05000270/LER-1980-025-03, /03L-0:on 801217,HPI Pump 2B Declared Inoperable Because Motor Indicated High Upper Bearing Temp.Caused by Personnel Error in Replacing Oil.High Bearing Temp Probably Due to Restricted Cooling Water Flow
| ML16148A405 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 01/30/1981 |
| From: | Jackie Jones DUKE POWER CO. |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| Shared Package | |
| ML16148A406 | List: |
| References | |
| LER-80-025-03L-01, LER-80-25-3L-1, NUDOCS 8102100099 | |
| Download: ML16148A405 (2) | |
| Event date: | |
|---|---|
| Report date: | |
| 2701980025R03 - NRC Website | |
text
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8102100099 DOC.DATE1 81/01/30 NOTARIZED: NO DOCKET #
FACIL:50-270 Oconee Nuclear Station, Unit 2, Duke Power Co, 05000270 AUTHONAME AUTHOR AFFILIATION JONESJ.L, Duke Power Co,.
RECIP.NAME RECIPIENT AFFILIATION Region 2, Atlanta, Office of the Director SUBJECT: LER 80-025/03L-0:on 801217*,28 HPI pump declared Inoperable because motor indicated high upper bearing temp,Cavsed by personnel error in replacing oilqHigh bearing temp probably due to restricted cooling water flow, DISTRIBUTION CODE: A0028 COPIES RECEIVED:LTR.S ENCL SIZE:.
TITLE: Incident Reports NOTES:M Cunningham:all amends to FSAR & changes to Tech Specs, 05000270 AEODOrnstein:1cc.
RECIPIENT COPIES RECIPIENT COPTES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL ACTION:
- REIDR, 04 3
3 INTERNAL: A/D COMP&STRU06 1
1 A/D ENV TECH 07 1
1 A/D MATL & QUO8 1
1 A/D OP REACT009 1
1 A/D PLANT SYSIO 1
1 A/D RAD PROT 11 1
1 A/D SFTY ASSE12 1
1 A/D TECHNOLOG13 1
1 ACC EVAL BR:
14 1
1 AEOD 3
3 ASLBP/J.HARD 1
1 AUX SYS BR 15 1
1 CHEM ENG BR 16 1
1 CONT SYS BR 17 1
1 CORE PERF BR 18 1
1 DIRDIV OF LIC 1
1 DIRENGINEERI20 1
1 DIR,HUM FAC S21 1
1 DIR,SYS INTEG22 1
1 EFF TR SYS BR23 1
I EQUIP QUAL BR25 I
1 GEOSCIENCES 26 1
1 I&C SYS BR 29 1
1 I&E 05 2
2 JORDANE,/IE 1
1 LIC GUID BR 30 1
1 MATL ENG BR 32 1
1 MECH ENG BR 33 1
1 MPA 5
3 NRC PDR 02 1
1 OP EX EVAL BR34 3
3 OR ASSESS BR 35 1
1 POWER SYS BR 36 1
1 8 BR39 1
I REACT SYS BR 40 1
1 01 1
1 REL & RISK A 41 1
1
.SF PROG EVA42 1
1 STRUCT ENG BR44 1
1 SYS INTERAC 845 1
1 EXTERNAL: ACRS 46 16 16 LPDR 03 1
1 NSIC 05 1
1 TERA:DOUG MAY 1
1 FEBT 6
TOTAL NUMBER OF COPIES REWUJ.RED:lLTTR 64 ENCL 6A
.7 0
(7771 F 0U.
S. NUCLEAR RECUL.ATORY COMpAISSION LICENSEE EVENT REPORT EXHIBIT A CONTROL 8LOCK:-
(PLEASE PRINT OR TYPE ALL RECUIRED INFORMATION)
S1 sC cN IE IE 12 1/J0 t0 1-01 010 10 1a -
10 O(4(11 l 1l 7
. LIUCENSER CODE 1 I UCNS NU15 2
23 UCENS8 Type jo 57 CAT 5a CONrT REPORT
.\\
souca L
0J..!J 5 1010 10 7
217 IcJ]
1 211 171 81 0na 10 113 10 1 8 11 DO 61 00CKET NUMBER 6S 69 EVENT OATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROSASLE CONSEQUENCES o 2 I On December 17, 1980, the 2B HPT nump wAs deca1re-d inoperahLe The pump hr I
o 3 jbeen removed from service for a motor oil change. On four consecutive test o ~
J runs after the oil change, the motor indicated high upper bearing temperatures.
ro s IThe pump was returned to service well within the.time permitted. HPI pumps 2A I ro-- Land 2C were available as well as all other ECC systems. Thus this incident wasi o of no sighificance with respect to safe operation, and the health and safety
- - o7 8
of the public were not affected.
7 89 so SYSTEM
CAUSE
CAUSE Comp.
VALVV ccoa coo l SUSCOoe COMPONENT Cooe SUacoo SU BCTD FOT-91I S I F j(
LJ @ ILCJ@ [ MFOITIO[RIXl~g UI LIZ(1 7
9 9
o 111 o
92 TYEA t-UENAL OCCUROReNCE REPORT REVIS2O.
REPORT 18 10 1-1 02502 L 5 NUNS E7 234 215 27 23 2
30 31 32 AC71ON FTURE EPPECT SHUTDOWN~T ATTrACHMENT NPIRO-4 PRIME =fMp.
COMPONENT TAKEN ACTION ON PLUJT METWOO HOs SUIIPAIT71 fOawua.
SuprP EA MNUFACTUJRER 01 0,10 1
[Yj 23 1y(B4 L
LX 19 19 9l--
1iJ~J aO Ji G0O0 I Z~J W20 Wi 10199 CAUSE DESCRIPT1ON AND CORRECnVE ACT1ONS 4
[The cause of this incident was the result of personnel being confused and doingj I the wrong things.
The exact cause for the high temperatures is not known.
[Personnel have been instructed not to perform actions that they know are not [correct. Future corrective action are planned to have appropriate personnel 4 review the incident and to try to correct the problem with the high bearing 7
a ste eratures.
STATUS
% POWQR OTHER STATUS OISCOVEAY DISCOVERY OE3CRIpTIo 1,-
7 ItJ 0
IF 1
L 9
91 NA J
Operations Observation 7
a69 to 12 13 44 46 44s ACTIVITY CONTENT NEA31O OP RILLAS AMAOUNT OF ACTIVITY LOCATION oF RELEASE ElfLi (9LZJIL-NA
- - 1N 7
69 10t 11
__4_
PERSONN1L EXPOSURES NUMBER TYPe DeSCRIPTION S El 1 LLQ of o 6 NA 7
6 9 11 12 13 P"RSONNEL INJUR1 ES NUMBER OeSCRIPTION 7EI lO o
01 i
NA 7
8 9 11 12 LOSS OF OR OAMAGE TO ACILITrY TYPE
DESCRIPTION
E l LJl NA 7
8 9
10 PUBLICITY IssuED OeSCRIPToN NAC USE ONLY to s
so NAME OF PREPARER J.
L.
Jones PHONE: (704) 373-8197 810 2010 094