approximately 2 tablespoons of oil dropped onto the pressurizer

support stand and flashed. The licensee initiated a task force to

review this event and determine corrective actions to prevent

reoccurrence.

Unit 2 operated at power for the entire reporting period.

Unit 3 operated at power until July 3, when it automatically tripped

on loss of both main feedwater pumps due to low suction pressure.

The unit was returned to service on July 4.

On July 15, the unit

experienced a runback from 100 percent power due to loss of control

rod group 3 out-limit.

Control

Rod Drive

(CRD)

breaker 11

3

replacement was in progress.

The licensee postulated that when the

breaker was opened, the D.C.

hold power to one of the two phases was

isolated which caused the rods to align to the single phase D.C. hold

power supply.

This realignment caused the control rod group 3

out-limit to be lost resulting in the runback.

The runback was

stopped at 71 percent power by taking the Integrated Control System

(ICS) to manual.

The runback was determined to be invalid since the

100 percent lights were on, indicating that the rods had not moved

significantly.

CRD breaker replacement was suspended and the Unit

was returned to 100 percent power.

c. Unit 3 Reactor Trip.

On July 3, Unit 3 tripped from 100 percent power due to the loss of

both Main Feedwater Pumps (MFPs).

The MFPs tripped due to low

suction pressure caused by a failure in the Powdex Master controller

while controlling in automatic that resulted in the powdex outlet

valves closing. During the failure of the Powdex Master controller

the powdex bypass valve controller was in manual and the bypass

valves remained shut. This resulted in the condensate booster pumps

and the MFPs tripping on low suction pressure followed by a reactor

trip signal due to the loss of both MFPs.

The licensee determined that the failure of the Powdex Master

controller was caused by a failed gasket that blocked the outlet port

to the valve relay.

This was perceived as a loss of instrument air

by the controller and the powdex valves closed.

Following the reactor trip and Emergency Feedwater (EFW)

initiation

on loss of both MFPs, the EFW flow control valve (EFDW-315) to the 3A

steam generator failed to control steam generator water level.

The

control room operator took manual control of the valve to maintain

level in the 3A steam generator. The solenoid valve controlling the

automatic function of the flow control valve had not operated

properly.

The solenoid valve was agitated and the controller was

returned to automatic and operated properly. The solenoid valve was

replaced prior to returning the unit to power operation and the

licensee is investigating to determine if more frequent cycling of

the solenoid is appropriate to prevent reoccurrence.

During recovery two main steam relief valves did not reseat within

the guidelines of the post trip review procedure.

Valve 3MS-5 did

not reseat until main steam pressure was lowered to 88 percent of

setpoint and valve 3MS-11 did not reseat until pressure was reduced

to 90 percent of setpoint. The normal value specified in the post

trip review procedure is 93 percent of setpoint. The reseat values

for relief valves 3MS-5 and 3MS-11 were reviewed by mechanical

maintenance and the vendor prior to restart of the Unit.

This issue

was also discussed with Region II personnel on July 8, 1991.

4

During review of the post trip response, the licensee determined that

MFP discharge pressure remained above 750 psig when both MFPs tripped

until the "D" heater drain pumps were secured.

The EFW system

automatically initiates only on the loss of both MFPs.

The loss of

MFPs is sensed by loss of control oil pressure or low MFP discharge

pressure.

The low discharge pressure setpoint is set at 750 psig.

The licensee determined that the discharge pressure of the "D" heater

drain pumps could maintain MFP discharge pressure above the actuation

setpoint for automatic initiation of EFW on low MFP discharge

pressure.

Review of past trips that involved loss of both MFPs

indicated that the heater drain pumps installed in Units 1 and 2

could also maintain discharge pressure above the actuation setpoint.

Based on this determination the licensee reduced power on Units 1 and

2 to approximately 70 percent power and secured the heater drain

pumps to ensure that the EFW pumps would receive an auto start signal

on low MFP discharge pressure on a loss of both MFPs. The restart of

Unit 3 was allowed based on the heater drain pumps remaining secured

or isolated from the condensate system.

The licensee generated a procedure to run the heater drain pumps with

the discharge valve closed and the recirculation valves to the heater

drain tank locked open to determine if this configuration would

preclude MFP discharge pressure from staying above the EFW automatic

initiation setpoint. The procedure was only performed on the Unit 1

heater drain pumps.

The 1D heater drain pump developed a discharge

pressure of 710 psig. The 2D heater drain pump developed a discharge

pressure of 720 psig.

Based on this information, the licensee

determined that at 100 percent power, discharge pressure could still

remain above the initiation setpoint with the recirculation flowpath

open.

The licensee performed an engineering evaluation to raise the

actuation setpoint to 800 psig.

This setpoint change also effected

the actuation setpoint for the Reactor Protection System anticipatory

trip on loss of both MFPs and the ATWS Mitigation System Actuation

Circuitry (AMSAC).

The setpoint change was in the conservative

direction.

The engineering evaluation determined that the maximum

discharge pressure available from the heater drain pumps would be 773

psig based on original manufacturers head curves and that the lowest

possible actuation pressure including instrument inaccuracies would

be 782.8 psig.

The 773 psig discharge pressure was based on pump

dead heading and the licensee agreed to operate with the valves in

the pump recirculation lines locked open.

Review of the engineering calculation determined that design

engineering reviewed five available pump curves for the "D" heater

drain pumps originally installed.

The sixth pump curve was not

available when the engineering calculation was performed.

The

inspector also determined that the pump internals for all the heater

drain pumps had been refurbished and swapped between units so that

the pump curves reviewed were not for the presently installed pump

5

configuration. Subsequent to the evaluation, a sixth pump curve was

obtained and the maximum discharge pressure was below the assumed

value in the engineering evaluation.

When questioned on the

acceptability of only reviewing five pump curves for the original

pump configurations the licensee stated that the value used in the

calculation was based on engineering judgement and conversations with

the pump manufacturer.

The inspector considers the engineering

calculation to support the operation of the heater drain pumps to

have been weak with respect to maximum discharge pressure available

from the heater drain pumps; however, the licensee agreed to operate

with the pump recirculation flowpath open to provide a greater margin

than the calculated values.

Long term corrective actions and

followup of this event will be accomplished by review of the

licensee's LER.

No violations or deviations were identified.

3. Surveillance Testing (61726)

Surveillance tests were reviewed by the inspectors to verify procedural

and performance adequacy. The completed tests reviewed were examined for

necessary test prerequisites, instructions, acceptance criteria, technical

content, authorization to begin work,

data collection, independent

verification where required, handling of deficiencies noted, and review of

completed work.

The tests witnessed, in whole or in part, were inspected

to determine that approved procedures were available, test equipment was

calibrated, prerequisites were met, tests were conducted according to

procedure,

test results were acceptable and systems restoration was

completed.

Surveillances reviewed and witnessed in whole or in part:

IP/O/A/0275/006C Safety Related Functional Test of the MDEFWP

Initiation Pressure Switches

IP/O/A/0275/005I MDEFWP Safety Related Instrumentation

Calibration and System Functional Check

IP/O/B/0275/005B Feedwater System Feedwater Pump Suction and

Discharge Pressure Switch Calibration

PT/1/A/600/01

Periodic Instrument Surveillance

PT/2/A/600/01

Periodic Instrument Surveillance

PT/3/A/600/01

Periodic Instrument Surveillance

PT/2/A/600/12

TDEFWP Performance Test

No violations or deviations were identified.

4. Maintenance Activities (62703)

Maintenance activities were observed and/or reviewed during the reporting

period to verify that work was performed by qualified personnel and that

approved procedures in use adequately described work that was not within

'the skill of the trade.

Activities, procedures, and work requests were

6

examined to verify; proper authorization to begin work, provisions for

fire, cleanliness, and exposure control, proper return of equipment to

service, and that limiting conditions for operation were met.

Maintenance reviewed and witnessed in whole or in part:

WR 53090 Determine valve position upon loss of air for MS-93.

WR 57385 Determine valve position upon loss of air for MS-87

WR 55168 CRD Breaker 3-DC-4 Replacement

No violations or deviations were identified.

5. Review of Licensee Event Report (LER) (92700)

The following LER was reviewed to determine if the information provided

met the NRC requirements.

(Closed)

LER 50-287/91-05: Design Deficiency and Procedure Deficiency

Cause Spurious ATWS System Actuation Resulting in Manual Reactor Trip.

This item was addressed in NRC inspection report 50-269,270,287/91-09 and

the inspectors reviewed the licensee response dated April 30, 1991.

Based

on this review, this item is closed.

6. Exit Interview (30703)

The inspection scope and findings were summarized on July 29, 1991, with

those persons indicated in paragraph 1 above.

The inspectors described

the areas inspected and discussed in detail the inspection findings. The

licensee did not identify as proprietary any of the material provided to

or reviewed by the inspectors during this inspection.

0II