LER-1980-003, /01T-0:on 800507,deborating Demineralizer Was Placed in Svc While Plant in Cold Shutdown & RCS Drained Down.Rcs Boron Concentration Reduced from 1,895 Ppm to 1,539 Ppm.Apparently Caused by Incorrect Chemistry Records |
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REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8006110326 DOCDATE: 80/06/05 NOTARIZED: NO DOCKET #
FACIL:50-270 Oconee Nuclear Station, Unit 2, Duke Power Co.
05000270 AUTH.NAME AUTHOR AFFILIATION LEWISS.R,.
Duke Power Co.
RECIP.NAME:
RECIPIENT AFFILIATION Region 2, Atlanta, Office of the Director SUBJECT: LER 80-003/01T-0:on 800507,deborating demineralizer was placed in svc while plant in cold shutdown & RCS drained down,RCS boron concentration was reduced from 1895 ppm to 1539 ppm.Apparently caused by incorrect chemistry records.
DISTRIBUTION CODE: A0028 COPIESRECEIVED:LTR I ENCL SIZE:..
n TITLE: Incident Reports, NOTES:
RECIPIENT COPIES RECIPIENT, COPIES ID CODE/NAME LTTR ENCL I CODE/NAME LTTR ENCL ACTION:
05 BC <&
4 INTERNAL:
EGFIL 1
1 02 NRC PDR 1
1 09 2
2 1t MPA 3
3 15 NOVAK/KNIEL
- 1.
- 1.
16 EEB 1
1 17 AD FOR ENGR 1
1 18 PLANT SYS BR 1
1 19 I&C SYS BR 1
1 20 AD PLANT SYS 1
1 22 REAC SAFT BR 1
1 23 ENGR BR 1
I 24 KREGER 1
1 25 PWR SYS BR 1
1 26 AD/SITE:ANAL 1
1 27 OPERA LIC BR 1
1 28 ACDENT ANLYS 1
1 29 AUX SYS BR 1
1 AD/0RP-DOR 1
1 AEOD 10 10 BERLINGERC,.
3 3
DOUG MAY-TERA 1
1 HANAUERrS, 1
1 JORDANPE,/IE 1
1 EXTERNAL: 03 LPDR 1
1 04 NSIC 1
1 29 ACRS 16 16 JUN 12 1980 TOTAL NUMBER OF COPIES REQUIRED: LTTR 60 ENCL 60
0 0
NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7-771 LICENSEE EVENT REPORT EXHIBIT A CONTROL BLOCK: l 11Jl l
l l
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
EE Is I clNIE E 12 ()D 00 1 - 1 0 101 01 01 01 -1010 g 4 1(
l1. 1 0 10iJ 7
a 9
.LICENSEE CODE 14 15 LICENSE NUMBER 25 25 LICENSE Type 30 57 CAT 58 CONT REPORT SOuRCE LIji'10O 5 1 01 010 12171 1(D)10151 01718 10 1(s)101 610 151 810 1()
7 a
so 61 DOCKET NUMBER 8
69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES o 2 I A deborating demineralizer was placed in service while Ocnee 2 was at cold Fo31 shutdown and. the RCS was:.drained down. Chemistry records and the first r5J M4 sample indicated a boron concentration close to that of the RCS. However, oT51 RCS boron concentration was reduced from 1895 ppm to 1539 ppm. A substantial 056 concentration above that necessary for a 1% Ak/k shutdown margin was main tained. This incident was not considered to be significant with respect to o a I-safe operation, and the health and safety of the public were not affected.
SYSTEM
CAUSE
CAUSE CO CODE SUSCODE COMPONENT CODE SUBCODE SUBCOOE 9
(D Uc @ I Zi 1
1 DIEIMI INIX E(9 L
S DG 8
9a0 11 12 1318 19 20 LER/RO EVENTYEAR SEENTAL OCCURDENCE REPORT REVISION.
REP AEOR NT COD 810 NO.
'NUMBELS~
W-1010131 W
L oLJ Lii U-J ILB 4
2228 27 28 2
30 31 32 ATIN A
ENFFECT MT. 0 ATTACHMENT NPRO-A PRIME COMP COMPONENT TA C", O O NP IT ME HD 20U R 23 SUB ITED FORM SU B.
SuppLIER M ANUFACTURER 33 3
s36 37 41 42 4I 4 Z47ZIZ CAUSE DESCRIPTION AND CORRECriVE ACTIONS @o 42 44 0
ILApparently the chemistry records were not up-to-date.
It is possible that an 1-J I equilibrium demineralizer outlet concentration was not reached prior to taking [the first sample. Administrative controls will be developed concerning use L-of the demineralizers, including precluding use while the RCS is drained down.
7 89 FACILITYOFs STATUS SPOWER OTHER STATUS DIOE R
1 SFAISITYSNA U
DMETHCOD OPDSOEYDSCRIPTION
=s I.J@
l9 o10 NA IC
(
RCS Chemistry Sample Analysis ACTIVITY CO TENT 2
13 44 48 46 RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OP RELEASE EE-7 LJ Lz l
n 3
NA NA 7
8 9 10 45 PERSONNEL EXPOSURES sO 1 7
___NUMBER TYPE
DESCRIPTION
NA N
[
M0]
0 0 1 ofo g
(NA 7
8 9 11 17 13 PERSONNEL INJURIES s
ER DESCRIPTIONI 4
N II I0181 NA.
7 8
9 11 12 LOSS OF OR DAMAGE TO FACILITY so TYPE
DESCRIPTION
N IE Z zet NA 7
8 9
10 PUBLICITY s0 ISSUED
DESCRIPTION
NC USE ONLY [F2illLN.JNI NA 0
9 10 Ch mi tr Sapl Analysis9 s
NAME OF PREPARER R
sPHONE (704) 373-8285 8006110326
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| 05000270/LER-1980-003-01, /01T-0:on 800507,deborating Demineralizer Was Placed in Svc While Plant in Cold Shutdown & RCS Drained Down.Rcs Boron Concentration Reduced from 1,895 Ppm to 1,539 Ppm.Apparently Caused by Incorrect Chemistry Records | /01T-0:on 800507,deborating Demineralizer Was Placed in Svc While Plant in Cold Shutdown & RCS Drained Down.Rcs Boron Concentration Reduced from 1,895 Ppm to 1,539 Ppm.Apparently Caused by Incorrect Chemistry Records | | | 05000270/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000270/LER-1980-006-03, /03L-0:on 800625,at 40% Full Power,Valve 2LP21 Failed to Open Electrically on Command.Caused by Loose Setscrew on Motor Driven Pinion.Screw Repaired | /03L-0:on 800625,at 40% Full Power,Valve 2LP21 Failed to Open Electrically on Command.Caused by Loose Setscrew on Motor Driven Pinion.Screw Repaired | | | 05000270/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000259/LER-1980-009, Has Been Cancelled | Has Been Cancelled | | | 05000270/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000270/LER-1980-014-03, /03L-0:on 800822,concentrated Boric Acid Storage Tank Pump Removed from Svc Due to Oil & Flange Leaks.Caused by Torn Oil Seal,Worn Worm Gear,Bad Flange Gasket & Stuck Pressure Relief Valve.Items Replaced | /03L-0:on 800822,concentrated Boric Acid Storage Tank Pump Removed from Svc Due to Oil & Flange Leaks.Caused by Torn Oil Seal,Worn Worm Gear,Bad Flange Gasket & Stuck Pressure Relief Valve.Items Replaced | | | 05000270/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000270/LER-1980-015-03, /03L-0:on 800916,valve 2LP21 Failed to Open During Performance of Engineered Safeguard Channel Test.Caused by Loose Setscrew on Motor Driven Pinion.Screw Repaired | /03L-0:on 800916,valve 2LP21 Failed to Open During Performance of Engineered Safeguard Channel Test.Caused by Loose Setscrew on Motor Driven Pinion.Screw Repaired | | | 05000287/LER-1980-016-03, /03L-1:on 801123,fire Detectors String B-2 Went Into Alarm Condition.Caused by Dust Buildup in Detector. Detector Cleaned & Verified Operable | /03L-1:on 801123,fire Detectors String B-2 Went Into Alarm Condition.Caused by Dust Buildup in Detector. Detector Cleaned & Verified Operable | | | 05000287/LER-1980-016, Forwards LER 80-016/03L-1.Detailed Event Analysis Encl | Forwards LER 80-016/03L-1.Detailed Event Analysis Encl | | | 05000270/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000270/LER-1980-020-03, /03L-0:on 801013,during Performance of Es on-line Test,Valve 2FDW-103 Failed to Close During Cycling.Caused by Failure of Torque Switch.Valve Manually Closed.Bad Torque Switch Replaced | /03L-0:on 801013,during Performance of Es on-line Test,Valve 2FDW-103 Failed to Close During Cycling.Caused by Failure of Torque Switch.Valve Manually Closed.Bad Torque Switch Replaced | | | 05000270/LER-1980-022-01, /01T-0:on 801011,four Holes Were Knocked in Fire Barrier Between Cable Spread Room & Turbine Bldg W/O Establishment of Hourly Fire Watch.Caused by Failure to Provide Proper Notificaion.Hourly Fire Watch Established | /01T-0:on 801011,four Holes Were Knocked in Fire Barrier Between Cable Spread Room & Turbine Bldg W/O Establishment of Hourly Fire Watch.Caused by Failure to Provide Proper Notificaion.Hourly Fire Watch Established | | | 05000270/LER-1980-022, Forwards LER 80-022/01T-0 | Forwards LER 80-022/01T-0 | | | 05000270/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000270/LER-1980-024-03, /03L-0:on 801105,HPI Pump 2B Declared Inoperable Due to High Upper Bearing Temp.Caused by Isolation of Normal Cooling Water Supply to Unit 2 HPI Pumps,Personnel Error, Equipment Malfunction & Design Deficiency | /03L-0:on 801105,HPI Pump 2B Declared Inoperable Due to High Upper Bearing Temp.Caused by Isolation of Normal Cooling Water Supply to Unit 2 HPI Pumps,Personnel Error, Equipment Malfunction & Design Deficiency | | | 05000270/LER-1980-025, Forwards LER 80-025/03L-0 | Forwards LER 80-025/03L-0 | | | 05000270/LER-1980-025-03, /03L-0:on 801217,HPI Pump 2B Declared Inoperable Because Motor Indicated High Upper Bearing Temp.Caused by Personnel Error in Replacing Oil.High Bearing Temp Probably Due to Restricted Cooling Water Flow | /03L-0:on 801217,HPI Pump 2B Declared Inoperable Because Motor Indicated High Upper Bearing Temp.Caused by Personnel Error in Replacing Oil.High Bearing Temp Probably Due to Restricted Cooling Water Flow | | | 05000269/LER-1980-040-01, /01T-0:on 801226,removable Instrument Assembly 40 Count Rate Increased,Apparently Due to Leak in once-through Steam Generator Tube.Caused by High Cycle Fatigue.Tube Replaced.Leak Procedure Implemented | /01T-0:on 801226,removable Instrument Assembly 40 Count Rate Increased,Apparently Due to Leak in once-through Steam Generator Tube.Caused by High Cycle Fatigue.Tube Replaced.Leak Procedure Implemented | | | 05000269/LER-1980-040, Forwards LER 80-040/01T-0.Detailed Event Analysis Encl | Forwards LER 80-040/01T-0.Detailed Event Analysis Encl | |
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